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LOUISIANA PIPELINE ACCIDENTS 2016labucketbrigade.org/sites/default/files/Louisiana Pipeline Accidents 2016 .pdfLOUISIANA PIPELINE ACCIDENTS 2016 These pipeline accidents are reports

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Page 1: LOUISIANA PIPELINE ACCIDENTS 2016labucketbrigade.org/sites/default/files/Louisiana Pipeline Accidents 2016 .pdfLOUISIANA PIPELINE ACCIDENTS 2016 These pipeline accidents are reports
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LOUISIANA PIPELINE ACCIDENTS 2016 

These  pipeline  accidents  are  reports  filed  to  the National  Response  Center,  the  federal  point  of 

contact  for oil  spills.  The  reports were  filed either by an employee of  the company or by a  third 

party who noticed the problem. These accidents include both oil and gas pipelines. 

Total pipeline accidents in 2016: 144 

That is 2.7 per week and doesn’t include the accidents that are not reported. 

SUMMARY: The high number of pipeline accidents from corrosion and leaks shows that pipelines in 

Louisiana  are  in  deplorable  condition.  The  problems  with  the  current  network  of  pipelines, 

including  the high number of accidents and  lack of  information about accidents, should preclude 

permitting of new pipelines, including the Bayou Bridge pipeline. 

FINDING #1 Leaks, holes, ruptures and corrosion were responsible for 48% of all pipeline accidents.  

Cause  Number of reports citing this cause 

Leak / hole / rupture in a pipe  56 

Corrosion  13 

 The most common phrase in these reports is “pinhole leak in a flow line.” The size of these holes seems to vary, from a leak that resulted in a spill of quarts of oil (#20732) to a release visible from the air (#20756).  FINDING #2 There is a lack of information about pipeline accidents.  Forty‐seven of the accidents (33%) had an unknown or unexplained cause. There are few follow up reports and no information about if or when the problems are fixed.   Many of the reports also lack information about how much was released. Others, like one from an underground  pipeline  in  Chipola  (#18990)  provided  confusing  information  of  the  release  of  100 barrels of gasoline. The measurement for gas is gallons. Oil is measured in barrels (or gallons).    FINDING #3 This kind of publicly available information is at risk under a Trump Administration.   Republicans have long attempted to gut publicly available environmental  information such as the Toxic Release Inventory. Louisiana Representative Garrett Graves was the author of a bill to keep  

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   the  public  from  the  oil  lease  auctions.  The  reports  from  the  National  Response  Center  is information the oil industry would likely prefer to be kept out of the public hands.   More information:  The  major  oil  companies  and  small,  privately  owned  firms  are  responsible  for  the  accidents. Texas Petroleum Investment Corporation reported 13% of all the accidents (19). There are several other companies  frequently mentioned  in  the reports,  including Hillcorp, Stone Energy, Shell and ExxonMobil.  Number of oil spills: 85 Number of natural gas spills: 37  Many accidents did not specify if it was oil or gas.  Reports by location: No location names are given in 65 of the reports. 

 Golden Meadow ‐ 7 Venice ‐ 6 Baton Rouge ‐ 3 Grand Isle ‐ 3 Hackberry ‐ 3 Leeville ‐ 3 Abbeville ‐ 2 Chipola ‐ 2 Cypremort Point ‐ 2 Cut Off ‐ 2 Lake Charles ‐ 2 Plaquemine ‐ 2 Port Sulphur ‐ 2 

 Each of the following places was the site of at least one accident:  Amelia,  Augusta,  Belle  River,  Belle  Rose,  Berwick,  Buras,  Calumet,  Cameron,  Church  Point, Delcambre,  Dequince,  Dubach,  Galliano,  Garyville,  Grand  Chenier,  Gueydan,  Intercoastal  City, Johnson  Bay,  Kinder,  Lafitte,  Luling,  Melville,  Meraux,  Morgan  City,  New  Orleans,  New  Roads, Oakdale,  Oil  City,  Plaquemines  Parish,  Port  Sulfur,  Raceland,  Shreveport,  Sibley,  St.  Rose, Stephensville, Sulphur, Theriot, Vienna, Washington, West Lake Verret, Winnsboro       

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    Anticipating industry response  These are small leaks and small amounts being released.  Retort:   1. These are not small amounts.  One report (#19864) noted 25 gallons of oil into Catfish Lake and 

others (see below) show hundreds of gallons.  2. The industry is underreporting. The organization Sky Truth studies the satellite  images of the 

spills in the Gulf of Mexico and frequently adjusts the probable amount released based on the size  of  the  sheen.  For  example,  a  spill  in  the Chandeleur  Sound was  reported  as  8.5  gallons. Based on the satellite imagery, Sky Truth estimated that at least 116 gallons were spilled. 

 

3. Small spills have an impact. The oil industry has been drilling and spilling in Louisiana for nearly a  century.  Seemingly  small  leaks  over  such  a  long  time  have  an  impact.  Additionally,  these accidents are likely to be larger and more frequent than reported since the industry  is  largely self‐policing. 

 It’s in industry’s interest to have its equipment in good shape. It costs them money to lose product.  This  argument  would  seem  to  make  sense,  but  the  facts  do  not  support  this  claim.  The  oil  industry  in Louisiana has an accident problem, both off shore and at its refineries. There were 1,799 accidents through December  of  2016  (this  includes  all  accidents  and  not  just  pipeline  accidents  ‐ http://labucketbrigade.org/sites/default/files/Petrochemical%20Accidents%20Update%2011.18.16%20to%2012.1.16.pdf)  Refineries  reported  3,984  accidents  in  a  ten  year  period (http://www.louisianarefineryaccidentdatabase.org/).  Louisiana has a  lax  regulatory environment. When  the  Inspector General of  the Environmental Protection Agency  reviewed  enforcement  of  environmental  laws  (https://www.epa.gov/sites/production/files/2015‐10/documents/20111209‐12‐p‐0113.pdf) throughout the country, he found the enforcement in Louisiana to be the worst. One of  the  reasons  is cited on page 16: “a culture  in which  the state agency  is expected to protect industry.”  Oil and gas operators make a good bet that there will never be any enforcement on accidents and leaks, and that,  should  there  be  enforcement,  it  will  not  cost  the  company  very  much.  That’s  the  real  economic calculation.  The cost that we  in Louisiana bear  is terrible pollution of our  land, our air and our waterways. People are sick from this pollution. None of those costs factor into the oil industry’s bottom line. 

  

 

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# INCIDENT TITLEINCIDENT DATE LOCATION DESCRIPTION CATEGORY

20825NRC Report: Ethylene near Lake Charles, LA

2016-12-06 07:15:00 Lake Charles, LA

Incident Time: 2016-12-06 07:15:00<br/>Nearest City: Lake Charles, LA<br/>Location: 3330 SANCESS RD.<br/>Incident Type: PIPELINE<br/>Material: ETHYLENE<br/>Medium Affected: SUBSURFACE<br/>Suspected Responsible Party: BOARDWALK LOUISIANA MID-STREAM<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.161389, -93.277222 (Explicit)<br/><b>Report Description</b><br/>**POTENTIAL RELEASE**

RP IS REPORTING A POTENTIAL RELEASE OF ETHYLENE DUE TO UNKNOWN CAUSES (UNDER INVESTIGATION). RP STATED THAT IT IS BELIEVED THAT THE MATERIAL MAY HAVE RELEASED FROM AN UNDERGROUND FLOW LINE. RP STATED THAT DEAD VEGETATION WAS DISCOVERED AT THE LOCATION LISTED BELOW. RP STATED THAT SOIL SAMPLES WERE COLLECTED TO DETERMINE IF THERE WAS A RELEASE. Pipeline

20817NRC Report: Oil: Crude near Stephensville, LA

2016-12-05 03:00:00 Stephensville, LA

Incident Time: 2016-12-05 03:00:00<br/>Nearest City: Stephensville, LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.854444, -91.241389 (Explicit)<br/>Reported Sheen Size: 25 feet by 25 feet (area 625 sq. ft.)<br/>Reported Spill Volume: 10 gallon<br/>SkyTruth Minimum Estimate: 0.02 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A 4" LINE WAS DISCOVERED LEAKING DUE TO CORROSION, THIS RESULTED IN THE DISCHARGE OF 5-10 GALLONS OF CRUDE OIL INTO AN ACCESS CANAL OFF OF WEST LAKE VERETT. Pipeline

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20779NRC Report: Natural Gas near Venice, LA

2016-12-03 04:00:00 Venice, LA

Incident Time: 2016-12-03 04:00:00<br/>Nearest City: Venice, LA<br/>Location: SEE LAT AND LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: STONE ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.961944, -88.695833 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A SEAL DEVELOPED A HOLE ON A TIE-IN PIPELINE THAT CAUSED THE DISCHARGE OF AN UNKNOWN AMOUNT OF NATURAL GAS INTO THE GULF OF MEXICO.

Pipeline

20785NRC Report: Oil: Crude near Venice, LA

2016-12-02 12:45:00 Venice, LA

Incident Time: 2016-12-02 12:45:00<br/>Nearest City: Venice, LA<br/>Location: WEST BAY<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILCORP ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.165278, -89.432222 (Explicit)<br/>Reported Sheen Size: 600 feet by 15 feet (area 9000 sq. ft.)<br/>Reported Spill Volume: 3 gallon<br/>SkyTruth Minimum Estimate: 0.22 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF CRUDE OIL INTO WEST BAY FROM AN OLD OUT OF SERVICE TRANSFER LINE FOR UNKNOWN REASONS. THERE IS ONLY RESIDUAL MATERIAL LEFT IN THE LINE. Pipeline

20780 NRC Report: Oil: Crude2016-11-29 03:15:00 Unspecified

Incident Time: 2016-11-29 03:15:00<br/>Nearest City: LA<br/>Location: BLOCK 32<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ENERGY 21<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.312500, -91.535278 (Explicit)<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE TO A LEAK ON A SALES PIPELINE. RP STATED THE LEAK WAS DISCOVERED ON THE OIL SALES PIPELINE (KAH4600). RP STATED THE LINE HAD DEVELOPED A HOLE ON THE RISER ABOVE THE WATERLINE. THE IMPACT IS THE GULF OF MEXICO. Pipeline

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20718NRC Report: Oil: Crude near Leeville, LA

2016-11-27 12:24:00 Leeville, LA

Incident Time: 2016-11-27 12:24:00<br/>Nearest City: Leeville, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHORELINE S.E. LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.248889, -90.217500 (Explicit)<br/>Reported Spill Volume: 25 gallon<br/><b>Report Description</b><br/>CALLER STATED AN LP LINE LEAKED 25 GALLONS OF CRUDE OIL INTO AN UNNAMED CANAL DUE TO CORROSION. Pipeline

20755NRC Report: Natural Gas near Berwick, LA

2016-11-25 03:35:00 Berwick, LA

Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: COLUMBIA GAS TRANSMISSION<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.692222, -91.260833 (Explicit)<br/><b>Report Description</b><br/>CALLER REPORTED THAT A TRANSMISSION NATURAL GAS PIPELINE RELEASED BUBBLES ON THE RIVER DUE TO UNKNOWN REASONS. Pipeline

20748NRC Report: Natural Gas near Calumet, LA

2016-11-24 02:00:00 Calumet, LA

Incident Time: 2016-11-24 02:00:00<br/>Nearest City: Calumet, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.695000, -91.375278 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS FROM AN UNDER WATER PIPELINE DUE TO UNKNOWN CAUSES. Pipeline

20706NRC Report: Oil: Crude near Raceland, LA

2016-11-23 10:25:00 Raceland, LA

;Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: LAND<br/>Suspected Responsible Party: CENTRAL CRUDE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.758605, -90.553244 (Approximated from street_address)<br/><b>Report Description</b><br/>CALLER IS REPORTING THEY RECEIVED A REPORT THAT A CRUDE OIL PIPELINE IS DISCHARGING MATERIAL ONTO THE GROUND. RESPONSE PERSONNEL ARE EN ROUTE TO INVESTIGATE. Pipeline

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20732NRC Report: Oil: Crude near Venice, LA

2016-11-22 12:15:00 Venice, LA

Incident Time: 2016-11-22 12:15:00<br/>Nearest City: Venice, LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.081667, -89.280000 (Explicit)<br/>Reported Sheen Size: 20 feet by 2 miles (area 4.85 acres)<br/>Reported Spill Volume: 0.4 gallon<br/>SkyTruth Minimum Estimate: 5.18 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A PIN HOLE LEAK IN A FLOW LINE OFF OF A WELL, THIS RESULTED IN THE DISCHARGE OF AN ESTIMATED 1.6 QUARTS. Pipeline

