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1
CII18th National Award for Excellence in Energy Management-2017
Fortis Healthcare Ltd,Mohali
2
FHM- BRIEF INTRODUCTIONFortis Hospital Mohali Establishes in 2001, and today we are considered to be one of India's most recognized Super specialty hospital.
Hospital set on sprawling 8.22 acres, with built up area of 50336 square meters.
FHM is a 360(435) bedded, JCI and NABH certified multi specialty tertiary care hospital,
Fortis Hospital, Mohali has won several awards, including; Best Design Award from American Institute of Architects,1999
Number of Buildings: 3• IPD Block (A block)• OPD Block (B block)• Rehabilitation Centre• Fortis Cancer Institute
Best Design Award from American Institute of Architects,1999
3
OUR ENERGY & ENVIRONMENTAL POLICYWe Believe In
• Identify, control and endeavor to reduce emissions, waste & inefficient use of resources & energy.
• Measure and periodically review our progress and strive for continuous improvement.
• Protect the safety & health of our employees and patients and minimize the environmental footprint for our operations.
• Commitment to supply energy on 27x7 basis
4
Benchmarking – Energy Usage- Our ChallengesCurrent – Consumption patterns ,Perpetual growth in facilities thus increased Energy, additional beds expansion.
Consumption patterns aren’t fixed, they vary depending on the number of occupied beds, the footfalls & the local weather conditions. Increasing energy &Maintenance costs.
EquipmentAve.
Consumption
HVAC (heating, ventilation, & air conditioning)
40-50%
Lighting 10-15%
Medical Equipment 10-15%
Boilers 10-12%
Water Systems 8-10%
DG Sets (Diesel generator) 2-3%
Laundry 2-3%
Medical Gases 1-2%
STP (sewage treatment plant) 1-2%
Lighting 10-15%
Medical Equipment
10-15%
Boilers 10-12%
Water Systems 8-10%
DG Sets 2-3%
Laundry 2-3%
STP 1-2%
Medical Gases 1-
2%
HVAC 40-50%
1-1.5 % of Revenue
now spent on Energy
5
60126246
7009 7116
72907526
179 149 145 141 137
2011 -12 2012 -13 2013 -14 2014 -15 2015-16 2016-17
0
20
40
60
80
100
120
140
160
180
200
0
1800
3600
5400
7200
9000
CO
NN
ECTE
D L
OA
D IN
KW
H
----CONNECTED LOAD IN KWH --SEC
Additional Load & Specific Energy Consumption YOY
SEC
(K
WH
/SQ
M)
145
New Machines PET Scan and new NICU ward
New Machines Gamma Scan and new lifts
Additional Block FCI
Project
How to further nullify the
effect?
6
On line monitoring of chillers and strict controls on validation velocity meters by entire area cfm/validation
List of Projects with No investmentSAVINGS/YEARPROJECT TITLE Glimpse
0.75LkWh
Rs.5.36 Lacs
2.25LkWh
Rs.16.87 Lacs
0.10LkWh
Rs.1.20Lacs
2x20kva and 2 x 60 kva ups got stopped and connected with central UPS thus optimized its operation
Water conservation by utilizing STP Water in Toilets as wel as Cooling Towers
Cooling towers Aluminum Fan replaced with FRP Fans
0.05LkWh
Rs.0.40Lacs
Reduction of water pressure to 2.5Kg/cm2 by disconnecting overhead tanks from the Hydro Pneumatic System
0.10L kWh
Rs.1.20Lacs
Boiler operation optimization by rerouting of piping for minimum transmission losses
1.60KLitres
Rs.8.80Lacs
7
List of EnCon Project with InvestmentSAVINGS/YEARPROJECT TITLE (FY 2014-15) Glimpse
4.72LkWh
Rs. 49.0Lacs
Investment
Rs.33.71 Lacs
0.47LkWh
Rs. 40.0Lacs
Rs.23.66 Lacs
0.28LkWh
Rs. 51.0Lacs
Rs.2.6 Lacs
0.13LkWh
Rs. 0.37Lacs
Rs.0.95 Lacs
0.75LkWh
Rs.7.0Lacs
Rs.5.36 Lacs
Led Lights
Solar Lighting
Rain water harvesting
LDR and motion sensors
Energy efficient cooling towers replaced
CO2 EMISSIONS REDUCTION- 455MT/PA
8
List of EnCon Project with InvestmentPROJECT TITLE (FY 2015-16) SAVINGS/YEAR Investment Glimpse
Replacement of energy efficient primary and secondary pumps and condenser pumps as per tailor made design
Another ENERGY EFFICIENT COOLING TOWER replacement( Balance left)
Highly energy efficient elevator installed with approx. 55% energy efficient gearless motor for cons
Replacement of Conventional Motors with Energy Efficient Motors.
