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7/30/2019 BWRO Silica 65 Ppm Case Study Results
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Operational Experience With BWRO Membrane Fouling With High Silica
Groundwater
N.W. Swain*#
Arup Water,
Level 2, Optus Centre, 431-439 King William Street, Adelaide, SA 5000, Australia
Tel. +61 (8) 8212-5580; Fax +61 (8) 8212-5590; email: [email protected]
Abstract
A brackish water reverse osmosis plant (BWRO) treating groundwater with silica levels up to 65 mg/L was
installed in October 2000 to supply 1,300 m per day of potable water to the township of Yulara in the Northern
Territory of Australia. This paper presents data from 827 days of operation for this high silica BWRO
application, demonstrating that designers of such applications should allow contingencies for reduced recovery,
increased cleaning and reduced membrane life. The BWRO was operated at an average recovery of 73% using
a silica specific antiscalant compared to the design target of 76.8%. At this recovery fouling of the membranes
was experienced but was managed by cleaning with an ammonium bifluoride solution every 87 days. Cleaning
was not completely effective in removing the fouling and the membranes had to be replaced after 2 years,
compared to the target 3 years. The reduced recovery, specialised cleaning and reduced membrane life due to
the silica scaling was estimated to add 4.6 per m3
to the cost of producing the water, around 4% of the full cost
of treatment.
1. Introduction
In October 2000, a brackish water reverse osmosis plant (BWRO) was installed to supply
1,300 m per day of potable water to the township of Yulara in the Northern Territory of
Australia. Yulara is the gateway to one of Australias premier tourist attractions, the Uluru
and Kata Tjuta National Park and serves more than 350,000 international and local visitors
each year. Water infrastructure at Yulara is owned and operated by Power and Water
Corporation, a Northern Territory government corporation that engaged Arup Water to
undertake concept design, tender documentation preparation and project management for the
provision of the BWRO. The plant was supplied by QED Occtech under a design and
construct contract and replaced an electro dialysis reversal (EDR) plant that had been inoperation since 1983. BWRO was selected in preference to EDR during the tender stage due
to lower overall costs.
The feed water for the plant is sourced from the Dune Plains aquifer and contains up to
2,200 mg/L of total dissolved solids (TDS) and 65 mg/L of silica. The aquifer is recharged on
an irregular and unpredictable basis. The unreliable nature of the recharge necessitates strict
groundwater resource conservation in this arid environment. To this end it was vital to
maintain as high a recovery as possible from the BWRO but it was understood from the
outset of the project that this goal would be limited by the potential for silica scaling.
This paper presents data from 2 years of operation for this high silica BWRO application
demonstrating that designers of such applications should allow contingencies for reducedrecovery, increased cleaning and reduced membrane life.
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2. Water Treatment Plant Description
Raw water to the Yulara Water Treatment Plant is a blend of five individual bores and has atypical analysis as presented in Table 1. Upstream of a reverse osmosis stage (RO), the water
LVSXPSHGWKURXJKD PVFUHHQD89GLVLQIHFWLRQXQLWDQGILQDOO\D PFDUWULGJHILOWHUThe water is dosed continuously with a silica specific antiscalant and fortnightly with a non-
oxidising biocide. The RO was configured with Hydranautics 8 ESPA1 elements in twostages with seven pressure vessels and 42 elements in the first stage and three pressure
vessels and 18 elements in the second stage. The design capacity was 1,300 m3
per day at a
recovery of 76.8% giving a flux of 24.2 L/m2/h. Following RO, the water is blended with a
side stream of raw water, passed through a degassing tower and finally dosed with caustic
soda and chlorine to achieve the desired water quality.
Table 1. Typical Blended Bore Water Quality (all mg/L unless stated or pH)
Parameter Value Parameter Value Parameter Value
pH 7.2 Na 339 Al
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On the basis of successful reference sites for the antiscalant proposed and the fact that aside
from hardness there appeared to be no obvious additional risk factors, the tendered design
was accepted.
4. Operating Data
Operating data for the 827-day period from start up on October 31, 2001 to February 5, 2003
was examined. The plant operates according to the levels in the treated water storage tanks
and on average operated for 18.6 hours per day, meeting an average demand of 900 m per
day. Table 2 presents a comparison between the predictions at the design stage with the
average values for this period.
Table 2 Comparison of Design Predictions with Actual Operation
Parameter Design Actual
Permeate Production Rate 1,300 m per day 1,160 m per day
Recovery 76.8% 73%
Flux 24.4 L/m/h 21.7 L/m/h
Feed Pressure-New Membranes 10.0 bar 10.6 bar
Feed Pressure-Old Membranes 11.1 bar
(@ 3 yrs)
12.0 bar
(@ 2.5 yrs)
Table 2 shows that the design targets have not been met. This is due to fouling being more of
a problem than anticipated. A recovery of around 73% has been adopted and while this
appears to be achievable, it has not been rigorously optimised.
Figure 1 and Figure 2 present trends of membrane permeability over the period examined
showing a gradual reduction in the overall membrane permeability from a starting point of
40 L/h/m2/kPa to 26.6 L/h/m
2/kPa at the end of the period examined, a reduction of 34%.
Both figures reveal that the silica fouling was managed via regular cleaning, however it can
be seen that cleaning would not fully restore permeability. At many sites a reduction inpermeability of 34% would be considered unacceptable but it was tolerated as there was
sufficient spare capacity available.