20756NRC Report: Natural Gas near Intercoastal City, LA

2016-11-21 04:30:00 Intercoastal City, LA

Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HARVEST PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.718333, -92.020833 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT WHILE PERFORMING AN OVERFLIGHT THERE WAS SOME BUBBLING NOTICED IN VERMILLION BAY, MAINTENANCE CREW VERIFIED THAT THERE IS A PINHOLE LEAK IN THE SRP NATURAL GAS PIPELINE. CALLER STATES THAT REPAIR ESTIMATES WILL EXCEED THE 50K THRESHOLD Pipeline

20736 NRC Report: Oil: Crude2016-11-21 01:15:00 Unspecified

Incident Time: 2016-11-21 01:15:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.944722, -93.137500 (Explicit)<br/>Reported Sheen Size: 100 feet by 100 feet (area 0.23 acres)<br/>Reported Spill Volume: 5 gallon<br/>SkyTruth Minimum Estimate: 0.25 gallons<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE A PINHOLE LEAK DEVELOPED ON FLOW LINE (WELLHEAD). RP STATED THE EXACT WELL THE FLOW LINE GOES TO IS UNKNOWN. THE IMPACT IS SWEET LAKE.& Pipeline

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20711NRC Report: Oil: Crude near Cameron, LA

2016-11-16 09:00:00 Cameron, LA

Incident Time: 2016-11-16 09:00:00<br/>Nearest City: Cameron, LA<br/>Location: 1236 CAMERON MEADOW OILFIELD ROAD<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ENERGY QUEST 2 LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.786970, -93.630659 (Approximated from route)<br/>Reported Spill Volume: 0.13 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A SIX INCH PIPELINE DEVELOPED A LEAK, RESULTING IN A DISCHARGE OF CRUDE OIL. Pipeline

20734 NRC Report: Natural Gas2016-11-13 05:33:00 Unspecified

Incident Time: 2016-11-13 05:33:00<br/>Nearest City: LA<br/>Location: BLOCK 50<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: KINETICA PARTNERS, LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.403889, -92.158889 (Explicit)<br/><b>Report Description</b><br/>CALLER STATED THAT BUBBLES OF WHAT IS BELIEVED TO BE NATURAL GAS ARE FORMING ON THE SURFACE OF THE WATER APPROXIMATELY 500 FEET FROM A 12" NATURAL GAS PIPELINE. THERE ARE NO SIGNS OF A SHEEN AT THIS TIME. DIVE CREWS ARE BEING ASSEMBLED TO DETERMINE IF THE PIPELINE IS THE SOURCE, OR WHAT THE SOURCE ACTUALLY IS Pipeline

20717NRC Report: Oil: Crude near Lake Charles, LA

2016-11-13 05:00:00 Lake Charles, LA

Incident Time: 2016-11-13 05:00:00<br/>Nearest City: Lake Charles, LA<br/>Location: CITGO REFINERY<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: SUBSURFACE<br/>Suspected Responsible Party: SHELL PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.179167, -93.341389 (Explicit)<br/>Reported Spill Volume: 2 gallon<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE TO A PINHOLE LEAK IN A 24" LATERAL PIPELINE (STEEL). THE IMPACT IS SOIL. RP STATED THE REPAIR COST IS EXPECTED TO EXCEED THE $50,000 THRESHOLD (REPAIR ESTIMATES WERE NOT DETERMINED UNTIL TODAY). Pipeline

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20633 NRC Report: Natural Gas2016-11-03 05:00:00 Unspecified

Incident Time: 2016-11-03 05:00:00<br/>Nearest City: LA<br/>Location: BLOCK: E. CAMERON 293<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SPECTRA ENERGY TRANSMISSION<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.343611, -92.766111 (Explicit)<br/>Reported Sheen Size: 100 feet by 0.5 miles (area 6.06 acres)<br/>Reported Spill Volume: 0.24 gallon<br/>SkyTruth Minimum Estimate: 6.48 gallons<br/><b>Report Description</b><br/>CALLER REPORTED THAT WHILE REPAIRING A PREVIOUS LEAK, THEY PRESSURIZED THE LINE AND SAW A SHEEN THAT THEY THINK IS FROM CORROSION. Pipeline

20616NRC Report: Oil: Crude near Grand Isle, LA

2016-11-01 10:15:00 Grand Isle, LA

Incident Time: 2016-11-01 10:15:00<br/>Nearest City: Grand Isle, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HARVEST PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.289167, -90.929722 (Explicit)<br/>Reported Sheen Size: 20 feet by 20 feet (area 400 sq. ft.)<br/>Reported Spill Volume: 84 gallon<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE TO EQUIPMENT MALFUNCTION. RP IS REPORTING THAT THE PRODUCT CAME FROM A 12" STEEL PIPELINE. THE IMPACTS ARE CONTAINMENT AND MUD LAKE. Pipeline

20596NRC Report: Oil: Crude near Cut Off, LA

2016-10-28 08:15:00 Cut Off, LA

Incident Time: 2016-10-28 08:15:00<br/>Nearest City: Cut Off, LA<br/>Location: 224 EAST 101ST PLACE<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHELL PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.462466, -90.308461 (Approximated from street_address)<br/><b>Report Description</b><br/>CALLER IS REPORTING WHILE CONDUCTING MAINTENANCE ON A PIPELINE, A SPRAY OF OIL OCCURRED, RESULTING IN A DISCHARGE OF CRUDE OIL Pipeline

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20579NRC Report: Oil: Crude near Golden Meadow, LA

2016-10-25 09:00:00 Golden Meadow, LA

Incident Time: 2016-10-25 09:00:00<br/>Nearest City: Golden Meadow, LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.368333, -90.345000 (Explicit)<br/>Reported Sheen Size: 4 feet by 10 feet (area 40 sq. ft.)<br/>Reported Spill Volume: 8 gallon<br/>SkyTruth Minimum Estimate: 0 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A LEAK DEVELOPED ON A 4" FLOW LINE ON THE LL&E NUMBER 234, THIS RESULTED IN THE DISCHARGE OF 8 GALLONS OF CRUDE OIL INTO A MARSH AREA ADJACENT TO CATFISH LAKE. Pipeline

20587NRC Report: Oil: Crude near Theriot, LA

2016-10-25 08:30:00 Theriot, LA

Incident Time: 2016-10-25 08:30:00<br/>Nearest City: Theriot, LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.388889, -90.960833 (Explicit)<br/>Reported Sheen Size: 25 feet by 25 feet (area 625 sq. ft.)<br/>Reported Spill Volume: 0 gallon<br/>SkyTruth Minimum Estimate: 0.02 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THE DISCOVERY OF A 25 X 25 SILVERY SHEEN BUBBLING UP ON THE WATERS SURFACE, SHEEN IS ASSUMED TO BE COMING FROM AN OUT OF SERVICE FLOW LINE. Pipeline

20545

NRC Report: Oil: Light Crude near Cypremort Point, LA

2016-10-21 11:50:00 Cypremort Point, LA

Incident Time: 2016-10-21 11:50:00<br/>Nearest City: Cypremort Point, LA<br/>Location: STATE LEASE WATERS 230<br/>Incident Type: PIPELINE<br/>Material: OIL: LIGHT CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: GULF PORT ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.725026, -91.878225 (Approximated from CITY_STATE)<br/>Reported Sheen Size: 150 feet by 90 feet (area 0.31 acres)<br/>Reported Spill Volume: 0.01 gallon<br/>SkyTruth Minimum Estimate: 0.33 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT AN OUT OF SERVICE FLOW LINE HAD A PINHOLE THAT ALLOWED .0121 GALLONS OF LIGHT CRUDE OIL TO DISCHARGE INTO WEST COTE BLANCHE BAY CREATING A 30 YARD BY 50 YARDS BARELY VISIBLE SHEEN ON THE WATERS SURFACE. Pipeline

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20554NRC Report: Natural Gas near Washington, LA

2016-10-21 07:00:00 Washington, LA

Incident Time: 2016-10-21 07:00:00<br/>Nearest City: Washington, LA<br/>Location: MARTIN LUTHER KING AVE.<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: TOWN OF WASHINGTON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.609346, -92.058733 (Approximated from route)<br/><b>Report Description</b><br/>THE RP IS REPORTING A RELEASE OF NATURAL GAS. RP STATED THERE IS A FIRE ON A 2" STEEL PIPELINE DUE TO UNKNOWN CAUSES. NO REPORTED INJURIES OR EVACUATIONS. Pipeline

20525 NRC Report: Oil: Crude2016-10-14 06:25:00 Unspecified

Incident Time: 2016-10-14 06:25:00<br/>Nearest City: LA<br/>Location: LAT: 29N 59" 33"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITNEY OIL & GAS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.992500, -89.266111 (Explicit)<br/>Reported Sheen Size: 225 feet by 0.68 miles (area 18.6 acres)<br/>Reported Spill Volume: 5.9 gallon<br/>SkyTruth Minimum Estimate: 19.88 gallons<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A 10 INCH BULK LINE DUE TO INTERNAL CORROSION. Pipeline

20510 NRC Report: Natural Gas2016-10-14 02:00:00 Unspecified

Incident Time: 2016-10-14 02:00:00<br/>Nearest City: LA<br/>Location: BLOCK 132<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.251944, -93.965833 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE ARE GAS BUBBLES COMING UP THROUGH THE WATER FROM A PIPELINE. THE CAUSE OF THE RELEASE AND OWNER OF THE PIPELINE ARE UNKNOWN Pipeline

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20512 NRC Report: Natural Gas2016-10-12 12:35:00 Unspecified

Incident Time: 2016-10-12 12:35:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TRANSCANADA/ANR PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.806111, -93.081389 (Explicit)<br/>Reported Spill Volume: 50000 cubic ft<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS FROM A PIPELINE. THE CAUSE IS UNKNOWN. Pipeline

20474 NRC Report: Oil: Crude2016-10-07 08:00:00 Unspecified

Incident Time: 2016-10-07 08:00:00<br/>Nearest City: LA<br/>Location: CHANDELEUR SOUND<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: COX OPERATING LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.701389, -89.389722 (Explicit)<br/>Reported Sheen Size: 1.5 miles by 600 feet (area 109.09 acres)<br/>Reported Spill Volume: 8.5 gallon<br/>SkyTruth Minimum Estimate: 116.63 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A LEAK DEVELOPED ON A FLOW LINE ASSOCIATED WITH WELL 12503 NUMBER 1. RESULTING IN THE DISCHARGE OF 8.5 GALLONS OF CRUDE OIL INTO THE GULF OF MEXICO. Pipeline

20476NRC Report: Natural Gas near Baton Rouge, LA

2016-10-05 08:08:00 Baton Rouge, LA

Incident Time: 2016-10-05 08:08:00<br/>Nearest City: Baton Rouge, LA<br/>Location: 12318 LEON IDAS DR<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.557444, -91.166186 (Approximated from street_address)<br/><b>Report Description</b><br/>CALLER STATED THAT THEY RECEIVED A REPORT OF AN INDIVIDUAL WHO STRUCK A NATURAL GAS PIPELINE BREAKING A REGULATOR WHICH CAUSED AN UNKNOWN AMOUNT OF RELEASE OF NATURAL GAS. THE INCIDENT CAUSED AN EXPLOSION WHICH IN TURN DAMAGED A NEARBY HOUSE AS WELL AS STARTED A FIRE. Pipeline

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20477

NRC Report: Drilling Brine (With Zinc Salts) near Belle River, LA

2016-10-05 01:00:00 Belle River, LA

Incident Time: 2016-10-05 01:00:00<br/>Nearest City: Belle River, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: DRILLING BRINE (WITH ZINC SALTS)<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HELLES OIL & GAS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.883056, -91.301111 (Explicit)<br/><b>Report Description</b><br/>THE RP IS REPORTING A RELEASE OF SALT WATER DUE TO A PINHOLE LEAK IN THE SALT WATER LINE. RP STATED THAT THE PIPELINE LEADS TO THE WILLIS COVE PRODUCTION FACILITY. THE IMPACT IS LITTLE BAYOU LONG. Pipeline

20470 NRC Report: Oil: Crude2016-10-03 11:45:00 Unspecified

Incident Time: 2016-10-03 11:45:00<br/>Nearest City: LA<br/>Location: WEST BAY<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILCORP ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.108889, -89.373056 (Explicit)<br/>Reported Sheen Size: 5 feet by 50 feet (area 250 sq. ft.)<br/>Reported Spill Volume: 42 gallon<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE TO FLUSHING AN ABANDONED LINE. RP STATED THAT THE LINE WAS FLUSHED TO ELIMINATE HAZARDS. THE IMPACT IS WEST BAY Pipeline