Energy efficient LED lights Placed at Number of Places ( 2nd phase)
3.06LkWh
Rs. 24.48Lacs
Rs.24.4Lacs
0.60LkWh
Rs. 8.02Lacs
Rs.4.50 Lacs
0.58LkWh
Rs. 30Lacs
Rs.3.98 Lacs
1.00LkWh
Rs. 4.25Lacs
Rs.7.50Lacs
2.69LkWh
Rs. 17.23Lacs
Rs.15.8Lacs
CO2 EMISSIONS REDUCTION- 455 MT/PA
9
List of EnCon Project with InvestmentPROJECT TITLE (FY 2016-17) SAVINGS/YEAR Investment Glimpse
Replacement of Old Compressor with VFD operated Efficient Motor
VFD on AHU's identified for OT Operations
Replacement of Old inefficient Cooling Tower with new High Efficiency Cooling Tower
LED Lights Replacement for 2500 balance CFL Lights
200Kw Solar Photovoltaic Roof Top Plant
1.16LkWh
Rs. 4.50Lacs
Rs.12.93 Lacs
1.21LkWh
Rs. 7.0Lacs
Rs.13.31 Lacs
0.20LkWh
Rs. 5.0Lacs
Rs.2.46Lacs
3.0LkWh
Rs. 98.0Lacs
Rs.34.82Lacs
0.28LkWh
Rs. 4.0Lacs
Rs.3.0 Lacs
Addition in Capacitors in Capacitor bank as well as machines end
Installed PowaTrim to at main EB incommerTo protect against spikes etc and improves PF.
0.50LkWh
Rs. 1.10Lacs
Rs.3.75Lacs
1.68LkWh
Rs. 10.67Lacs
Rs.13.51Lacs
10
List of EnCon Project with InvestmentPROJECT TITLE (FY 2016-17) SAVINGS/YEAR Investment Glimpse
Water Conservation by utilizing STP water in toilets etc
HSD savings in steam and boiler operations Rs. 4.50Lacs
1.21LkWh
Rs.13.31 Lacs
0.10LkWh
Rs. 6.0Lacs
Rs.3.0 Lacs
HSD savings in Boiler steam
CO2 EMISSIONS REDUCTION- 790 MT/PA
11
Encon Initiatives-1Replacement of Old inefficient Cooling Tower with
new High Efficiency Cooling TowerCBA
Energy Savings 20000 kWh/Year
HSD Savings 2000 Ltrs/Years
Cost Savings 2.46 Lacs/YearInvestment 7.0 LacsPayback 32 Months
Statement
• As a part of Energy Saving initiative end of life equipment contributing energy losses, were planned to replaced
CO2 EMISSIONS REDUCTION- 21.6
MT/PA
12
Encon-2 Water conservation by utilizing of waste
STP Water in Toilets as well as Cooling Towers
CBA
Energy Savings 10000 kWh/YearHSD Savings 1000 Ltrs/YearsCost Savings 12.0 Lacs/YearInvestment NilPayback Immediate
Statement
• To maintain Ground water table, water conservation project selected
• Reduction in bore well usage• 2-3% energy savings• 10-12% bore well water saved
CO2 EMISSIONS REDUCTION- 10.8 MT/PA
13
ENCON-3 VFD on AHU’s identified for OT Operations
CBA
Energy Savings 121250 kWh/Year
HSD Savings 9000 Ltrs/Years
Cost Savings 13.31 Lacs/Year
Investment 4.5 Lacs
Payback 5 Months
Statement
• Wasteful Energy losses were controlled during night hours by placing VFD’s for energy saving purpose
• 15-20% energy savings
CO2 EMISSIONS REDUCTION- 123.27 MT/PA
14
Encon-4 LED Lights Replacement for 2500Balance CFL Lights
CBA
Energy Savings 116000 kWh/Year
HSD Savings 9000 Ltrs/YearsCost Savings 12.93 Lacs/YearInvestment 5.0 LacsPayback 5 Months
Statement
• As a part of Energy conservation afford balance left out CFL lights replaced with LED Lights
• 5 years warranty, hence R&M cost reduced
• 40-45% energy savings
CO2 EMISSIONS REDUCTION- 118.11 MT/PA
15
ENCON-5 200Kw Solar Photovoltaic Roof Top Plant
CBA
Energy Savings300000 kWh/Year
