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Stripping Efficiency ImprovementAfter Catalyst Stripper Packing Installation
in RFCC Unit
2007.12
Location Of ONSAN Complex
JAPAN
CHINA
O
S Seoul
UlsanOnsanPusan
Seoul ↔ Ulsan : 400 Km
Pusan ↔ Ulsan : 50 Km
Ulsan ↔ Onsan: 15 Km
S-OiL
Refinery Overview
SPM
BTX/P-X
CDU
R2RR2RHYC/HVL
R&D Center
CDU CDU
MHC
#2CDU
MHC
#1HVL
#3CDU
#2VDU
RFCC
HYC
MTBE
H2Crude
Atm. Residue
VGO
Vac. Residue
HydrotreatedResidue
Hydrotreated Residue
Lube Base Oil
LPGNaphthaKeroseneDiesel
Propylene
Gasoline
MTBE
Slurry
LPG
LCO
NaphDSL
NaphDSL
KeroDSL
LPG
NaphKeroDSL
LPG
#1CDU Lube
Plant
Lube Base Oil / Wax
BTXBenzene
TolueneXylene
H2
H2
C9 Aro.
H2
Naph
Atm. Residue Para Xylene
Benzene
X-C#1
VDU
Asphalt
MDO
HDO
DAO
SDASDA
#1HMP#2HMP#3HMP
#2HVL
R2R
Overall Process Flow Scheme
RFCC
ㆍ RFCC (Residue Fluidized Catalytic Cracking) Unit
The purpose of RFCC unit is to convert heavy feedstockssuch as AR or VR into lighter valuable products mainlyGasoline,C3=,LPG and Light Cycle Oil.
Besides the valuable products, the catalytic reactions produces dry gas,slurry oil and coke.
The cracked gaseous products are treated in the fractionatorand downstream units.
The coke ,deposited on the catalyst in the reaction zone,is burnt in the regeneration zone.
RFCC Process(R2R)
ㆍDesign : 40,000 BPD
ㆍCurrent: 73,000 BPD
.New Air blower
.New Catalyst cooler
.New Feed injector/Stripper Packing
.New Tower internal
ㆍLicensor : Axens(IFP,France)
ㆍFeed : Treated (VR + VGO)
ㆍ1 Reactor / 2 Regenerators(R2R)
ㆍMain Products
. Propylene (10 vol%)
. Gasoline (55 vol%)
ㆍConversion : 80 vol%
Catalyst Stripper(1)
ㆍ Catalyst Stripper in FCC Unit
The FCC process is using small particles of catalyst whichbehave as a fluid when aerated with gas.
The catalyst is continuously circulated from the reaction zone to the regeneration zone.
The Catalyst Stripper located in Reactor bottom section whichrecovers volatile hydrocarbon contained in the catalystparticles before the catalyst enters regenerators.
Catalyst Stripper(2)
ㆍ Catalyst Stripper in FCC Unit
The internals in the Catalyst Stripper improve
hydrocarbon recovery by prompting intimate contact of
the stripping steam and catalyst,
however R2R Unit doesn’t have the internals and
this is known to cause the increase of coke yield and
stripping steam consumption.
R2R Reactor & RegeneratorsR2R Reactor & Regenerators
SLURRY
LCO
HVY GASOLINE
GAS RECOVERYSECTION
FUEL GAS
PROPYLENE
PROPANE
C4
LT. GASOLINE
FEED
Fractionator
Disengager / Stripper
RISER
2nd Regenerator
1st Regenerator
CatalystCooler
R2 FLUE GASR1 FLUE GAS
740 ℃1.15 KSCG
660 ℃1.90 KSCG
526 ℃1.25 KSCG
Combustion Air
Packing nstallation Backgrounds
ㆍ H2 on Coke level in R2R Unit was around 7~8 wt%.(While, well-designed catalyst stripper internals could achieve below 6 wt% )
ㆍ Under the bottleneck of Air Blower.
ㆍ Frequent Catalyst Cooler isolation by tube leak Charge down.
ㆍ 2 Licensors was competitors.( Axens (manufactured by Koch-Glitsch), ABB Lummus )
ㆍ Commercial experiences was key reason for selection.( Axens (20 units, as of 2005), Lummus (No, as of 2005))
Before Packing Installation
- Stripping Steam Ring.. Upper steam ring. Main steam ring. Lower steam ring. Half moon steam ring
- Steam Flow :10.7 T/H
- H2 on Coke : 7~8 wt%
Stripping Steam
Hydrocarbon
Reactor
Stripper
After Packing Installation
- Stripper Steam Ring(Upper ring removed)
- 8 Layers Structured Packing
- Stripping Steam : 8.0 T/H(Steam Reduction : 2.7 T/H)
- H2 on Coke : 5~6 wt%Stripping Steam
Hydrocarbon
Reactor
Stripper
Packing
Stripper Packing (8 Layers)
Structured Packing Picture (S-OiL)
Installed Packing Picture (S-OiL)
RISER
SHELL
Packing
Stripping Efficiency Improvement
Before After- CCR (Ton/min.) 36.0 39.0- Steam (Ton/h) 10.8 8.0- Steam/CCR (kg/Ton) 5.0 3.4- H2 on Coke (wt%) 7~8 5~6
o In spite of higher CCR and lower Stripping Steam rate, Stripping Efficiency was improved. (H2 on Coke can be decreased)
H2 on Coke After Packing Installation
H2 on Coke / Stripping Steam
0.0
2.0
4.0
6.0
8.0
10.0
12.0
2005-03-01 2005-03-31 2005-04-30 2005-05-30 2005-06-29 2005-07-29 2005-08-28 2005-09-27 2005-10-27
Date
H2 o
n C
oke,w
t%
0
2000
4000
6000
8000
10000
12000
Strip
pin
g s
team
,
kg/h
H2 on Coke Stripping steam
Economics Analysis
- Total Investment Cost : 1 billion won
(including installation cost)
- Steam (MP) reduction : 2.8 Ton/h
* CO2 emission reduction : 5,000 Ton/Year
- Payout periods (IRR) : About 2 years (40%)
(excluding Charge increase)
Reference (By Axens)
Reference (By Axens)
Reference (By Axens)
Reference (By Axens)
Reference (By Axens)
Reference (By Lummus)
Car Loves S-OiL