20419NRC Report: Methane near Plaquemine, LA

2016-10-01 11:15:00 Plaquemine, LA

Incident Time: 2016-10-01 11:15:00<br/>Nearest City: Plaquemine, LA<br/>Location: 21255 HWY 1<br/>Incident Type: PIPELINE<br/>Material: METHANE<br/>Medium Affected: AIR<br/>Suspected Responsible Party: THE DOW CHEMICAL COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.322220, -91.252348 (Approximated from street_address)<br/><b>Report Description</b><br/>FUEL GAS (METHANE) RELEASED FROM A FEED PIPELINE INSIDE THE PLANT DUE TO OVERPRESSURING. Pipeline

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20416 NRC Report: Oil: Crude2016-09-28 10:30:00 Unspecified

Incident Time: 2016-09-28 10:30:00<br/>Nearest City: LA<br/>Location: SOUTH TIMBALIER 301<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHELL PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.158611, -90.667222 (Explicit)<br/>Reported Sheen Size: 12 feet by 30 feet (area 360 sq. ft.)<br/>Reported Spill Volume: 0.13 gallon<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT WHILE PERFORMING A SUBSEA HOT TAP, DIVERS NOTICED BUBBLES OF CRUDE OIL DISCHARGING FROM A PREVIOUS CUT ON THE PIPELINE Pipeline

20302NRC Report: Oil: Crude near Venice, LA

2016-09-21 08:30:00 Venice, LA

Incident Time: 2016-09-21 08:30:00<br/>Nearest City: Venice, LA<br/>Location: STATE LEASE 214<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITNEY OIL & GAS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.080278, -89.160833 (Explicit)<br/>Reported Sheen Size: 30 feet by 30 feet (area 900 sq. ft.)<br/>Reported Spill Volume: 0.01 gallon<br/>SkyTruth Minimum Estimate: 0.02 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF CRUDE OIL INTO GARDEN ISLAND BAY FROM AN UNDERWATER PIPELINE FOR UNKNOWN REASONS. Pipeline

20292 NRC Report: Oil: Crude2016-09-20 10:30:00 Unspecified

Incident Time: 2016-09-20 10:30:00<br/>Nearest City: LA<br/>Location: BLOCK 22L<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ENERGY 21<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.100833, -89.977500 (Explicit)<br/>Reported Sheen Size: 10 feet by 50 feet (area 500 sq. ft.)<br/>Reported Spill Volume: 0.01 gallon<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>CALLER REPORTED THAT DURING DIVE BOAT OPERATIONS A SHEEN WAS DISCOVERED POSSIBLY FROM A 6" PIPELINE DUE TO EQUIPMENT FAILURE. INVESTIGATIONS FOR THE CAUSE ARE STILL UNDERWAY. Pipeline

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20232 NRC Report: Natural Gas2016-09-18 02:45:00 Unspecified

Incident Time: 2016-09-18 02:45:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: PIONEER EXPLORATION LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.057222, -92.688333 (Explicit)<br/><b>Report Description</b><br/>THE RP IS REPORTING THE DISCOVERY OF BUBBLES (NO VISIBLE SHEEN) DUE TO A NATURAL GAS RELEASE IN LAKE ARTHUR. RP STATED THAT IT IS BELIEVED THAT THE SOURCE IS AN UNDERWATER 8" TRANSMISSION PIPELINE. RP STATED THE CAUSE OF THE LEAK IS CURRENTLY UNKNOWN. Pipeline

20229 NRC Report: Oil: Crude2016-09-17 01:20:00 Unspecified

Incident Time: 2016-09-17 01:20:00<br/>Nearest City: LA<br/>Location: BLOCK 608<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ANADARKO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 27.361944, -90.181389 (Explicit)<br/>Reported Sheen Size: 30 feet by 150 feet (area 4500 sq. ft.)<br/>Reported Spill Volume: 1 gallon<br/>SkyTruth Minimum Estimate: 0.11 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT WHEN AN EXPORT PIPELINE WAS BEING BROUGHT BACK ON-LINE THERE WAS A LEAK OF CRUDE OIL ONTO THE DECK OF THE PLATFORM AND INTO THE WATER. Pipeline

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20250 NRC Report: Condensate2016-09-16 07:15:00 Unspecified

Incident Time: 2016-09-16 07:15:00<br/>Nearest City: LA<br/>Location: SHIP SHOAL 27<br/>Incident Type: PIPELINE<br/>Material: CONDENSATE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: W&T OFFSHORE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.131111, -91.114444 (Explicit)<br/>Reported Sheen Size: 50 feet by 600 feet (area 0.69 acres)<br/>Reported Spill Volume: 0.01 gallon<br/>SkyTruth Minimum Estimate: 0.74 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT DURING HYDROTESTING THERE WAS PINHOLE LEAK DISCOVERED ON A 4" NATURAL GAS AND CONDENSATE LINE. THE SECTION WHERE THE LEAK WAS DISCOVERED WAS A RISER THAT WAS EXPOSED TO AIR AT THE PLATFORM. RELEASE IS ONLY AN OILY WATER MIX. RELEASE IS RESIDUAL SALT WATER AND CONDENSATE INTO THE GULF OF MEXICO. PIPELINE SEGMENT IS 9827. Pipeline

20231NRC Report: Oil: Crude near Galliano, LA

2016-09-13 05:05:00 Galliano, LA

Incident Time: 2016-09-13 05:05:00<br/>Nearest City: Galliano, LA<br/>Location: EAST 101 PLACE<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: LOOP LLC.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.462406, -90.309735 (Approximated from route)<br/>Reported Sheen Size: 16 feet by 60 feet (area 960 sq. ft.)<br/>Reported Spill Volume: 0.01 gallon<br/>SkyTruth Minimum Estimate: 0.02 gallons<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE TO A LEAK FROM A STEM CELL VALVE (FLOW VALVE 6461). RP STATED THAT THE VALVE IS ON A PIPING MANIFOLD (FLOW LINE). RP STATED THAT A PRIVATE CANAL WAS IMPACTED (TRIB OF BRETON CANAL). Pipeline

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20237NRC Report: Oil: Crude near Buras, LA

2016-09-12 06:35:00 Buras, LA

Incident Time: 2016-09-12 06:35:00<br/>Nearest City: Buras, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: COX OPERATING LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.419167, -89.486111 (Explicit)<br/>Reported Sheen Size: 300 feet by 600 feet (area 4.13 acres)<br/>Reported Spill Volume: 0.35 gallon<br/>SkyTruth Minimum Estimate: 4.42 gallons<br/><b>Report Description</b><br/>CALLER STATED THAT A 90 DEGREE ELBOW IN A FLOW LINE 36D DEVELOPED A PIN HOLE LEAK WHICH CAUSED A DISCHARGE OF 1.4 QUARTS OF CRUDE OIL TO QUARANTINE BAY Pipeline

20217 NRC Report: Natural Gas2016-09-08 08:18:00 Unspecified

Incident Time: 2016-09-08 08:18:00<br/>Nearest City: LA<br/>Location: SEE LAT - LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.353611, -92.771389 (Explicit)<br/><b>Report Description</b><br/>CALLER REPORTED NATURAL GAS BUBBLES FROM AN UNKNOWN SOURCE ON THE GULF OF MEXICO OBSERVED DURING AN OVER FLIGHT OF THE AREA Pipeline

20208 NRC Report: Natural Gas2016-09-08 02:30:00 Unspecified

Incident Time: 2016-09-08 02:30:00<br/>Nearest City: LA<br/>Location: BLOCK 293<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SPECTRA ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.343611, -92.766111 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS FROM A PIPELINE. THE CAUSE OF THE INCIDENT IS UNKNOWN. THIS IS RELATED TO NRC REPORT 1158470 Pipeline

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20191 NRC Report: Oil: Crude2016-09-07 02:55:00 Unspecified

Incident Time: 2016-09-07 02:55:00<br/>Nearest City: LA<br/>Location: SP BLOCK 28<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITNEY OIL & GAS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.992500, -89.266111 (Explicit)<br/>Reported Sheen Size: 30 feet by 60 feet (area 1800 sq. ft.)<br/>Reported Spill Volume: 0 gallon<br/>SkyTruth Minimum Estimate: 0.04 gallons<br/><b>Report Description</b><br/>CALLER REPORTED THAT THEY WERE DECOMMISSIONING A 12 INCH PIPELINE, REMOVED A FLANGE AND OIL DISCHARGED INTO THE GULF OF MEXICO. Pipeline

20216

NRC Report: Oil: Crude near West Lake Verret, LA

2016-09-06 01:13:00 West Lake Verret, LA

Incident Time: 2016-09-06 01:13:00<br/>Nearest City: West Lake Verret, LA<br/>Location: SEE POSITION (NEAREST FACILITY)<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WIDEOAK OPERATING<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.854444, -91.241389 (Explicit)<br/>Reported Spill Volume: 42 gallon<br/><b>Report Description</b><br/>THE RP IS REPORTING A DISCHARGE OF CRUDE OIL DUE TO A HOLE CAUSED BY CORROSION ON A FLOW LINE. RP STATED THAT THE SIZE OF THE FLOW LINE IS UNKNOWN. THE IMPACT IS SWAMP AREA OF WEST LAKE VERRET. Pipeline

20205NRC Report: Oil: Crude near Grand Isle, LA

2016-09-05 10:40:00 Grand Isle, LA

Incident Time: 2016-09-05 10:40:00<br/>Nearest City: Grand Isle, LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HARVEST PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 89.807778, -89.319167 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A DREDGE BARGE STRUCK A 12" PIPELINE RESULTING IN THE DISCHARGE OF AN UNKNOWN AMOUNT OIL INTO THE GULF OF MEXICO. Pipeline

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20222NRC Report: Unknown Oil near Grand Isle, LA

2016-09-05 08:50:00 Grand Isle, LA

Incident Time: 2016-09-05 08:50:00<br/>Nearest City: Grand Isle, LA<br/>Location: (SOUTH OF NEW ORLEANS)<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN OIL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: GREAT LAKES DREDGE & DOCK CO LLC.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.318611, -89.814167 (Explicit)<br/>Reported Spill Volume: 420 gallon<br/><b>Report Description</b><br/>CALLER STATED COMPANY WAS PERFORMING EXCAVATION WORK ON A MARSH BUGGY (A PIECE OF EQUIPMENT THAT FLOATS), WHEN AN UNDERWATER PIPELINE WAS STRUCK. Pipeline

20166 NRC Report: Oil: Crude2016-09-03 07:20:00 Unspecified

Incident Time: 2016-09-03 07:20:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.284722, -89.098611 (Explicit)<br/>Reported Sheen Size: 200 feet by 6 miles (area 145.45 acres)<br/>Reported Spill Volume: 9.5 gallon<br/>SkyTruth Minimum Estimate: 155.5 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A LEAK DEVELOPED ON A SIX INCH FLOW LINE, RESULTING IN A DISCHARGE OF CRUDE OIL. Pipeline

20160 NRC Report: Oil: Crude2016-09-02 09:30:00 Unspecified

Incident Time: 2016-09-02 09:30:00<br/>Nearest City: LA<br/>Location: SEE LAT - LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITE OAK OPERATING<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.851389, -91.222222 (Explicit)<br/>Reported Spill Volume: 42 gallon<br/><b>Report Description</b><br/>CALLER REPORTED A FLOW LINE LEAK AT THE WEST LAKE VERRET FACILITY DUE TO AN EQUIPMENT FAILURE DISCHARGING 1 BARREL OF CRUDE OIL INTO AN UNNAMED CANAL. Pipeline

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20180 NRC Report: Oil: Diesel2016-09-01 04:55:00 Unspecified

Incident Time: 2016-09-01 04:55:00<br/>Nearest City: LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: DIESEL<br/>Medium Affected: OTHER<br/>Suspected Responsible Party: FIELDWOOD ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.309167, -90.070278 (Explicit)<br/>Reported Spill Volume: 0 gallon<br/><b>Report Description</b><br/>ONE (1) DROP OF DIESEL DISCHARGED FROM A 2" PIPELINE, DUE TO UNKNOWN CAUSES. Pipeline

20114NRC Report: Unknown Oil near Oil City, LA

2016-08-27 09:00:00 Oil City, LA

Incident Time: 2016-08-27 09:00:00<br/>Nearest City: Oil City, LA<br/>Location: 119 SOUTH TRDIS AVE<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN OIL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 32.884590, -93.709892 (Approximated from ZIP)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE ARE OIL PIPES THAT RUN ALONGSIDE A DITCH NEAR HER RESIDENCE. CALLER IS REPORTING THAT SOME OF THESE PIPES ARE DRAINING DIRECTLY INTO THE DITCH AND A THICK BLACK OIL CAN BE VISIBLY SEEN POURING OUT. Pipeline