HSD Savings 26000 Ltrs/YearsCost Savings 34.82 Lacs/YearInvestment 98.0 LacsPayback 36 Months
Statement
• For clean/renewable energy initiative rooftop was utilized by placing 200Kw clean energy Solar PV panels thus reducing the heat load on Third floor beside generating renewable energy
• 3-4% EB units savings
CO2 EMISSIONS REDUCTION- 313.60 MT/PA
16
CBA
Energy Savings 50000 kWh/Year
Cost Savings 3.75Lacs/YearInvestment 1.10 LacsPayback 4 Months
StatementMaintaining power factorProblemWith PSPCL started billing us on KVAH instead of kWh.Since ours is an inductive load contributed by high end chillers, motors electronic machinesMaintaining power factor to near to one is a challengeResult After careful study placed capacitor near the chillers, machines as well as in automatic main capacitor panel
EnCon-6 Project improvement in Power Factor
CO2 EMISSIONS REDUCTION- 42.30.11 MT/PA
17
Energy saving calculation is determined on the basis of actual kW consumption of
old and new pumps.
Running hrs of chiller-3 & 4 are 6000 hrs/year as per average for last 2.5 years.
On analysis we find that the total electrical energy saving is 306000 kWh/year.
Total monetary saving is 22.03 Rs Lakh/Year.
Payback period for pumping system is 13 months.
Encon-8Commissioning of New Energy Efficient Tailor made designed
Pumps in HVAC section with VFD
Before After
CO2 EMISSIONS REDUCTION- 258.88 MT/PA
18
Solar water heating
Outcome: • 57 Tones of CO2• Equivalent 148 trees planted• Savings in Million Rs. 1.98
Results Achieved on Green Initiatives
CO2 EMISSIONS REDUCTION- 57 MT/PA
19
60126246 7009 7116
7290 7526
179
149 145 141 137
130
2011 -12 2012 -13 2013 -14 2014 -15 2015-16 2016-17
0
20
40
60
80
100
120
140
160
180
200
0
1800
3600
5400
7200
9000
CO
NN
ECTE
D L
OA
D IN
KW
H
----CONNECTED LOAD IN KWH --SEC
Results:Additional Load & Specific Energy Consumption YOY
SEC
(K
WH
/SQ
M)
145
New Machines PET Scan and new NICU ward
New Machines Gamma Scan and new lifts
Additional Block FCI
Project
20
• 18.7 % reduction achieved in last 3yearsEnergy Efficiency
• 15.1 % reduction in last 3 yearsWater Conservation
• Using 19 % Renewable EnergyRenewable Energy
• 30.7 % Reduction in GHG Emission since last 3 yearsGHG Reduction
ENCON EFFORTS: KEY IMPACT
Special Focus on Reduction of “Energy” and “Water” Consumption
• 28% Reduction in thermal energyThermal Energy
• 13% Reduction in Hazardous Waste and 24% Reduction in Process Effluent in last 3 years
Water Management
• Environment friendly HK/Cleaning agents & Chem. Green Supply Chain
• 8Project recognized as innovative projects
• Started use of Eco friendly HK chemical and paintsOthers
Key ImpactArea
21
SPECIFIC ENERGY REDUCTION
Parameter 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
KWH 7487915 7138206 7058913 6998773 6805785 6568395
SEC in kWh/M2
179 149 145 141 137 130
Total kWh/Bed
26838 24530 21787 20111 16014 15100
No. Of Beds 279 291 324 348 425 435
Average Occupancy
76% 73% 78% 82% 88% 89%
Built Up area 41,760 47,791 48,719 49,720 49,720 50,336
22
YEAR KWH (LAC)
2011-12 74.88
