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8/8/2019 Bravo Line lean manfacturing
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The Story of the Bravo Line:A Tale of Reduced Lead Times
and Lots of Early GainsPresented by:
Charan
Nageswara Rao
BupendraNarayan
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If process improvement and the elimination of waste is yourobjective the Bravo Line improvements, show in dramatic
fashion how important lead-time reductions are.
They also show just how importantjidoka is to these processimprovements. Lead-time reductions serve many worthwhilefunctions.
Quick feedback for problem solving Quick turnover of product
Improved cash flow
Generating future business
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On this line, which produced 11 different models, they hadalso made an effort to go to small lot production.
They described a small lot as 50 units, which was a tray. Four trays were stacked in a small box and five small boxes
were packed in a larger box, for a total of 1000 units perbox, and a typical shipping lot was 2000 units, or two large
boxes on one pallet. The customer demand was 10,000 units per week
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Their problems were threefold:
They could not produce to schedule and frequently missedshipments.
It took nearly twice the time.
It took nearly 70 percent extra labor to make a batch.
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Approaches:
Synchronize supply to the customer, externally
The Takt calculation
Synchronize production, internally
The Basic Time and Balancing Studies
Create flow, including
Establishingjidoka
Working to destroy batches
Establish a pull demand system
Kanban system, Heijunka
Implementing the Prescription
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Redesign based on an OEE of 1.00, so takt timeeffectively became cycle time.
The work (from the time study) for Cell 1 was 207seconds and the work for Cell 2 was 105 seconds.Consequently, for a 39-second takt:
I. At Cell 1 we needed 207/39 = 5.3, or six stations
II. At Cell 2 we needed 105/39 = 2.7, or three stations
Synchronizing Production, Internally
The Basic Time and Balancing Studies
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It took less than one hour to see one of the major issues.
Station 6 of Cell 1 was now only used for final visualinspection and packing.
The very first unit it received had an incorrect O-ringinstalled.
Fortunately, due to the kanban system, we had less than 25units to rework.
On this run, we had to stop four more times for qualityproblems in the first four hours of production alone. It was
clear at this point that process stability was nonexistent.
he Production Run, with Problems Galor
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The most important quantity control tactic for process
improvement is often first piece lead-time reduction.
It is accomplished mainly by a reduction in lot size, ideallygoing to one-piece flow.
Once achieved, this will allow the problem solving process
to be responsive, and in this case, rework can be reduced onboth a batch and permanent basis.
RESULTS
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The company was now able to produce to schedule, and missedshipments dropped to zero.
First piece lead time was reduced from 3.9 hours to 6.5 minutes.
They had now reduced the lot lead time from over six days toless than 30 hours.
They found they could achieve these numbers with much less
manpower. They reduced from 336 md/10,000 units to theplan of 210 md/10,000 units and then to a new low of 135md/10,000 units. All with virtually no extra investment.
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The Three Fundamental Issues of Cultural Change
- Plan - motivation - problem solvers
Foundational issues of quality
Problem solving by all
Understanding variation
Process stability (Cp, Cpk)
Cycle times reductions
Standard work
Availability
How the Gains Were Achieved
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Quantity Control Techniques Applied
Jidoka
One-piece flow, small lot flow
Balancing to takt
Minimizing lot sizes
Reducing bothWIP and lead times, which caused asignificant improvement in the flow
Quality was improved.
Lead times were reduced.
The cost to produce was reduced.
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1. Reduce processing time
2. Reduce piece wait time
3. Reduce lot wait time
4. Reduce process delays5. Manage the process to absorb deviations, solve problems
6. Reduce transportation delays
7. Reduce changeover times; employSMED
Application of The Seven
Techniques to Improve Flow
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And the Story Goes OnThank U