20138NRC Report: Oil: Crude near Port Sulphur, LA

2016-08-24 10:15:00 Port Sulphur, LA

Incident Time: 2016-08-24 10:15:00<br/>Nearest City: Port Sulphur, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SWIFT ENERGY OPERATING<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.485980, -89.700670 (Approximated from CITY_STATE)<br/>Reported Sheen Size: 10 feet by 50 feet (area 500 sq. ft.)<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>CALLER STATED THAT THEY NOTICED A PIN HOLE LEAK IN A 2" BLOW LINE CAUSED BY RUST. THIS RESULTED IN THE DISCHARGE OF 3.8 OZ OF CRUDE OIL INTO THE WATERS OF THE LAKE WASHINGTON. Pipeline

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20142 NRC Report: Oil: Crude2016-08-22 09:15:00 Unspecified

Incident Time: 2016-08-22 09:15:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ALTA MESA SERVICES<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.810278, -91.826667 (Explicit)<br/>Reported Sheen Size: 600 feet by 0.23 miles (area 16.53 acres)<br/>Reported Spill Volume: 34 gallon<br/>SkyTruth Minimum Estimate: 17.67 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A PINHOLE LEAK IN A FLOW LINE RESULTED IN A DISCHARGE OF CRUDE OIL. Pipeline

20080NRC Report: Unknown Material

2016-08-19 11:00:00 Unspecified

Incident Time: 2016-08-19 11:00:00<br/>Nearest City: LA<br/>Location: TERREBONNE BAY<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN MATERIAL<br/>Medium Affected: AIR<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.206389, -90.533889 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF AN UNKNOWN GAS INTO THE ATMOSPHERE FROM AN UNDERWATER LINE FOR UNKNOWN REASONS. A MARKER HAS BEEN APPLIED TO MARK THE SITE. MATERIAL IS BUBBLING UP TO THE SURFACE. Pipeline

20090 NRC Report: Oil: Crude2016-08-19 07:35:00 Unspecified

Incident Time: 2016-08-19 07:35:00<br/>Nearest City: LA<br/>Location: LAT: 29N 18" 36.71"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CRIMSON GULF<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.310278, -89.296944 (Explicit)<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A DRAIN PAN FOR A RECEIVING TRAP DUE TO AN UNKNOWN CAUSE AT THIS TIME. Pipeline

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20073 NRC Report: Oil: Crude2016-08-18 03:30:00 Unspecified

Incident Time: 2016-08-18 03:30:00<br/>Nearest City: LA<br/>Location: WEST CAM 426<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: PETROQUEST<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.702778, -93.324444 (Explicit)<br/>Reported Sheen Size: 10 feet by 15 feet (area 150 sq. ft.)<br/>SkyTruth Minimum Estimate: 0 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF CRUDE OIL FROM A PIPELINE ASSOCIATED WITH A PLATFORM DUE TO A LOOSE FLANGE ON THE LINE. Pipeline

20050NRC Report: Natural Gas near New Orleans, LA

2016-08-18 02:00:00 New Orleans, LA

Incident Time: 2016-08-18 02:00:00<br/>Nearest City: New Orleans, LA<br/>Location: INTERSECTION OF INDUSTRIAL BLVD.<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: ENTERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.986291, -90.066488 (Approximated from intersection)<br/><b>Report Description</b><br/>CALLER REPORTED THAT A PIPELINE RELEASED NATURAL GAS DUE TO UNKNOWN REASONS. INVESTIGATION UNDERWAY. Pipeline

20094NRC Report: Oil: Crude near St. Rose, LA

2016-08-16 12:30:00 St. Rose, LA

Incident Time: 2016-08-16 12:30:00<br/>Nearest City: St. Rose, LA<br/>Location: SHELL METER STATION<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: LAND<br/>Suspected Responsible Party: SHELL PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.949372, -90.320157 (Approximated from CITY_STATE)<br/><b>Report Description</b><br/>CALLER STATED THERE IS A SPILL OF CRUDE OIL COMING FROM AN UNDERGROUND PIPELINE. Pipeline

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20098 NRC Report: Oil: Crude2016-08-16 07:45:00 Unspecified

Incident Time: 2016-08-16 07:45:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CHEVRON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.406389, -89.020000 (Explicit)<br/>Reported Sheen Size: 10 feet by 200 feet (area 2000 sq. ft.)<br/>Reported Spill Volume: 0 gallon<br/>SkyTruth Minimum Estimate: 0.05 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A PINHOLE IN A FLOW LINE DUE TO CORROSION RESULTED IN A DISCHARGE OF CRUDE OIL. Pipeline

20074NRC Report: Oil: Crude near Venice, LA

2016-08-15 08:15:00 Venice, LA

Incident Time: 2016-08-15 08:15:00<br/>Nearest City: Venice, LA<br/>Location: UNNAMED CANAL<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVETSMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.096667, -89.281944 (Explicit)<br/>Reported Spill Volume: 840 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A FLOW LINE LEAKED DUE TO CORROSION RESULTING IN A DISCHARGE OF 20 BARRELS OF CRUDE OIL. Pipeline

20020

NRC Report: Unknown Material near Morgan City, LA

2016-08-14 11:56:00 Morgan City, LA

Incident Time: 2016-08-14 11:56:00<br/>Nearest City: Morgan City, LA<br/>Location: GULF INTERCOASTAL WATERWAY<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN MATERIAL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.685833, -91.191944 (Explicit)<br/><b>Report Description</b><br/>CALLER STATED GAS WAS DISCOVERED BUBBLING IN THE GULF INTERCOASTAL WATERWAY FROM UNKNOWN SOURCES (POSSIBLY AN UNDERWATER PIPELINE). Pipeline

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20005NRC Report: Oil: Crude near Hackberry, LA

2016-08-08 10:50:00 Hackberry, LA

Incident Time: 2016-08-08 10:50:00<br/>Nearest City: Hackberry, LA<br/>Location: BLACK LAKE<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.000556, -93.423333 (Explicit)<br/>Reported Sheen Size: 150 feet by 900 feet (area 3.1 acres)<br/>Reported Spill Volume: 1 gallon<br/>SkyTruth Minimum Estimate: 3.31 gallons<br/><b>Report Description</b><br/>CALLER STATED THERE WAS A SPILL OF CRUDE OIL DUE TO A HOLE IN A FLOW LINE (PIN HOLE LEAK) AT A TANK BATTERY. Pipeline

20006NRC Report: Oil: Crude near Meraux, LA

2016-08-08 04:00:00 Meraux, LA

Incident Time: 2016-08-08 04:00:00<br/>Nearest City: Meraux, LA<br/>Location: 2500 EAST ST. BERNARD HWY<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.930037, -89.943825 (Approximated from street_address)<br/><b>Report Description</b><br/>CALLER STATED TWO BARGES (BARGE GBL 1732B AND BARGE GBL 5030) STRUCK THE DOCK AND NOW THERE IS A DRIP OF CRUDE OIL INTO THE WATER FROM A PIPELINES UNDER THE DOCK. Pipeline

19962NRC Report: Unknown Oil

2016-08-05 07:40:00 Unspecified

Incident Time: 2016-08-05 07:40:00<br/>Nearest City: LA<br/>Location: BRETON SOUND BLOCK 31<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN OIL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.539722, -89.261389 (Explicit)<br/>Reported Sheen Size: 600 feet by 3 miles (area 218.18 acres)<br/>SkyTruth Minimum Estimate: 233.25 gallons<br/><b>Report Description</b><br/>THE RP IS REPORTING A SHEEN THAT WAS SPOTTED COMING FROM THE AREA OF AN UNMANNED BARGE PRODUCTION FACILITY. RP STATED IT APPEARS THAT THE SOURCE IS FROM A FLOW LINE ON THAT PRODUCTION FACILITY. RP STATED THAT THE CAUSE OF THE SPILL IS UNKNOWN.

**RP HAD LIMITED INFORMATION AT THE TIME OF THE REPORT. Pipeline

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19904NRC Report: Natural Gas near Shreveport, LA

2016-07-31 07:00:00 Shreveport, LA

Incident Time: 2016-07-31 07:00:00<br/>Nearest City: Shreveport, LA<br/>Location: 2437 FAIRFIELD AVE.<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 32.488224, -93.749618 (Approximated from street_address)<br/><b>Report Description</b><br/>NATURAL GAS RELEASED FROM A PIPELINE DUE TO AN UNKNOWN CAUSE AT THIS TIME. CALLER STATES THEY FOUND GAS IN THE VICINITY OF AN AREA WHERE THERE WAS A RECENT SHED (OUT-BUILDING) THAT CAUGHT ON FIRE. THE FIRE TOOK PLACE AROUND 1630 AND THEY BEGAN TO DISCOVER GAS MAY BE INVOLVED AROUND 1900. INVESTIGATION IS UNDERWAY. Pipeline

19933NRC Report: Oil: Crude near Cut Off, LA

2016-07-30 10:35:00 Cut Off, LA

Incident Time: 2016-07-30 10:35:00<br/>Nearest City: Cut Off, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TPIC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.476944, -90.240833 (Explicit)<br/>Reported Sheen Size: 3 feet by 25 feet (area 75 sq. ft.)<br/>Reported Spill Volume: 42 gallon<br/>SkyTruth Minimum Estimate: 0 gallons<br/><b>Report Description</b><br/>CALLER STATED THAT A 2" FLOW LINE DEVELOPED A LEAK AT SHELF ENERGY LL NUMBER 27. THE LEAK DISCHARGED LESS THAN 1 BARREL OF CRUDE OIL TO THE MARSH. Pipeline

19932 NRC Report: Natural Gas2016-07-29 02:30:00 Unspecified

Incident Time: 2016-07-29 02:30:00<br/>Nearest City: LA<br/>Location: EAST CAMERON<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: FIELDWOOD ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 27.690833, -93.007500 (Explicit)<br/><b>Report Description</b><br/>CALLER REPORTED THAT THE CREW NOTICED GAS BUBBLES COMING TO THE SURFACE NEAR A 2 INCH DEPARTING FLOW LINE. Pipeline

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19909NRC Report: Oil: Crude & Produced Water

2016-07-28 07:15:00 Unspecified

Incident Time: 2016-07-28 07:15:00<br/>Nearest City: LA<br/>Location: SOUTH MARSH ISLAND<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE & PRODUCED WATER<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CHEVRON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.407500, -91.998056 (Explicit)<br/>Reported Sheen Size: 600 feet by 2 miles (area 145.45 acres)<br/>Reported Spill Volume: 11.36 gallon<br/>SkyTruth Minimum Estimate: 155.5 gallons<br/><b>Report Description</b><br/>CALLER REPORTED THAT A PIN-HOLE LEAK DEVELOPED ON THE RISER PORTION OF THE PIPELINE TO THE PLATFORM DISCHARGING A CRUDE OIL AND PRODUCED WATER MIXTURE INTO THE GULF OF MEXICO. Pipeline

19963NRC Report: Unknown Oil

2016-07-25 12:00:00 Unspecified

Incident Time: 2016-07-25 12:00:00<br/>Nearest City: LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN OIL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.535556, -91.391111 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE WAS A PIPELINE LEAK OF AN UNKNOWN AMOUNT OF OIL THAT THE CALLER DOESN"T BELIEVE WAS REPORTED. CALLER STATES THAT THE SUSPECTED RESPONSIBLE PARTY HAS BEGUN DREDGING IN A MARSH AREA AND HAS RUINED ABOUT AN ACRE OF PROPERTY IN ATTEMPTING TO REPAIR THE LEAK. Pipeline

19829 NRC Report: Oil: Crude2016-07-20 09:20:00 Unspecified

Incident Time: 2016-07-20 09:20:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.373889, -90.290556 (Explicit)<br/>Reported Sheen Size: 100 feet by 300 feet (area 0.69 acres)<br/>Reported Spill Volume: 20 gallon<br/>SkyTruth Minimum Estimate: 0.74 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A THREE INCH FLOW LINE EXPERIENCED A LEAK, RESULTING IN A DISCHARGE OF CRUDE OIL Pipeline

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19879NRC Report: Oil: Diesel near Baton Rouge, LA

2016-07-16 08:50:00 Baton Rouge, LA

Incident Time: 2016-07-16 08:50:00<br/>Nearest City: Baton Rouge, LA<br/>Location: 1621 WINDSOR DR.<br/>Incident Type: PIPELINE<br/>Material: OIL: DIESEL<br/>Medium Affected: LAND<br/>Suspected Responsible Party: SHELL PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.467491, -91.039657 (Approximated from route)<br/>Reported Spill Volume: 420 gallon<br/><b>Report Description</b><br/>DIESEL FUEL DISCHARGED FROM A 16 INCH PIPELINE DUE TO AN UNKNOWN CAUSE AT THIS TIME. Pipeline

