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Improving Phosphorus Removal with
Magnetite Assisted Settlement.
BioMag and CoMag
Adam Brookes, Bernie Glanville, Stephen Tomlin, Jane Youdan.
Anglian Water, Northumbrian Water, Wessex Water.
The BIG P conference, Manchester, 5th July 2017
National Collaborative Project
Improving Phosphorus Removal with Magnetite Assisted Settlement
Content:
• Process background – the use of magnetite
• Trial sites and results
• Common findings
Process Background
• Magnetite assisted settlement
• Both BioMag and CoMag can be retrofitted
• Magnetite recovery system
• Co-Mag:
– Use of magnetite to assist with settlement after secondary
treatment (trickling filters or activated sludge)
– Separate floc tank and settlement tanks
• BioMag:
– Addition of magnetite into activated sludge
– Use of existing FST
• Shear mill
• Magnetic recovery drum
• Return of magnetite to
process
• Removal of excess
sludge
Magnetite Recovery
System
Trials
• Part of the AMP6 national phosphorus removal technology trials.
• Market Harborough STW, Anglian Water. CoMag
– Oxidation ditch, followed by CoMag, PE = 23,000
• Esh Winning STW, Northumbrian Water. Co-Mag
– Trickling filters, PE = 5,000 (100% of flow)
• Bowerhill STW, Wessex Water. BioMag
– ASP, PE treated = 4,000 (50% of site flow)
CoMag
Market Harborough STW
Market Harborough STW
Overview of CoMag Process Installation
• CoMag installed post ASP, fed from feed/overflow chamber
Note: upstream chemical dosing for P removal to target of around 1 mg/L
Market Harborough STW
CoMag Installation
Market Harborough STW
Results of CoMag Trial
Influent total P
Average
(mg/l)
Effluent total P
Average
(mg/l)
Effluent total P
Min
(mg/l)
Effluent
total P
Max
(mg/l)
% removal
1.13 0.17 0.06 0.4 85
Market Harborough STW Summary
• The principal issues encountered during the trial were the
robustness and reliability of individual components that are
fundamental to successful and stable operation.
• Numerous problems with polymer make up and dosing system.
• Duty only on trial plant so single point of failure
• The performance of the clarifier was identified by EWT as being
deficient, limiting the overall performance of the plant
• Relatively high chemical use per volume treated and load
removed (polymer and ferric)
• Excellent performance when everything was working correctly
CoMag
Esh Winning STW
Esh Winning STW
Overview of Comag Process Installation
• Comag retrofit between the trickling filters and the humus tanks
• Diversion of flows post trickling filters into wet well then pumped
into package plant for ferric and caustic dosing
• Flow passing through several reaction tanks mixing with sludge
returns and polymer
• Flow passing into humus tanks for settlement and sludge
recovery
• Initial hydrostatic valves for desludge of humus tanks. Required
replacement with progressive cavity pumps due to blockages
• Sludge wastage and magnetite recovery process
• Note; no upstream chemical dosing for P removal
Esh Winning STW – Process Layout
Esh Winning STW
Impact of Process Stability on Final
Effluent
0
0.5
1
1.5
2
2.5
3
3.5
4
4.5
5
24
-May
31
-May
07
-Jun
14
-Jun
21
-Jun
28
-Jun
05
-Jul
12
-Jul
19
-Jul
26
-Jul
02
-Aug
09
-Aug
16
-Aug
23
-Aug
30
-Aug
06
-Sep
13
-Sep
20
-Sep
27
-Sep
04
-Oct
11
-Oct
18
-Oct
25
-Oct
01
-Nov
08
-Nov
15
-Nov
22
-Nov
29
-Nov
06
-Dec
mg
/l P
ho
sp
ho
rus FE total P
FE SRP
P 1
SRP 1
P 2
SRP 2
Level of Control
Esh Winning STW
The Good and the Bad
When stable, good settlement
and visibility within the humus
tankWear on PC pumps after 3
months
Esh Winning STW – Summary of Trial
• Major equipment failures during the trial; shear mill, transfer pumps and
dosing systems, resulting in an unstable process.
• When the plant was working correctly the final effluent quality was good
with total P levels down to 0.22mg/l and less.
• SRP values were less than 0.1mg/l unless the chemical dosing system
failed.
• If the dosing system failed the final effluent quality deteriorated within 24
hours.
• If the magnetite sludge was allowed to settle for more than 2 hours in
the tanks a vactor was required to re-suspend or remove it.
• Further investigation of the control and set up of the technology required
BioMag
Bowerhill STW
Bowerhill STW
BioMag Installation
• Aeration lanes
• PE approx. 4000
• Primary ferric ahead of the PSTs
• Additional secondary ferric dose into aeration lanes
• Polymer dose at outlet of aeration lanes
Primary
Settlement
Tanks
Sludge Storage Tank
ASP
Inlet Works
Final Effluent to River
Final
Settlement
Tank
RAS
BioMag® Unit… …
SAS
Shear Mill
Magnetic Drum
SAS Buffer Tank
Recovered
Magnetite
SAS
Addition of
magnetite
Bowerhill STW
BioMag Results
• Results (1 year period):
– Average Total P = 0.23 mg/l
– Average SRP = 0.10 mg/l
Bowerhill STW
BioMag Summary
• Other findings:
– The polymer did not show any impact on results
– Due to settlement of magnetite in the aeration lanes, it was
challenging to maintain the suggest magnetite:MLSS ratio
– Secondary ferric dose was critical to low P concentrations
• The BioMag system could be used to increase treatment capacity,
but this was not looked at as part of this trial.
Common Findings
BioMag & CoMag
Common Findings
• Total P concentrations of between 0.17 mg/l and 0.23 mg/l
• No benefit seen from use of polymer in BioMag
• Issues with reliability of process
• Some issues with replacement parts for magnetite recovery system
• Issues with settlement of magnetite
• Magnetite measurement method was not user friendly
Any Questions?
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