2016-17 65.68
SAVINGS 9.2LAKHS
0
20
40
60
80
100
120
140
160
180
200179
149 145 141 137130
200
SPECIFIC ENERGY CONSUMPTION kwh/M2
National Bench mark 200 KWh/ sq. mtr./ year (reference Bureau of Energy Efficiency, Govt. of India ECO-III project)
31.28%
Reduction
24
EPI Index across Fortis
Energy performance Index for Fortis Group Hospitals All Weather
0
0.5
1
1.5
2
2.5
3
3.5
4
4.5
1.65 1.73
1.03
4.3
1.42
1.76
1.49
2.48
1.99
1.56
1.28
2.5
2.13
1.19
1.81.94
1.42
1.92
1.35
1.74
ENERGY PERFORMANCE INDEX (EPI)
Fridabad
Ludhiana
Shalimar Bagh
Kalyan
SL Raheja
Jaipur
RajaJi Nagar
Raipur
Escorts, Okhla
Anandpore
FMRI, Grn
Malar
CG Road
Mohali
Vashi
Mulund
Nagarbhavi
25
International Benchmarking
Comparison of building energy benchmarks in Serbia, UK and Germany
(CIBSE TM 46), (EnEv)----- KWH/M2
Specific Energy Consumption -kWh/Sq.Mtrs./year
0
50
100
150
200
250
300
UK-Typical Practice Germany-Typical Practice
Serbia-After Refurbishment
Fortis Hospital Mohali
International Bench mark
263
225
205
130
205
Kwh/m2
26
ENCON Roadmap – Sustaining continual improvement
Condensate recovery from
Boilers
25000units & 12 tons HSD per Annum
Energy Efficient LED
Lights Phase II
50000 units/annum
Biomass Gassifier
2ton HSD/Annum
VFD Operated Vacuum Pumps
70000 Units/Annum
Solar Water Heating System
50000 units and 42 MT of CO2 REDUCTION
Geo Thermal System for HVAC
250000 units & 211MT of CO2
REDUCTION
Solar Photovoltaic
Lighting
300000Units & 253 MT of CO2
EMISSION REDUCTION
Right now % Renewable Electrical
14.2%
PNG for Boilers
469 MT of CO2 reduction
ENCON Roadmap – Sustaining continual improvement
19.2% by 2017
27
With increase in bed strength and new Operation Theatres commissioning
the working of Air compressor increased during day time but night time the
working was normal and hence old Air –Compressors were not giving
optimum results and huge energy losses were felt.
Innovative Project (1)Optimum and Efficient usage of Air Compressor Operation
Thinking /Brain Storming Phase:
After observing the data on year to year basis Engineering team felt the
need that a lot of energy is being getting wasted and observed that even
night the energy is getting wasted as Air compressor was hardly getting
stopped
28
Action Plan:Phase -1
o Planned and stopped the air compressor during idle running at night.
Phase -IIReplaced the Air compressor with VFD operated with high efficiency motor.
Optimum and Efficient usage of Air Compressor Operation
BeforeAfter
29
Annual Energy Consumed (KWH) 160600
Annual Energy Cost (In Rs.) 130124
Energy Saved (In KWH) 30474
Energy Cost Saved Annually (in Rs.) 228555
Before modification: Rhrs 24 hrs/day
After modification: RHrs
13-14 hrs/day
Results achieved
Optimum and Efficient usage of Air Compressor Operation
30
INNOVATION PROJECT -2 PowaTRIM
Corrects Power Factor
Protects Against Surges & Spikes
Reduces kVAh, kWh & Cost
31
PowaTRIMAll PowaTRIM savings are determined by the site inductive load profile, typically:
kVAh & kWh. By the amount of current that’s
magnetically induced into circuit.