19855 NRC Report: Natural Gas2016-07-16 08:45:00 Unspecified

Incident Time: 2016-07-16 08:45:00<br/>Nearest City: LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: FIELDWOOD ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.588056, -92.899444 (Explicit)<br/><b>Report Description</b><br/>CALLER STATED THAT GAS BUBBLES WERE SPOTTED COMING FROM THE WATER 100 FEET NORTH EAST OF THE PLATFORM. THE PIPELINE WAS SHUT DOWN WHICH STOPPED THE BUBBLES. Pipeline

19867 NRC Report: Natural Gas2016-07-15 10:32:00 Unspecified

Incident Time: 2016-07-15 10:32:00<br/>Nearest City: LA<br/>Location: WEST CAM 480<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: SPECTRA ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.533056, -93.171111 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS INTO THE ATMOSPHERE FROM AN UNDERWATER PIPELINE FOR UNKNOWN REASONS. Pipeline

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19830NRC Report: Ethylene near Belle Rose, LA

2016-07-14 12:15:00 Belle Rose, LA

Incident Time: 2016-07-14 12:15:00<br/>Nearest City: Belle Rose, LA<br/>Location: 158 SHELL PIPELINE CT<br/>Incident Type: PIPELINE<br/>Material: ETHYLENE<br/>Medium Affected: OTHER<br/>Suspected Responsible Party: SHELL PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.014709, -91.116247 (Approximated from street_address)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE WAS AN ETHYLENE FIRE AT THE INCIDENT LOCATION DUE TO UNKNOWN CAUSES. PIPELINE AND PUMPING STATION HAVE BEEN SECURED BUT THE FIRE HAS NOT BEEN EXTINGUISHED AT THIS TIME. Pipeline

19888 NRC Report: Oil: Crude2016-07-14 08:15:00 Unspecified

Incident Time: 2016-07-14 08:15:00<br/>Nearest City: LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: IG PETROLEUM<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.932222, -89.423889 (Explicit)<br/>Reported Sheen Size: 50 feet by 50 feet (area 2500 sq. ft.)<br/>SkyTruth Minimum Estimate: 0.06 gallons<br/><b>Report Description</b><br/>AN UNKNOWN AMOUNT OF CRUDE OIL (SUSPECTED LESS THAN 1 BARREL) DISCHARGED FROM A 3" TRANSFER PIPELINE, DUE TO UNKNOWN CAUSES. Pipeline

19864 NRC Report: Oil: Crude2016-07-14 06:20:00 Unspecified

Incident Time: 2016-07-14 06:20:00<br/>Nearest City: LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.373889, -90.290556 (Explicit)<br/>Reported Spill Volume: 25 gallon<br/><b>Report Description</b><br/>CALLER STATED THAT A FLOW LINE ASSOCIATED WITH GOLDEN MEADOW TANK BATTERY NUMBER 15 HAD A PIN HOLE LEAK THAT RESULTED IN A DISCHARGE OF APPROXIMATELY 25 GALLONS OF CRUDE OIL TO CATFISH LAKE. Pipeline

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19889 NRC Report: Oil: Crude2016-07-13 01:30:00 Unspecified

Incident Time: 2016-07-13 01:30:00<br/>Nearest City: LA<br/>Location: GULF OF MEXICO<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: W & T OFFSHORE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.285278, -89.021667 (Explicit)<br/>Reported Sheen Size: 40 feet by 300 feet (area 0.28 acres)<br/>SkyTruth Minimum Estimate: 0.29 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A SPILL OF CRUDE OIL FROM A TWO INCH OFFSHORE PIPELINE DUE TO AN EQUIPMENT FAILURE. Pipeline

19876NRC Report: Natural Gas near Dubach, LA

2016-07-13 01:15:00 Dubach, LA

Incident Time: 2016-07-13 01:15:00<br/>Nearest City: Dubach, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: BOARDWALK PIPELINES/ TEXAS GAS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 32.700220, -92.651581 (Approximated from CITY_STATE)<br/><b>Report Description</b><br/>CALLER STATED DUE TO UNKNOWN CAUSES A TRANSMISSION LINE RUPTURED AND RELEASED AN UNKNOWN AMOUNT OF NATURAL GAS TO THE AIR. CALLER HAD LIMITED INFORMATION, AS HE DID NOT KNOW THE EXACT LOCATION OF THE RELEASE AT THIS TIME. Pipeline

19808 NRC Report: Natural Gas2016-07-06 03:00:00 Unspecified

Incident Time: 2016-07-06 03:00:00<br/>Nearest City: LA<br/>Location: E CAM 2<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: FIELDWOOD ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.683611, -93.210833 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS FROM AN UNDER WATER PIPELINE DUE TO A LEAK IN THE FLOW LINE Pipeline

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19778

NRC Report: Gasoline: Automotive (Unleaded) near Baton Rouge, LA

2016-07-01 09:15:00 Baton Rouge, LA

Incident Time: 2016-07-01 09:15:00<br/>Nearest City: Baton Rouge, LA<br/>Location: BLOUNT RD<br/>Incident Type: PIPELINE<br/>Material: GASOLINE: AUTOMOTIVE (UNLEADED)<br/>Medium Affected: SOIL<br/>Suspected Responsible Party: EXXON MOBIL PIPELINE COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.541667, -91.191111 (Explicit)<br/>Reported Spill Volume: 42 gallon<br/><b>Report Description</b><br/>CALLER REPORTED THAT DURING ROUTINE INSPECTION, GASOLINE WAS FOUND DISCHARGING FROM A VALVE VAULT ON A PIPELINE AND ONTO THE GROUND. Pipeline

19781

NRC Report: Gasoline: Automotive (Unleaded) near Baton Rouge, LA

2016-07-01 09:15:00 Baton Rouge, LA

<b>Report Details</b><br/>NRC Report ID: <a href="http://nrc.uscg.mil/">1152243</a><br/>Incident Time: 2016-07-01 09:15:00<br/>Nearest City: Baton Rouge, LA<br/>Location: BLOUNT RD & HWY 61<br/>Incident Type: PIPELINE<br/>Material: GASOLINE: AUTOMOTIVE (UNLEADED)<br/>Medium Affected: LAND<br/>Suspected Responsible Party: EXXON MOBIL PIPELINE COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.540515, -91.190987 (Approximated from intersection)<br/>Reported Spill Volume: 5040 gallon<br/><b>Report Description</b><br/>*** THIS IS AN UPDATED REPORT, REFERENCE NRC REPORT #1152184 ***

* AMOUNT DISCHARGED HAS INCREASED FROM 1BBL TO 120BBL.* A REPORT 100 BARRELS HAS BEEN RECOVERED* HIGHWAY 61 WAS SHUT-DOWN FOR APPROXIMATELY 8 HOURS AND HAS SINCE BEEN REOPENED. * LOCAL MEDIA ARE COVERING THIS INCIDENT. * NO STORM DRAINS OR WATERWAYS WERE IMPACTED.

INITIAL REPORT:CALLER REPORTED THAT DURING ROUTINE INSPECTION, GASOLINE WAS FOUND DISCHARGING FROM A VALVE VAULT ON A PIPELINE AND ONTO THE GROUND. Pipeline

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19737 NRC Report: Natural Gas2016-06-24 12:02:00 Unspecified

Incident Time: 2016-06-24 12:02:00<br/>Nearest City: LA<br/>Location: WEST CAM 480<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.531111, -93.179167 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS FROM A BELOW WATER PIPELINE IN THE GULF OF MEXICO FOR UNKNOWN REASONS. Pipeline

19715NRC Report: Unknown Oil

2016-06-21 09:17:00 Unspecified

Incident Time: 2016-06-21 09:17:00<br/>Nearest City: LA<br/>Location: MAIN PASS 69B<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN OIL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: W & T OFFSHORE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.283056, -89.022500 (Explicit)<br/>Reported Sheen Size: 50 feet by 300 feet (area 0.34 acres)<br/>SkyTruth Minimum Estimate: 0.37 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THE SUSPECTED RESPONSIBLE PARTY WAS CUTTING A 2" LIFT LINE THAT WAS SUPPOSED TO BE SECURED, BUT AFTER NOTICING OIL SEEPING DURING THE INITIAL CUT THEY SECURED OPERATIONS. Pipeline

19681 NRC Report: Oil: Crude2016-06-15 10:05:00 Unspecified

Incident Time: 2016-06-15 10:05:00<br/>Nearest City: LA<br/>Location: BLOCK 1<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CHEVRON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.103333, -90.151111 (Explicit)<br/>Reported Sheen Size: 5 feet by 80 feet (area 400 sq. ft.)<br/>Reported Spill Volume: 0 gallon<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A PINHOLE LEAK ON A PIPELINE RESULTED IS A SPILL OF CRUDE OIL. Pipeline

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19696NRC Report: Produced Water

2016-06-14 12:18:00 Unspecified

Incident Time: 2016-06-14 12:18:00<br/>Nearest City: LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: PRODUCED WATER<br/>Medium Affected: WATER<br/>Suspected Responsible Party: S2 ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.517500, -90.141667 (Explicit)<br/>Reported Sheen Size: 120 feet by 20 feet (area 2400 sq. ft.)<br/>Reported Spill Volume: 40 gallon<br/>SkyTruth Minimum Estimate: 0.06 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE IS A PINHOLE LEAK ON A PIPELINE UNDERWATER CAUSING A 20 X 120 FOOT SHEEN ON LITTLE LAKE. Pipeline

19680NRC Report: Natural Gas near Amelia, LA

2016-06-14 04:50:00 Amelia, LA

Incident Time: 2016-06-14 04:50:00<br/>Nearest City: Amelia, LA<br/>Location: CL&F NUMBER ONE<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ENERGY XXI<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.660139, -91.101412 (Approximated from CITY_STATE)<br/>Reported Sheen Size: 15 feet by 15 feet (area 225 sq. ft.)<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>CALLER STATED THERE WAS A SPILL FROM A FOUR INCH FLOW LINE DUE TO UNKNOWN CAUSES. Pipeline

19647 NRC Report: Condensate2016-06-09 03:05:00 Unspecified

Incident Time: 2016-06-09 03:05:00<br/>Nearest City: LA<br/>Location: BLOCK:WEST CAMERON # 480<br/>Incident Type: PIPELINE<br/>Material: CONDENSATE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SPECTRA ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.531111, -93.170833 (Explicit)<br/>Reported Sheen Size: 300 feet by 5 feet (area 1500 sq. ft.)<br/>Reported Spill Volume: 1 gallon<br/>SkyTruth Minimum Estimate: 0.04 gallons<br/><b>Report Description</b><br/>THE CALLER IS REPORTING THAT THERE IS A SHEEN ON THE WATER DUE TO UNKNOWN REASONS FROM A PIPELINE THAT HAD BEEN ISOLATED FOR A NUMBER OF MONTHS. Pipeline

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19664NRC Report: Unknown Oil

2016-06-09 01:00:00 Unspecified

Incident Time: 2016-06-09 01:00:00<br/>Nearest City: LA<br/>Location: WEST CAM 487<br/>Incident Type: PIPELINE<br/>Material: UNKNOWN OIL<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS EASTERN TRANSMISSION<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.530833, -93.172222 (Explicit)<br/>Reported Sheen Size: 20 feet by 150 feet (area 3000 sq. ft.)<br/>SkyTruth Minimum Estimate: 0.07 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF AN UNKNOWN GAS/OIL FROM AN UNDERWATER PIPELINE FOR UNKNOWN REASONS. MATERIAL IS BUBBLING TO THE SURFACE. SHEEN IS LIGHT IN COLOR. Pipeline

19639 NRC Report: Condensate2016-06-08 11:20:00 Unspecified

Incident Time: 2016-06-08 11:20:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: CONDENSATE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHORELINE SOUTHEAST<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.260556, -90.229722 (Explicit)<br/>Reported Spill Volume: 0 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING FACILITY PERSONNEL DISCOVERED A LEAK COMING OUT OF A FLOW LINE, RESULTING IN A RELEASE OF CONDENSATE Pipeline

19671 NRC Report: Oil: Crude2016-06-08 06:45:00 Unspecified

Incident Time: 2016-06-08 06:45:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CASTEX OFFSHORE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.485833, -91.258056 (Explicit)<br/>Reported Sheen Size: 10 feet by 20 feet (area 200 sq. ft.)<br/>Reported Spill Volume: 42 gallon<br/>SkyTruth Minimum Estimate: 0 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THE DISCOVERY OF A PIN HOLE LEAK IN THE #4 FLOW LINE, RESULTING IN A DISCHARGE OF 1 BARREL OF CRUDE OIL. Pipeline

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19657 NRC Report: Oil: Crude2016-06-06 06:30:00 Unspecified

