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“Despite requiring extensive civil structure modifications, the project was completed on time thanks to the support and experience of FLSmidth in completing retrofits”. MR. MOORTHY RAIN CEMENTS LIMITED Rain Cements Limited (RCL) has produced cement since 1986 at an annual output of up to 3.6 million tonnes. It’s two integrated plants located in South India are self-sufficient in all critical raw materials – limestone, additives and coal. RCL made an important decision to address inefficiencies in one of its existing systems at the cement plant based in Ramapuram, Mallacheruvu, Kodad in Nalgonda. They paid particular attention to the grate cooler, which was an older generation with low thermal efficiency, and high-energy consumption and requiring more maintenance. RCL approached FLSmidth to audit the cooler system in 2016. The audit involved taking detailed measurements of the existing cooler’s performance. The findings identified the potential to reduce cooler losses and create thermal and electrical energy savings, and as a result, FLSmidth recommended replacing and installing a more reliable, efficient cooler. Rain Cement’s South India-based Ramapuram plant has achieved impressive performance results following the successful replacement with an FLSmidth® Cross-Bar® cooler WE DISCOVER POTENTIAL Clinker cooler replacement delivers improved productivity at Rain Cement

Clinker cooler replacement delivers improved productivity

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Page 1: Clinker cooler replacement delivers improved productivity

“Despite requiring extensive civil structure modifi cations, the project was completed on time thanks to the support and experience of FLSmidth in completing retrofi ts”.

MR. MOORTHYRAIN CEMENTS LIMITED

Rain Cements Limited (RCL) has produced cement since 1986 at an annual output of up to 3.6 million tonnes. It’s two integrated plants located in South India are self-su� cient in all critical raw materials – limestone, additives and coal.

RCL made an important decision to address ine� ciencies in one of its existing systems at the cement plant based in Ramapuram, Mallacheruvu, Kodad in Nalgonda. They paid particular attention to the grate cooler, which was an older generation with low thermal e� ciency, and high-energy consumption and requiring more maintenance.

RCL approached FLSmidth to audit the cooler system in 2016. The audit involved taking detailed measurements of the existing cooler’s performance. The fi ndings identifi ed the potential to reduce cooler losses and create thermal and electrical energy savings, and as a result, FLSmidth recommended replacing and installing a more reliable, e� cient cooler.

Rain Cement’s South India-based Ramapuram plant has achieved impressive performance results following the successful replacement with an FLSmidth® Cross-Bar® cooler

WE DISCOVER POTENTIAL

Clinker cooler replacement delivers improved productivity at Rain Cement

Page 2: Clinker cooler replacement delivers improved productivity

CASE STORY

FIND OUT MORE THE PRODUCT ATWWW.FLSMIDTH.COM

Copyright © 2020 FLSmidth A/S. ALL RIGHTS RESERVED. FLSmidth is a (registered) trademark of FLSmidth A/S. This brochure makes no o� ers, representations or warranties (express or implied), and information and data contained in this brochure are for general reference only and may change at any time.

FLSmidth A/SVigerslev Allé 772500 ValbyDenmark

www.fl smidth.com

Tel: +45 36 18 10 00

WE DISCOVER POTENTIAL

Venkata Siva Ram Kollipara, Assistant General Manager at FLSmidth, sees the guarantees achieved on performance parameters as an indication of the Cross-Bar cooler’s exceptional performance and reliability:

“It pays to make the initial investment to reap the performance benefi ts well into the future. The success of this project demonstrates FLSmidth’s commitment to deliver impressive results through collaboration with our valued customers.”

The Cross-Bar® Cooler met the needs of RCL in terms of possessing ■ high thermal e� ciency, ■ reduced power consumption, ■ relatively low maintenance requirements ■ and low civil construction and operating costs.

The optimised design is fl exible enough to enable partial or complete upgrades of most existing old-generation clinker coolers.

The return on investment for RCL can be realised within an estimated four-year period, just from the energy benefi ts and fuel savings alone.

Performance of Rain Cement’s Cross-Bar® Cooler

Performance parameter

Before upgradation

After upgradation

Production (Mtpd) 2864 2910

Recuperation effi ciency (%) 68 77

Actual cooler loss (Kcal/Kg clinker) 149 110

Standard cooler loss (Kcal/Kg clinker) 131 92

Clinker temperature (Celcius)

112 degrees + ambient

57 degrees + ambient

Specifi c power consumption (Kwh/t)(Fans, drives and breakers)

4.6 4.4

The RCL project team emphasised that the quality of the equipment, including its durability, was key, along with delivery of the equipment in time for its effi cient installation within the planned shutdown period.