Approx. 70% of savings.
Surges and spikes (IE).“Dirty Power” that’s
filtered & re-introducedas usable power.
Approx. 20% of savings.
Total harmonic currentreduction.
Approx. 5% of savings.
I2R losses due to poor powerfactor.
Approx. 5% of total savings
In addition to the hard savings, PowaTRIM also provides soft savings, such as extension of motor life and spike/surge reduction, reducing motor & spike repair costs.
32
Energy Saving Results from PowaTRIM at Fortis Healthcare Mohali
Invoice value in Rupees Rs. 1,067,339
Average kVAh savings per hour 19.3
hours per day 24
days per annum 365
kVAh savings per annum 168,939
kVAh cost in Rps Rs. 8
Gross Savings per annum Rs. 1,351,509
ROI in Months 9.5
33
Innovative Project (3)Optimum AHU Operation in operation theatres during night
AHU’s are the life line for the hospital operation theatres, not only maintaining
temperatures are important but beyond that humidity controls too. At Fortis
Hospital ,Mohali the operation theatres are designed with 100% fresh air to
avoid any infections but at the same time it is a challenge for Energy Managers
to have its operation cost effective. Because 100 % fresh air means cooling air
from ambient of 42 -44 deg to less than 22deg.has its toll on chillers and hence
less energy efficient operation.
Thinking /Brain Storming Phase:
Engineering team took this initiative and a brain storming session it was
decided to talk to Infection control and quality teams.
34
Optimum AHU Operation in operation theatres during night
Action Plan:
Phase -1
o Raising the temperature of OT during off hours when the surgery is notscheduled.
Phase -IIo Running of one motor for giving air to 2-3 OT’s.
Challenges / Risk Involved o Increase in Infection rate when temperature goes up.
CONCLUSION
o We made modification in ducting by placing dampers in the duct supply.
o Besides this during night CFM were reduced and instead of running 3 20 HP motors we managed to run OT’s and its modulation with one motor only.
35
Thus 30KW motor running each day was stopped for 8 -10 hours and 16-18 hours on Sundays resulting in an energy saving of 96960 units PA.
o Besides less AHU motor running resulted in enhanced life/less wear and tear.
o Less Chiller operation resulted in 23960 units more.
Optimum AHU Operation in operation theatres during night
37
Monitoring System
Monitoring
Online energy data capturing system
Online HVAC monitoring system (BMS)
Energy meters for load capturing
Reporting
Daily energy report
Monthly report on the energy indices
Monthly performance review
Energy trends analysis
Monitor
Analyze
Improve
17-Jun-16
Today Budg. MTD Act.MTD Budg.YTD Act.YTD
%Var
MTD
%VarY
TD 17/06/2015 MTD Diff. MTD. Jun-15
Energy consumed for the day units 24870 378533 413070 1605533 1730785 -9.12 -7.80 25830 397650 15420 720045
Total Day unit 14505 244610 1024835
Total Night unit 10365 168460 705950
D.G. unit 0 7987 34181 0 5211 2776 8742
Total unit 24870 421057 1764966 25830 402861 18196 728787
Power factor 0.99 0.99
H.S.D.Consumption in Boilers(Ltrs) 700 12215 56065 695 12435 -220 21710
H.S.D.Consumption in D.G.(Ltrs) 0 2216 9495 0 1425 791 2419
Total H.S.D. Consumption (Ltrs) 700 16433 14431 76439 65560 12.18 14.23 695 13860 571 24129
Medical Gas Oxygen Consumption 1310 22417 104558
Medical Gas Nitrous oxide Cons. 0 7 24
Energy consumed for Chiller TR 1 4320 57840 203520 4320 41280 16560 95760
Energy consumed for Chiller TR 2 1200 18960 68880 1200 20160 -1200 36480
Energy consumed for Chiller M/C 4 2093 49953 197975 3293 61353 -11400 101936
Total unit 7613 126753 470375 8813 122793 3960 234176
Oncology block Consumption 2317 34250 144699 2293 35666 -1416 64143
Energy consumed MRI Unit 570 9960 46020
Energy consumed for Laundry 262 4350 19334
Energy consumed for CSSD 168 2344 12680
Energy consumed for Rehab 664 11216 44976
Energy Genrated by Solar System 69 1273 6482
Energy consumed for PET CT 100 1745 7915
Energy consumed for LINAC 104 1780 7752
Raw Water total production(KL) 640 11430 46090
Raw Water Consumption (KL) 497 8481 27637
Municipal Corporation water (KL) 13 201 947Solar water system Cons.(KL) 25 533 2107
Running time of Equip. (hrs)Running time
of Equip. (hrs.)Running time of Equip. (hrs.)