Incident Time: 2016-06-06 06:30:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: AMERICAN NATURAL ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.780833, -90.286111 (Explicit)<br/>Reported Spill Volume: 10.5 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A FLOWLINE LEAK THAT RESULTED IN A DISCHARGE OF CRUDE OIL Pipeline

19630NRC Report: Oil: Crude near Hackberry, LA

2016-05-31 11:24:00 Hackberry, LA

Incident Time: 2016-05-31 11:24:00<br/>Nearest City: Hackberry, LA<br/>Location: 1642 GUM COVE RD<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ROBERTSON ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.026944, -93.000000 (Explicit)<br/>Reported Spill Volume: 21 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT HALF A BARREL OF CRUDE OIL DISCHARGED FROM A FLOW LINE DUE TO UNKNOWN CAUSES, POSSIBLY VANDALISM. SPILLED OIL IS BEING CONTAINED IN A DEAD END SLIP DUE TO WINDS. Pipeline

19577NRC Report: Oil: Crude near Golden Meadow, LA

2016-05-26 08:00:00 Golden Meadow, LA

Incident Time: 2016-05-26 08:00:00<br/>Nearest City: Golden Meadow, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TPIC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.383611, -90.310278 (Explicit)<br/>Reported Sheen Size: 50 feet by 500 feet (area 0.57 acres)<br/>Reported Spill Volume: 0.06 gallon<br/>SkyTruth Minimum Estimate: 0.61 gallons<br/><b>Report Description</b><br/>CALLER STATED THAT A LEAK DEVELOPED ON ONE OF THE FLOW LINES OF A CRUDE OIL WELL. THE LEAK CAUSED A DISCHARGE OF 1 CUP INTO CATFISH LAKE CAUSING A SHEEN. Pipeline

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19515NRC Report: Natural Gas near Winnsboro, LA

2016-05-21 11:00:00 Winnsboro, LA

Incident Time: 2016-05-21 11:00:00<br/>Nearest City: Winnsboro, LA<br/>Location: 3616 FRONT ST.<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: GULF SOUTH PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 32.170745, -91.724831 (Approximated from street_address)<br/><b>Report Description</b><br/>THE RP IS REPORTING A RELEASE OF NATURAL GAS DUE TO AN AUTOMOBILE STRIKING A 4" PIPELINE (METAL). RP STATED THAT TWO (2) OCCUPANTS OF THE VEHICLE WERE TRANSPORTED TO THE HOSPITAL DUE TO THE INCIDENT. THE IMPACT IS THE ATMOSPHERE. Pipeline

19499NRC Report: Oil: Crude near Sypremort Point, LA

2016-05-20 07:30:00 Sypremort Point, LA

<b>Report Details</b><br/>NRC Report ID: <a href="http://nrc.uscg.mil/">1148280</a><br/>Incident Time: 2016-05-20 07:30:00<br/>Nearest City: Sypremort Point, LA<br/>Location: WEST COTE BLANCHE BAY<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: GULF PORT ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.721111, -91.762222 (Explicit)<br/>Reported Sheen Size: 450 feet by 600 feet (area 6.2 acres)<br/>Reported Spill Volume: 1.9 gallon<br/>SkyTruth Minimum Estimate: 6.63 gallons<br/><b>Report Description</b><br/>CALLER STATED THAT THEY DISCOVERED A PARTED OUT OF SERVICE FLOW LINE ON WELL 808, WHICH CAUSED A DISCHARGE 1.9 GALLONS OF CRUDE OIL INTO THE BAY. THE PARTED LINE WAS DUE TO BAD WEATHER. Pipeline

19566NRC Report: Natural Gas; near Luling, LA

2016-05-20 06:25:00 Luling, LA

Incident Time: 2016-05-20 06:25:00<br/>Nearest City: Luling, LA<br/>Location: SEE LAT & LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS; MIXED "Y GRADE"<br/>Medium Affected: LAND<br/>Suspected Responsible Party: ENTERPRISE PRODUCTS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.916389, -90.322778 (Explicit)<br/>Reported Spill Volume: 1 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A STOPLE FITTING ON AN UNDERGROUND PIPELINE WAS DETERMINED TO BE LEAKING AT A SLOW RATE (BUBBLING). IT HAS BEEN DETERMINED THAT THE RATE OF DISCHARGE IS .014 GALLONS PER DAY. Pipeline

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19536 NRC Report: Oil: Crude2016-05-19 05:18:00 Unspecified

Incident Time: 2016-05-19 05:18:00<br/>Nearest City: LA<br/>Location: BLOCK: EUGENE ISLAND#24<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.351389, -91.760833 (Explicit)<br/>Reported Sheen Size: 75 feet by 1.5 miles (area 13.64 acres)<br/>SkyTruth Minimum Estimate: 14.58 gallons<br/><b>Report Description</b><br/>THE CALLER IS REPORTING A LIGHT RAINBOW SHEEN NEXT TO THEIR 12 INCH PIPELINE AREA DUE TO UNKNOWN REASONS. INVESTIGATION UNDERWAY. Pipeline

19543 NRC Report: Oil: Crude2016-05-18 12:37:00 Unspecified

Incident Time: 2016-05-18 12:37:00<br/>Nearest City: LA<br/>Location: GREEN CANYON 248<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHELL OFFSHORE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 27.730278, -90.570556 (Explicit)<br/>Reported Sheen Size: 30 feet by 300 feet (area 9000 sq. ft.)<br/>Reported Spill Volume: 21 gallon<br/>SkyTruth Minimum Estimate: 0.22 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF RESIDUAL HYDROCARBONS (CRUDE OIL) INTO THE GULF OF MEXICO FROM A SUBSEA FLOW LINE (JUMPER) DUE TO THE LINE BEING CUT OUT. A 70 FT PIECE OF PIPE IS BEING BROUGHT BACK TO THE SURFACE AND IS BEING CUT IN 3 PIECES. Pipeline

19534NRC Report: Oil: Crude near Leeville, LA

2016-05-18 11:19:00 Leeville, LA

Incident Time: 2016-05-18 11:19:00<br/>Nearest City: Leeville, LA<br/>Location: WEST TANK BATTERY 11<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITE MARLIN OPERATING<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.254023, -90.208782 (Approximated from CITY_STATE)<br/>Reported Sheen Size: 30 feet by 40 feet (area 1200 sq. ft.)<br/>Reported Spill Volume: 0.25 gallon<br/>SkyTruth Minimum Estimate: 0.03 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A HOLE IN AN OUT OF SERVICE PIPELINE WAS DISCOVERED AND THERE WAS A SPILL OF ONE QUART OF CRUDE OIL INTO THE WATER. Pipeline

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19488 NRC Report: Oil: Crude2016-05-12 06:30:00 Unspecified

Incident Time: 2016-05-12 06:30:00<br/>Nearest City: LA<br/>Location: SEE LAT AND LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHELL<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 27.451667, -90.343889 (Explicit)<br/>Reported Sheen Size: 0.5 miles by 3 miles (area 1.5 sq. miles)<br/>SkyTruth Minimum Estimate: 1026.3 gallons<br/><b>Report Description</b><br/>CALLER STATED A DISCHAGE OF OIL OCCURED AT THE INCIDENT LOCATION DUE TO UNKNOWN CAUSES. Pipeline

19523 NRC Report: Condensate2016-05-10 03:30:00 Unspecified

Incident Time: 2016-05-10 03:30:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: CONDENSATE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILCORP ENERGY CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.089444, -90.431667 (Explicit)<br/>Reported Spill Volume: 0.5 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A VERY SMALL SHEEN COMING FROM AN ISOLATED OUT OF SERVICE LINE DUE TO CORROSION. Pipeline

19527 NRC Report: Natural Gas2016-05-10 02:30:00 Unspecified

Incident Time: 2016-05-10 02:30:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: STONE ENERGY CORP<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.531389, -92.346389 (Explicit)<br/><b>Report Description</b><br/>CALLER REPORTED BUBBLING ON THE SURFACE OF THE WATER. NO SHEEN OR POLLUTION WAS SEEN, BUT A SEEPAGE OF NATURAL GAS IS SUSPECTED. Pipeline

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19529NRC Report: Natural Gas near Sibley, LA

2016-05-09 12:40:00 Sibley, LA

Incident Time: 2016-05-09 12:40:00<br/>Nearest City: Sibley, LA<br/>Location: SIBLEY LATERAL<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ETC FIELD SERVICES<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 32.504167, -93.292778 (Explicit)<br/><b>Report Description</b><br/>CALLER STATED THERE WAS A RELEASE OF NATURAL GAS TO THE AIR FROM A 12 INCH BELOW GROUND PIPELINE DUE TO UNKNOWN CAUSES. CALLER STATED THERE WAS A LIGHT SHEEN ON THE BEAVER POND DUE TO THIS RELEASE. THIS IS A BELOW GROUND PIPELINE THAT WAS COVERED BY WATER FROM THE NEARBY BEAVER DAM ON THE PIPELINE"S RIGHT OF WAY. Pipeline

19483

NRC Report: Well Produced Salt Water near Delcomber, LA

2016-05-09 01:10:00 Delcomber, LA

Incident Time: 2016-05-09 01:10:00<br/>Nearest City: Delcomber, LA<br/>Location: 18109 HWY 330<br/>Incident Type: PIPELINE<br/>Material: WELL PRODUCED SALT WATER<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILLCORP ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.915789, -91.999102 (Approximated from street_address)<br/>Reported Spill Volume: 4200 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A HOLE IN THE SALT WATER DISPOSAL LINE RESULTED IN A SPILL OF PRODUCED SALT WATER INTO A MARSH AREA. Pipeline

19476NRC Report: Other Oil (Condensate)

2016-05-08 09:24:00 Unspecified

Incident Time: 2016-05-08 09:24:00<br/>Nearest City: LA<br/>Location: GULF OF MEXICO<br/>Incident Type: PIPELINE<br/>Material: OTHER OIL (CONDENSATE)<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CENTURY EXPLORATION<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.920000, -93.166111 (Explicit)<br/>Reported Sheen Size: 500 feet by 500 feet (area 5.74 acres)<br/>SkyTruth Minimum Estimate: 6.14 gallons<br/><b>Report Description</b><br/>CALLER STATED WHILE FLUSHING OUT A SIX INCH STEEL PIPELINE IN THE GULF OF MEXICO BELOW THE SURFACE THERE WAS A SPILL OF CONDENSATE FROM THE POLLUTION DOME. Pipeline

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19453NRC Report: Oil: Crude near Port Sulfur, LA

2016-05-08 07:40:00 Port Sulfur, LA

Incident Time: 2016-05-08 07:40:00<br/>Nearest City: Port Sulfur, LA<br/>Location: LAT: 29N 22" 46.2"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SWIFT ENERGY OPERATING<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.379444, -89.785000 (Explicit)<br/>Reported Sheen Size: 0.5 miles by 90 feet (area 5.45 acres)<br/>Reported Spill Volume: 2 gallon<br/>SkyTruth Minimum Estimate: 5.83 gallons<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A FLOW LINE DUE TO AN UNKNOWN CAUSE AT THIS TIME. Pipeline

19457NRC Report: Natural Gas near Dequincy, LA

2016-05-06 08:40:00 Dequincy, LA

Incident Time: 2016-05-06 08:40:00<br/>Nearest City: Dequincy, LA<br/>Location: STATE HWY 389<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: GULF SOUTH PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.463669, -93.452652 (Approximated from route)<br/><b>Report Description</b><br/>CALLER STATED A NATURAL GAS LEAK OCCURRED ON A PIPELINE DUE TO UNKNOWN REASONS. Pipeline

19428NRC Report: Natural Gas near Melville, LA

2016-04-27 10:15:00 Melville, LA

Incident Time: 2016-04-27 10:15:00<br/>Nearest City: Melville, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WILLIAMS GAS PIPELINE TRANSCO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.723056, -91.793333 (Explicit)<br/><b>Report Description</b><br/>THE CALLER IS REPORTING A POTENTIAL RELEASE OF NATURAL GAS FROM A 6" STEEL LATERAL LINE. THE CALLER STATED THAT THE PIPELINE RUNS UNDER A CREEK AND "DIME SIZE" BUBBLES WERE DISCOVERED IN THE VICINITY OF WHERE THE PIPELINE IS IN THE CREEK. THE CAUSE IS CURRENTLY UNDER INVESTIGATION. Pipeline

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19437NRC Report: Produced Water near Vienna, LA

2016-04-26 04:22:00 Vienna, LA

Incident Time: 2016-04-26 04:22:00<br/>Nearest City: Vienna, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: PRODUCED WATER<br/>Medium Affected: SOIL<br/>Suspected Responsible Party: LINN ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 32.584167, -92.652778 (Explicit)<br/>Reported Spill Volume: 42 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A PIPELINE THAT IS EXPERIENCING SEEPAGE AND A RELEASE OF PRODUCED WATER. Pipeline