From Figure 1 and Figure 2 it should be noted that:
A faulty flowmeter causing a high (but unknown) recovery resulted in catastrophic
fouling on plant start up.
An apparent increase in permeability of stage 1 in May 2002 was due to failure of
seals and leakage of raw water into the permeate tubes.
The permeability of Stage 1 has also decreased although not to the same extent as
Stage 2. The reason for this has not been investigated.
Figure 3 presents the trend of normalised permeate TDS over time. Many of the increases in
TDS including the excursions during the May 2001 to March 2003 were caused by
problems with leaking permeate tube seals. However the general trend shows a gradual
increase in permeate TDS consistent with fouling. Cleaning had the expected effect of
reducing the TDS of the permeate.
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5. Evaluation of Silica Scaling Management Strategy
Silica scaling has been primarily managed by the use of a silica specific antiscalant and
regular cleaning. In general, the best silica antiscalant is selected by test work or field
trials [5] and in this case two proprietary silica specific antiscalant chemicals have been used.
Permatreat 510 supplied by PermaCare was used from plant start up until October 2002 after
which it was changed to MT1300i supplied by QED Occtech in an effort to see if the rate offouling could be reduced. It is unclear from the data presented in Figure 1 and Figure 2
whether this change has had any significant impact. However the plant operators are
continuing to use the MT1300i.
Periodic cleaning of the membranes is undertaken using an ammonium bifluoride based
chemical solution and cleaning procedure developed by the plant supplier QED Occtech. A
key element of the procedure is to circulate the cleaning solution for no longer than 3 hours
otherwise a reduction in membrane permeability may be experienced for two to three
days afterwards [5]. The supplier claims that this cleaning removes the order of 97% of the
silica. Although the removal rate cannot be practically quantified, the fact that membrane
permeability could not be restored suggests that cleaning was indeed less than 100%. The
membranes were cleaned on 10 occasions during the period examined, i.e., an average ofevery 83 days. The cleaning operation was effective in restoring membrane permeability in
the short term as illustrated in Figure 2. However over the longer term the membrane
permeability has deteriorated at relatively high rates, most likely due to a combination of
incomplete removal of scale and damage to the membranes by the cleaning operation. The
membranes were replaced on 20 May, 2003 as the plant could not meet an increased demand.
The resultant membrane life was around 2 years compared to the 3 years that was originally
expected. It is planned to conduct autopsies on the membranes removed to provide further
insights on the fouling problems.
A key question arising from the evaluation of the silica management strategy is what is the
impact on the cost of operation of not meeting the original design expectations? The author
has estimated that the cost of these items amounted to a total of 4.6 /m3, made up of
contributions from reduced recovery (1.2 ), increased cleaning (1.3 ), higher operating
pressures (0.5 ) and reduced membrane life (1.6 ). The additional cost is in the order of 4%
of the full cost of treating the water.
6. Conclusions
A review of the operation of the Yulara BWRO with 65 mg/L of silica in the feed feedwater
has identified that:
An achievable recovery was 73% using a silica specific antiscalant and this corresponds
to a nominal silica level in the brine of 240 mg/L.
Cleaning of the membranes was required every 80 days with an ammonium bifluoride
solution.
A membrane life of 2 years was achieved.
The additional costs due to the silica fouling were in the order of 4.6 per m3, around 4%
of the full cost of treatment.
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Acknowledgements
The author would like to thank Power and Water Corporation for giving permission to
publish this paper and to Neil Poulton, Andrew Mills and Mark Skinner of Power and Water
for their assistance in preparing the paper.
References
[1] Koo T, Lee Y.J., Sheikholeslami R, Silica Fouling and Cleaning of Reverse Osmosis
Membranes, Desalination 139(2001), 43-56.
[2] Darton E.G., RO Plant Experience with High Silica Waters in the Canary Islands, EDS
Conference, Desalination and the Environment, Las Palmas, November 1999.
[3] Sheikholeslami R, Tan S, Effects of Water Quality on Silica Fouling of Desalination
Plants, Desalination 126(1999), 267-280.
[4] Sahachaiyunta P, Koo T, Sheikholeslami R, Effect of Several Inorganic Species on Silica
Fouling in RO Membranes, Desalination 144(2002), 373-378.
[5] Wende N, QED Occtech, personal communication, 27/7/03.
Figure 1 Trend In Overall Membrane Permeability
15
20
25
30
35
40
45
10/11/2000 1/19/2001 4/29/2001 8/7/2001 11/15/2001 2/23/2002 6/3/2002 9/11/2002 12/20/2002 3/30/2003
Permea
bility
(x10^3L/h/m
2/kPa
)
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Figure 2 Trend In Stage 1 and Stage 2 Membrane Permeability
(arrows show cleaning events)
Figure 3 Trend In Normalised Permeate Total Dissolved Solids
0.00
10.00
20.00
30.00
40.00
50.00
60.00
10/11/2000 1/19/2001 4/29/2001 8/7/2001 11/15/2001 2/23/2002 6/3/2002 9/11/2002 12/20/2002 3/30/2003
Permea
bility
(x10^3L/h/m2/k
Pa
)
Stage 1
Stage 2
0
50
100
150
200
250
300
350
10/21/2000 1/29/2001 5/9/2001 8/17/2001 11/25/2001 3/5/2002 6/13/2002 9/21/2002 12/30/2002 4/9/2003
Date
NormalisedTDS(mg/L)