Running time
of Equip. (hrs.)YTD Budget
Running
time of
Equip.
(hrs.)
Running time
for Eqpt. (hrs)
Act.MTD
2015
Act.YTD
2015-16
PSEB power fail 0.00 NA 9.05 NA 35.35 0.00 5.40 37.20
Chiller no-1 0.00 NA 0.30 NA 0.40 0.00 5.40 7.50
Chiller no-2 0.00 NA 0.50 NA 0.50 1.30 5.55 7.50
Chiller no-3 14.15 NA 162.55 NA 543.25 9.45 77.40 489.00
Chiller no-4 8.20 NA 195.50 NA 777.05 13.00 242.15 761.25
HW Generators-2 0.00 NA 0.00 NA 0.00
Boiler no-1 11.55 NA 152.20 NA 628.89
Boiler no-2 13.07 NA 155.64 NA 626.16
Boiler no-3 0.72 NA 114.63 NA 389.22
Boiler no-4 0.00 NA 5.60 NA 318.75
DG-1 0.00 NA 5.35 NA 25.05
DG-2 0.00 NA 1.00 NA 11.05
DG-3 0.00 NA 7.35 NA 20.40
BOREWELL-1 9.75 NA 192.92 NA 648.37
BOREWELL-3 3.00 NA 29.45 NA 298.20
RO- WTP 25.00 NA 376.00 NA 1471.20
AIR COMPRESSOR-1 0.00 NA 0.00 NA 0.00
AIR COMPRESSOR-2 0.00 NA 0.00 NA 0.00
AIR COMPRESSOR-3 0.00 NA 75.00 NA 294.00
AIR COMPRESSOR-4 6.83 NA 107.48 NA 539.15
AIR COMPRESSOR-5 5.55 NA 48.58 NA 316.22
VACUUM PUMP-1 0.00 NA 23.07 NA 729.90
VACUUM PUMP-2 11.44 NA 197.16 NA 874.12
VACUUM PUMP-3 12.00 NA 166.50 NA 166.50
VACUUM PUMP-4 0.00 NA 20.53 NA 54.87
VACUUM PUMP-5 1.91 NA 21.23 NA 51.54
AGSS 20.00 NA 212.67 NA 919.77
38
Water – Conservation Methodology
Use of New Technology
Automated Water Taps
Sprinkler System for Irrigation
Automated Urinals
Water Recycling
STP Plant
ETP Plant
UV/SOFTNER in STP
RO Reject Water
Innovation
MGF Backwash
AHU Condensate
Cooling Tower blow down Reuse
Efficiency Improvement
Benchmarking
Auditing
Monitoring & Analysis
Improving
Renewable Substitution
Rain Water Harvesting
Municipal Waste Water Treatment and Reprocessing
MOHALI
Average Water Consumption Reduction
0
50
100
150
200
250
300
350
400
2011-12 2012-13 2013-14 2014-15 2015-16 2016-17
300315
330
375
345
280
Wat
er
Co
nsu
mp
tio
n in
KL
Water Consumption/Day (KL)
2011-12
2012-13
2013-14
2014-15
2015-16
2016-17
40
EMPLOYEE INVOLVEMENT /TEAM WORK • Suggestion from all levels of employees
on energy conservation• Training/Awareness for contract
labour/office staff on energy conservation.
• Sharing best practices among the industries
• Objective are set for employees on reduction in energy and water .