19426 NRC Report: Oil: Crude2016-04-25 02:15:00 Unspecified

Incident Time: 2016-04-25 02:15:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILCORP ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.135278, -89.391667 (Explicit)<br/>Reported Spill Volume: 43 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A PIPELINE HAD A PINHOLE LEAK THAT LED TO A DISCHARGE OF PRODUCED WATER AND OIL. Pipeline

19400NRC Report: Propane near Plaquemine, LA

2016-04-24 08:41:00 Plaquemine, LA

Incident Time: 2016-04-24 08:41:00<br/>Nearest City: Plaquemine, LA<br/>Location: 21255 HWY 1 SOUTH<br/>Incident Type: PIPELINE<br/>Material: PROPANE<br/>Medium Affected: AIR<br/>Suspected Responsible Party: DOW PIPELINE COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.322220, -91.252348 (Approximated from street_address)<br/>Reported Spill Volume: 130 gallon<br/><b>Report Description</b><br/>CALLER STATED DUE TO A PACKING LEAK ON A PIPELINE FROM A VALVE AT A PUMP STATION, 130 GALLONS OF PROPANE RELEASED TO THE AIR. Pipeline

19392 NRC Report: Oil: Crude2016-04-23 12:15:00 Unspecified

Incident Time: 2016-04-23 12:15:00<br/>Nearest City: LA<br/>Location: LAT: 29N 8" 29"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: ENERGY 21<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.141389, -89.595833 (Explicit)<br/>Reported Sheen Size: 120 feet by 1 miles (area 14.55 acres)<br/>Reported Spill Volume: 0.53 gallon<br/>SkyTruth Minimum Estimate: 15.55 gallons<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A PIPELINE DUE TO AN UNKNOWN CAUSE AT THIS TIME. Pipeline

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19384

NRC Report: Oil, Fuel: No. 2-D near Plaquemines Parish, LA

2016-04-20 09:40:00 Plaquemines Parish,

Incident Time: 2016-04-20 09:40:00<br/>Nearest City: Plaquemines Parish, LA<br/>Location: MM: 4.2<br/>Incident Type: PIPELINE<br/>Material: OIL, FUEL: NO. 2-D<br/>Medium Affected: LAND<br/>Suspected Responsible Party: COLONIAL PIPELINE COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.329845, -89.469590 (Approximated from CITY_STATE)<br/>Reported Spill Volume: 99 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A SECTION OF PIPELINE WAS BEING REMOVED FROM A SITE. DURING REMOVAL, A PUNCTURE OF THE PIPE OCCURRED, RESULTING IN A DISCHARGE OF DIESEL FUEL THAT WAS STILL IN THE OUT OF SERVICE PIPE. Pipeline

19336 NRC Report: Natural Gas2016-04-04 09:15:00 Unspecified

Incident Time: 2016-04-04 09:15:00<br/>Nearest City: LA<br/>Location: LAT: 29N 02.33"<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CHEVRON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.038889, -90.121667 (Explicit)<br/><b>Report Description</b><br/>NATURAL GAS RELEASED FROM A 4 INCH GAS LIFT LINE DUE TO AN UNKNOWN CAUSE AT THIS TIME Pipeline

19310 NRC Report: Oil: Crude2016-03-29 04:09:00 Unspecified

Incident Time: 2016-03-29 04:09:00<br/>Nearest City: LA<br/>Location: LAT: 30N 04.824"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILCORP ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.080278, -91.530833 (Explicit)<br/>Reported Sheen Size: 5 feet by 8 feet (area 40 sq. ft.)<br/>SkyTruth Minimum Estimate: 0 gallons<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A 3 INCH FLOW LINE DUE TO A FLANGE LEAK. Pipeline

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19294NRC Report: Oil: Crude near Golden Meadow, LA

2016-03-28 08:15:00 Golden Meadow, LA

Incident Time: 2016-03-28 08:15:00<br/>Nearest City: Golden Meadow, LA<br/>Location: CATFISH LAKE<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.377206, -90.264363 (Approximated from CITY_STATE)<br/>Reported Spill Volume: 42 gallon<br/><b>Report Description</b><br/>CALLER STATED CORROSION ON A FLOW LINE CAUSED THE RELEASE OF CRUDE OIL INTO THE WATER. Pipeline

19267NRC Report: Oil: Crude near Hackberry, LA

2016-03-26 09:45:00 Hackberry, LA

Incident Time: 2016-03-26 09:45:00<br/>Nearest City: Hackberry, LA<br/>Location: LAT: 30N 01" 19"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: GULFPORT ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.021944, -93.307778 (Explicit)<br/>Reported Spill Volume: 5 gallon<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A FLOW LINE DUE TO AN UNKNOWN CAUSE AT THIS TIME. Pipeline

19261NRC Report: Oil: Crude near Venice, LA

2016-03-25 07:25:00 Venice, LA

Incident Time: 2016-03-25 07:25:00<br/>Nearest City: Venice, LA<br/>Location: LAT: 29N .24554"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TX. PETROLEUM INVESTMENT CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.245556, -89.199167 (Explicit)<br/>Reported Spill Volume: 84 gallon<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A 3 INCH FLOW LINE DUE TO AN EQUIPMENT FAILURE INVOLVING THE BULL PLUG. Pipeline

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19271 NRC Report: Oil: Crude2016-03-23 05:15:00 Unspecified

Incident Time: 2016-03-23 05:15:00<br/>Nearest City: LA<br/>Location: HALF MOON LAKE FACILITY<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: COX OPERATING LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.234722, -89.416944 (Explicit)<br/>Reported Sheen Size: 150 feet by 2 miles (area 36.36 acres)<br/>Reported Spill Volume: 0.4 gallon<br/>SkyTruth Minimum Estimate: 38.88 gallons<br/><b>Report Description</b><br/>CALLER STATED THE COMPANY HAD A PINHOLE LEAK IN A DISCHARGE LINE WHICH CAUSED A DISCHARGE OF .4 GALLONS OF CRUDE OIL INTO THE ELOI BAY CAUSING A 2 MILE BY 50 YARD SHEEN. Pipeline

19230 NRC Report: Oil: Crude2016-03-16 11:10:00 Unspecified

Incident Time: 2016-03-16 11:10:00<br/>Nearest City: LA<br/>Location: BLOCK 23<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CHEVRON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.010278, -90.161944 (Explicit)<br/>Reported Sheen Size: 80 feet by 200 feet (area 0.37 acres)<br/>Reported Spill Volume: 0.04 gallon<br/>SkyTruth Minimum Estimate: 0.39 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A PIN HOLE LEAK WAS DISCOVERED ON A FLOW LINE. AN ESTIMATED .043 GALLONS OF CRUDE OIL INTO THE WATER. THIS IS RELATED TO NRC REPORT 1142991. Pipeline

19240 NRC Report: Oil: Crude2016-03-15 01:00:00 Unspecified

Incident Time: 2016-03-15 01:00:00<br/>Nearest City: LA<br/>Location: LAT: 29N 21" 16"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: CHEVRON<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.354444, -88.934444 (Explicit)<br/>Reported Sheen Size: 30 feet by 300 feet (area 9000 sq. ft.)<br/>Reported Spill Volume: 0.07 gallon<br/>SkyTruth Minimum Estimate: 0.22 gallons<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A 3 INCH FLOW LINE ONBOARD A PLATFORM DUE TO CORROSION. Pipeline

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19182NRC Report: Natural Gas near Oakdale, LA

2016-03-14 09:55:00 Oakdale, LA

Incident Time: 2016-03-14 09:55:00<br/>Nearest City: Oakdale, LA<br/>Location: LAT: 30N .723262"<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: GULF SOUTH PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.723333, -92.712222 (Explicit)<br/><b>Report Description</b><br/>NATURAL GAS IS RELEASING FROM AN UNDERGROUND 6 INCH PIPELINE DUE TO AN UNKNOWN CAUSE AT THIS TIME. Pipeline

19220NRC Report: Salt Water near Abbeville, LA

2016-03-12 08:45:00 Abbeville, LA

Incident Time: 2016-03-12 08:45:00<br/>Nearest City: Abbeville, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: SALT WATER<br/>Medium Affected: OTHER<br/>Suspected Responsible Party: HILCORP<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.601111, -92.258889 (Explicit)<br/>Reported Spill Volume: 13 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING A PIN HOLE LEAK IN A FLOW LINE, CAUSING A DISCHARGE OF 13 GALLONS OF SALT WATER AND AN UNKNOWN AMOUNT OF NATURAL GAS. Pipeline

19210 NRC Report: Oil: Crude2016-03-12 02:00:00 Unspecified

Incident Time: 2016-03-12 02:00:00<br/>Nearest City: LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITNEY OIL & GAS<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.038889, -89.282500 (Explicit)<br/>Reported Sheen Size: 45 feet by 300 feet (area 0.31 acres)<br/>Reported Spill Volume: 0.03 gallon<br/>SkyTruth Minimum Estimate: 0.33 gallons<br/><b>Report Description</b><br/>THERE WAS A SMALL LEAK ON A TWO INCH FLOW LINE WHICH CAUSED A DISCHARGE OF APPROXIMATELY .033 GALLONS OF CRUDE OIL TO DISCHARGE INTO THE GULF OF MEXICO. THIS CAUSED A SILVERY SHEEN OF 15 YARDS WIDE BY 100 YARDS LONG. Pipeline

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19184NRC Report: Oil: Crude near Golden Meadow, LA

2016-03-11 10:00:00 Golden Meadow, LA

Incident Time: 2016-03-11 10:00:00<br/>Nearest City: Golden Meadow, LA<br/>Location: CATFISH LAKE<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.383889, -90.310556 (Explicit)<br/>Reported Sheen Size: 50 feet by 200 feet (area 0.23 acres)<br/>SkyTruth Minimum Estimate: 0.25 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF CRUDE OIL INTO CATFISH LAKE FROM A FLOW LINE DUE TO EQUIPMENT FAILURE FROM CORROSION AND POSSIBLE PINHOLE LEAK. Pipeline

19116NRC Report: Oil: Crude near Lafitte, LA

2016-03-05 01:05:00 Lafitte, LA

Incident Time: 2016-03-05 01:05:00<br/>Nearest City: Lafitte, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HILLCORP ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.575278, -90.054722 (Explicit)<br/>Reported Sheen Size: 150 feet by 1 miles (area 18.18 acres)<br/>Reported Spill Volume: 84 gallon<br/>SkyTruth Minimum Estimate: 19.44 gallons<br/><b>Report Description</b><br/>CALLER STATED THAT THEY HAD BLOCK VALVE OF THE PIPELINE DEVELOPED A HOLE THAT CAUSED A DISCHARGE OF 2 BARRELS OF LIGHT CRUDE OIL INTO THE MARSH. THE OIL IS CONTAINED IN A DITCH WHICH IS BLOCKED OFF. Pipeline

19111 NRC Report: Oil: Crude2016-03-03 12:30:00 Unspecified

Incident Time: 2016-03-03 12:30:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.638611, -92.435278 (Explicit)<br/>Reported Sheen Size: 2 feet by 0.19 miles (area 2000 sq. ft.)<br/>Reported Spill Volume: 5 gallon<br/>SkyTruth Minimum Estimate: 0.05 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE WAS A SEPARATION IN A JOINT ON A 4 INCH FLOW LINE, CAUSING THE DISCHARGE OF APPROXIMATELY 5 GALLONS OF CRUDE OIL. Pipeline

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19161 NRC Report: Oil: Crude2016-03-03 07:15:00 Unspecified

Incident Time: 2016-03-03 07:15:00<br/>Nearest City: LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: GULF PORT ENERGY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.683611, -91.799722 (Explicit)<br/>Reported Sheen Size: 25 feet by 50 feet (area 1250 sq. ft.)<br/>Reported Spill Volume: 0.04 gallon<br/>SkyTruth Minimum Estimate: 0.03 gallons<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED THROUGH A PINHOLE LEAK ON A FLOWLINE (ON AN OUT OF SERVICE WELL) INTO WEST COTE BLANCHE BAY. Pipeline

19131NRC Report: Natural Gas near Church Point, LA

2016-03-02 04:20:00 Church Point, LA

Incident Time: 2016-03-02 04:20:00<br/>Nearest City: Church Point, LA<br/>Location: IN VICINITY OF<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: GULF SOUTH PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.396452, -92.211292 (Approximated from CITY_STATE)<br/><b>Report Description</b><br/>CALLER IS REPORTING A LEAK IN A NATURAL GAS PIPELINE. UNKNOWN CAUSE AT THIS TIME. Pipeline