• To adopt safe and hygienic hospital procedures and practices
• Environmental safety and fire fighting training sessions
• Hand Hygiene campaign launched and Emphasis on 5S initiative
• Trainings imparted and monitoring done on Energy Conservation measures.
• Energy savings Efficiencies of Boiler, DG sets and HVAC are regularly monitored for timely maintenance and energy savings.
41
WORLD CLASS O&M PRACTICES FOLLOWEDPractice FORTIS,
MOHALI
Adaption of Energy Management System Yes
Adaption of Environmental Management System Yes
Use of automated building Management System Yes
Use of Energy performance Indicator (KWH/Pax, KWH/TR ) Yes
Metering of Tenant energy Yes
Reporting of carbon emission to CDP Yes
Conduct energy audits Yes
Internal & External Stakeholder engagement Yes
Sharing of best practices with others hospitals Yes
Use of renewal energy for day to day operations In Progress
Mapping & reduction of carbon emission as per ACA Yes
42
ACHIEVEMENT
•Natural lighting in patient areas•Green house keeping •Better Indoor Air Quality•Sound Reduction•Mercury free hospital•20t-40% Energy savings•35-40% water savings•Good day lighting•No sick building syndrome•Faster patient recovery
BEST PRACTICES FOLLOWED
43
UTILIZATION OF WASTE RENEWABLE ENERGYSNo Description of scheme Amount INR Year Remarks
1Installation of 4 nos Rain Water Harvesting pits for improvement of ground water table.
4750000 2014-16Annual saving of 1708 Units
2Energy efficient LED lights Placed at Number of Places
4900000 2014-15Annual saving of 472000 Units
4 STP water reused 750000 2014-16Annual saving of 10000 Units
5 Installation of LED lights (2nd Phase) 1723000 2015-16Units Saved 275000 annually
6 HSD Saved in boiler efficiency 75000 2015-1627500 liters of HSD saved
8 Solar Lighting 200 KW 9800000 2016-17Annual Saving of 300000 Units
11 Summary Co2 Emission Reduction 2460 MT (App) 13313000Savings
1057908Units
RESULTS OF BEST PRACTICES IMPLEMENTED
CO2 REDUCTION (2460MT)
Energy Reduction
(25,32,432kWh)
Cost Reduction
(Rs. 2,33,44,315)
45
Energy Conservation Measure YearSavings (LkWh)
HSD (KLtrs)
Savings (INR Lacs)
Investment (In Lacs)
ROI (Years)
Solar Photovoltaic Lighting 2017-18 3 0 22.5 98 4.5PNG for Boilers 2017-18 0 275 27.5 13.5 0.5Water conservation by utilizing STP water in Toilets as welas Cooling towers/gardens of entire Hospital
2017-18 0.10 1 1.3 0 0
VFD on Identified AHU’s 2017-18 0.70 0 5.25 4.5LED Lights replacement for balance CFL lights 2017-18 0.50 0 3.75 5 1.4Online Chiller Condenser tube cleaning System 2017-18 0.18 0 1.25 5 4Geo Thermal system to be stop usage of cooling towers for water cooled Chillers
2018-19 2.50 10 57.6 180 3.5
Condensate recovery from boilers 2018-19 0.25 12 8.48 0 0Hot water generation through solar water heating system
2018-19 0.50 30 20.25 42 2
Replacement of Vacuum Pumps with new VFD operated Vacuum Pumps
2019-20 0.30 0 2.25 3 1.4
Biomass Gassifier 2019-20 0 2 11 22 2Summary 676 MT of CO2 REDUCTION 8.03 330 161.13 373
New ENCON Plans for the next 3 YearsFUTURE PLAN
CO2 Reduction
676MT
46
Going Forward
Benchmarks 17762 KWh/Bed (By Bureau of Energy Efficiency, Govt. of India ECO-III project)
179 149 145 141 137 130 123 120 117
26838 24530 21787 2011116014 15100 13900 13000 12500
1
10
100
1000
10000
100000
2011-12 2012-13 2013-14 2014-15 2015-16 2016-17 2017-18 2018-19 Target
ROAD MAP FOR 2018-2020
kwh/M2
kwh/bed
Reduction of CO2emissions by 2476 MT