19135NRC Report: Natural Gas near Kinder, LA

2016-02-25 12:15:00 Kinder, LA

Incident Time: 2016-02-25 12:15:00<br/>Nearest City: Kinder, LA<br/>Location: GREEN OAK CEMETERY RD<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.523610, -92.833027 (Approximated from route)<br/><b>Report Description</b><br/>CALLER REPORTED A LEAK OF NATURAL GAS. Pipeline

19164NRC Report: Natural Gas near New Roads, LA

2016-02-25 06:40:00 New Roads, LA

Incident Time: 2016-02-25 06:40:00<br/>Nearest City: New Roads, LA<br/>Location: 750W ON ST AUGUSTINE RD<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: AIR<br/>Suspected Responsible Party: WILLIAMS GAS PIPELINE TRANSCO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.709912, -91.434964 (Approximated from route)<br/><b>Report Description</b><br/>CALLER IS REPORTING A RELEASE OF NATURAL GAS INTO THE ATMOSPHERE FROM A PIPELINE FOR UNKNOWN REASONS. INCIDENT IS STILL UNDER INVESTIGATION Pipeline

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19129NRC Report: Propane near Sulphur, LA

2016-02-24 03:58:00 Sulphur, LA

Incident Time: 2016-02-24 03:58:00<br/>Nearest City: Sulphur, LA<br/>Location: SULPHUR PUMP STATION<br/>Incident Type: PIPELINE<br/>Material: PROPANE<br/>Medium Affected: AIR<br/>Suspected Responsible Party: DIXIE PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.241192, -93.370553 (Approximated from CITY_STATE)<br/><b>Report Description</b><br/>CALLER STATED THERE WAS A RELEASE OF PROPANE DUE TO RUPTURE WHICH RESULTED IN A FIRE. Pipeline

19078NRC Report: Oil: Crude near Golden Meadow, LA

2016-02-19 05:00:00 Golden Meadow, LA

Incident Time: 2016-02-19 05:00:00<br/>Nearest City: Golden Meadow, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.381389, -90.275833 (Explicit)<br/>Reported Spill Volume: 15 gallon<br/><b>Report Description</b><br/>THE CALLER IS REPORTING A DISCHARGE OF CRUDE OIL FROM A PINHOLE LEAK IN A FLOW LINE (CONNECTS WELLHEAD & FACILITY). THE IMPACT IS SURFACE WATER IN A MARSH AREA Pipeline

19083NRC Report: Oil, Fuel: No. 6 near Garyville, LA

2016-02-18 10:00:00 Garyville, LA

Incident Time: 2016-02-18 10:00:00<br/>Nearest City: Garyville, LA<br/>Location: 4084 HWY 44<br/>Incident Type: PIPELINE<br/>Material: OIL, FUEL: NO. 6<br/>Medium Affected: WATER<br/>Suspected Responsible Party: PETROLEUM FUEL<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.054533, -90.646640 (Approximated from street_address)<br/>Reported Spill Volume: 5 gallon<br/><b>Report Description</b><br/>#6 OIL DISCHARGED FROM A 12 INCH PIPELINE (WITH A 1 INCH BLEEDER VALVE) DUE TO A CHECK VALVE FAILURE. Pipeline

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19148NRC Report: Y-Grade near Augusta, LA

2016-02-18 07:45:00 Augusta, LA

Incident Time: 2016-02-18 07:45:00<br/>Nearest City: Augusta, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: Y-GRADE<br/>Medium Affected: AIR<br/>Suspected Responsible Party: ENTERPRISE PRODUCTS OPERATING<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.796111, -90.015000 (Explicit)<br/>Reported Spill Volume: 1 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING WHILE A PIPELINE WAS BEING WORKED ON, A FLASH FIRE OCCURRED, RESULTING IN A DISCHARGE OF Y-GRADE. Pipeline

19067NRC Report: Oil: Crude near Golden Meadow, LA

2016-02-14 02:30:00 Golden Meadow, LA

Incident Time: 2016-02-14 02:30:00<br/>Nearest City: Golden Meadow, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.373889, -90.290556 (Explicit)<br/>Reported Sheen Size: 40 feet by 100 feet (area 4000 sq. ft.)<br/>SkyTruth Minimum Estimate: 0.1 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A PINHOLE LEAK IN A 4 INCH FLOW LINE RESULTED IN A DISCHARGE OF CRUDE OIL. Pipeline

19066NRC Report: Oil: Crude near Johnson Bay, LA

2016-02-12 08:30:00 Johnson Bay, LA

Incident Time: 2016-02-12 08:30:00<br/>Nearest City: Johnson Bay, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: LAND<br/>Suspected Responsible Party: APOLLO ENERGY OPERATING COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.825278, -93.623056 (Explicit)<br/>Reported Spill Volume: 126 gallon<br/><b>Report Description</b><br/>APPROXIMATELY THREE (3) BARRELS OF CRUDE OIL DISCHARGED FROM A 2" FLOW LINE, DUE TO PINHOLE LEAK. Pipeline

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19046NRC Report: Oil: Crude near Leeville, LA

2016-02-05 01:00:00 Leeville, LA

Incident Time: 2016-02-05 01:00:00<br/>Nearest City: Leeville, LA<br/>Location: LAT: 29N 14" 34.5"<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: SHORELINE S.E. LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.243056, -90.227778 (Explicit)<br/>Reported Spill Volume: 2 gallon<br/><b>Report Description</b><br/>CRUDE OIL DISCHARGED FROM A GAS LINE ASSOCIATED WITH A FACILITY DUE TO CORROSION. Pipeline

19041NRC Report: Oil: Crude near Golden Meadow, LA

2016-02-03 10:00:00 Golden Meadow, LA

Incident Time: 2016-02-03 10:00:00<br/>Nearest City: Golden Meadow, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.382500, -90.369722 (Explicit)<br/>Reported Sheen Size: 20 feet by 40 feet (area 800 sq. ft.)<br/>Reported Spill Volume: 0 gallon<br/>SkyTruth Minimum Estimate: 0.02 gallons<br/><b>Report Description</b><br/>CALLER IS REPORTING A LEAK ON A FLOWLINE RESULTED IN A DISCHARGE OF CRUDE OIL. Pipeline

19053 NRC Report: Natural Gas2016-02-03 09:00:00 Unspecified

Incident Time: 2016-02-03 09:00:00<br/>Nearest City: LA<br/>Location: BLOCK 198<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 28.577500, -91.255833 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT BUBBLES WERE OBSERVED ON THE WATER IN THE VICINITY OF NATURAL GAS LINES. NO SHEEN ON THE WATER THE BUBBLE FIELD IS 25- 30 FEET IN DIAMETER Pipeline

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19035 NRC Report: Natural Gas2016-02-03 04:00:00 Unspecified

Incident Time: 2016-02-03 04:00:00<br/>Nearest City: LA<br/>Location: VERMILION BAY<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: HARVEST PIPELINE<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.716111, -92.016944 (Explicit)<br/><b>Report Description</b><br/>THE CALLER IS REPORTING A RELEASE OF NATURAL GAS DUE TO UNKNOWN CAUSES THIS TIME. THE CALLER STATED THAT BUBBLES WERE DISCOVERED COMING FROM THE UNDERWATER PIPELINE. THE IMPACT IS VERMILION BAY. Pipeline

19023 NRC Report: Oil: Crude2016-02-02 10:30:00 Unspecified

Incident Time: 2016-02-02 10:30:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.373611, -90.290556 (Explicit)<br/>Reported Spill Volume: 8 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT THERE WAS A LEAK THAT DEVELOPED ON A FLOW LINE ON AN OIL WELL. APPROXIMATELY 5-8 GALLONS OF CRUDE OIL DISCHARGED INTO THE MARSH. Pipeline

18898NRC Report: Natural Gas near Abbeville, LA

2016-01-31 08:00:00 Abbeville, LA

Incident Time: 2016-01-31 08:00:00<br/>Nearest City: Abbeville, LA<br/>Location: <br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: <br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.718333, -92.019722 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT NATURAL GAS IS LEAKING FROM AN UNDERWATER PIPELINE IN THE BAY AREA VICINITY DUE TO UNKNOWN CAUSES. CALLER STATED THERE WERE NO STRUCTURES IN THE AREA OF THE INCIDENT LOCATION. Pipeline

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18961NRC Report: Natural Gas near Grand Chenier, LA

2016-01-20 02:22:00 Grand Chenier, LA

Incident Time: 2016-01-20 02:22:00<br/>Nearest City: Grand Chenier, LA<br/>Location: IN MARSH LAND<br/>Incident Type: PIPELINE<br/>Material: NATURAL GAS<br/>Medium Affected: WATER<br/>Suspected Responsible Party: COLUMBIA GAS TRANSMISSION<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.767500, -92.691944 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT BUBBLES WERE OBSERVED IN THE WATER THAT ARE BELIEVED TO BE A RELEASE OF NATURAL GAS FROM AN UNDERWATER TRANSMISSION PIPELINE. Pipeline

18986NRC Report: Condensate (Crude Oil Byproduct)

2016-01-13 02:15:00 Unspecified

Incident Time: 2016-01-13 02:15:00<br/>Nearest City: LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: CONDENSATE (CRUDE OIL BYPRODUCT)<br/>Medium Affected: WATER<br/>Suspected Responsible Party: TEXAS PETROLEUM INVESTMENT CO.<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 29.390278, -90.962778 (Explicit)<br/>Reported Sheen Size: 20 feet by 20 feet (area 400 sq. ft.)<br/>Reported Spill Volume: 0 gallon<br/>SkyTruth Minimum Estimate: 0.01 gallons<br/><b>Report Description</b><br/>THE CALLER IS REPORTING A DISCHARGE OF CONDENSATE (CRUDE OIL BY PRODUCT) DUE TO UNKNOWN CAUSES. THE CALLER STATED THAT THE MATERIAL CAME FROM A FLOW LINE (SUBMERGED) ASSOCIATED WITH A WELL, POSSIBLY CAUSED BY CORROSION. THE IMPACT IS AN UNNAMED CANAL. Pipeline

18984

NRC Report: Gasoline: Automotive (Unleaded) near Chipola, LA

2016-01-12 03:15:00 Chipola, LA

Incident Time: 2016-01-12 03:15:00<br/>Nearest City: Chipola, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: GASOLINE: AUTOMOTIVE (UNLEADED)<br/>Medium Affected: LAND<br/>Suspected Responsible Party: COLONIAL PIPELINE COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.928889, -90.830556 (Explicit)<br/><b>Report Description</b><br/>CALLER IS REPORTING A DISCHARGE OF GASOLINE FROM A BELOW GROUND PIPELINE. Pipeline

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18990

NRC Report: Gasoline: Automotive (Unleaded) near Chipola, LA

2016-01-12 03:15:00 Chipola, LA

Incident Time: 2016-01-12 03:15:00<br/>Nearest City: Chipola, LA<br/>Location: SEE LAT/LONG<br/>Incident Type: PIPELINE<br/>Material: GASOLINE: AUTOMOTIVE (UNLEADED)<br/>Medium Affected: SUBSURFACE<br/>Suspected Responsible Party: COLONIAL PIPELINE COMPANY<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.928889, -90.830556 (Explicit)<br/>Reported Spill Volume: 4200 gallon<br/><b>Report Description</b><br/>///THIS IS AN UPDATE TO NRC REPORT NUMBER 1137906.///

CALLER IS REPORTING A DISCHARGE OF GASOLINE FROM A BELOW GROUND PIPELINE.

THE CAUSE OF THE INCIDENT WAS A CRACK IN THE PIPELINE. THE AMOUNT RELEASED IS 100 BARRELS. THE RELEASE ONLY AFFECTED THE SOIL. Pipeline

18995NRC Report: Oil: Crude near Gueydan, LA

2016-01-09 06:30:00 Gueydan, LA

Incident Time: 2016-01-09 06:30:00<br/>Nearest City: Gueydan, LA<br/>Location: 7110 COACH RD<br/>Incident Type: PIPELINE<br/>Material: OIL: CRUDE<br/>Medium Affected: WATER<br/>Suspected Responsible Party: WHITE OAK OPERATING CO. LLC<br/><b>SkyTruth Analysis</b><br/>Lat/Long: 30.050619, -92.467383 (Approximated from street_address)<br/>Reported Spill Volume: 20 gallon<br/><b>Report Description</b><br/>CALLER IS REPORTING THAT A FISHERMAN WAS IN A CRAWFISH POND AND THEY RAN INTO A 4 INCH PRODUCTION PIPELINE WHICH CAUSED THE PIPE TO DISCHARGE APPROXIMATELY 20 GALLONS OF CRUDE OIL INTO THE POND Pipeline

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