Upload
others
View
6
Download
0
Embed Size (px)
Citation preview
IFT\P2017-020
PERSISTENT SURVEILLANCE FOR
PIPELINE PROTECTION AND THREAT INTERDICTION
Depleted Uranium Hohlraum Process
Improvements
Javier Jaquez1, Martin Havre1, Tim Fuller1, Jason Wall1, Jorge Robles1,
Karina Kangas1, Abbas Nikroo2, Suhas Bhandarkar2
1General Atomics, P.O. Box 85608, San Diego, California 92186-56082Lawrence Livermore National Laboratories, P.O. Box 808,
Livermore, California 94550
22nd Target Fabrication MeetingLas Vegas, Nevada
March 12-16, 2017
This work performed under the auspices of the U.S. Department of Energy by General Atomics under Contract
DE-NA0001808 and by Lawrence Livermore National Laboratory under Contract DE-AC52-07NA27344 and
General Atomics IR&D Funds
IFT\P2017-020
General Atomics has dedicated equipment for
to process DU in support of the ICF program
U3 PVD system U2 PVD systemLathe
4mm 1mm 1mm 1mm
• DU is processed in a safe manner in compliance with state and federal
regulations
IFT\P2017-020
Depleted Uranium (DU) lined hohlraums have
advantages over Gold Hohlraums
• 30% less M-band radiation compared to Au allows for less
capsule pre-heat1
• Compared to Au hohlraums DU is more efficient in terms of
coupling incident laser energy into the capsule.– DU has a higher X-ray conversion compared to Au
– Less heat is absorbed into the wall with higher Z materials.
• ZAu=79, ZU=92
– Using less laser helps preserve the NIF optics
Hohlraum canIncident laser energy
1. N. B. Meezan, E. L. Dewald et al.,” http://meetings.aps.org/link/BAPS.2015.DPP.UO7.12
IFT\P2017-020
DU Hohlruam specifications are fairly stringent
~5 mm
Au Hohlraum
wall TorusFlange
575 scalePhysics
requirements Assembly
requirements
DU layer
5.75mm
DU linerAu liner, (varies)
Length Diameter DU liner Au liner* Au wall O at%
9.43-
11.24mm
5.75-
6.72mm
>7µm 0.7µm 23µm <5at%
*optional
IFT\P2017-020
The overall manufacturing process involves
many fabrication steps
E-Plate AuPVD Cu
Back-Machining Milling Leach CuLeach Al
Dimensional
Compositional
PVD DU/Au
Unlined hohlraums - Oxygen levels
NaOH NH4OH
Lined hohlraums - Au liner thickness
Auger Electron Spectroscopy
X-Ray Fluorescence
Defects
Nikon MM-400 (measured pre-leach)
Visual inspection
Turn Al mandrel
M1 coater U3 coater
IFT\P2017-020
0
2
4
6
8
10
12
14
16
09
/18
/20
14
12
/27
/20
14
04
/06
/20
15
07
/15
/20
15
10
/23
/20
15
01
/31
/20
16
05
/10
/20
16
08
/18
/20
16
11
/26
/20
16
03
/06
/20
17
Oxy
ge
n a
t% in
DU
Lin
er
Until recently the oxygen levels in many DU lined
hohlraums have been higher than NIF spec
– Oxygen levels within the the DU liner were found to be trending upwards
with the previous process
– The most recent process modification involves a change at the Cu liner
Low yield
process:
25%
Overall Yield: ~65%
Overall Yield: ~52%
NIF Spec
5 at%
IFT\P2017-020
The key process change was at the Cu liner
step
E-Plate AuPVD Cu
Back-Machining Milling Leach CuLeach Al
Dimensional
Compositional
PVD DU/Au
Unlined hohlraums - Oxygen levels
NaOH NH4OH
Lined hohlraums - Au liner thickness
Auger Electron Spectroscopy
X-Ray Fluorescence
Defects
Nikon MM-400
Visual inspection
Turn mandrel
M1 coater U3 coater
IFT\P2017-020
Changes to our production process have reduced
oxygen levels within the DU for unlined hohlraums
• In-situ etch functionality was added to our DU coating
system
– Previously this was performed in-situ with Cu deposition
0.0%
10.0%
20.0%
30.0%
40.0%
50.0%
60.0%
70.0%
80.0%
90.0%
0 500 1000 1500 2000 2500
Ox
yg
en
ato
mic
pe
rce
nt
nanometers
U3 In-situ old process
0.8at%4at%
300nm
• Active depth: 7um
• Important O remain low below 2um
depth (Active depth for foot)
• If high O level beyond 2um
the peak drive will be
affected
2000nm
IFT\P2017-020
The ion etch process is not the same between
systems
• Parts farther from ion source in the U3 system
– 6cm vs. 3.5cm
• Ion etch rate in M1 system ~3x higher
– About ~200nm removed in U3, 30min
– About ~600nm removed in M1, 30min
0
5
10
15
20
25
30
35
40
18-A
ug
7-S
ep
27-S
ep
17-O
ct
6-N
ov
26-N
ov
16-D
ec
5-J
an
25-J
an
etc
h r
ate
, n
m/m
in
M1 etch rate (Cu)
U3 etch rate (Cu)
IFT\P2017-020
Cu liner deposition step was found to be key to
oxygen variability within DU
• In-situ ion source etching is
key to good adhesion…too
much etching can damage
the Cu liner
• Data shows correlation
between etch time and
oxygen level
• Can infer the state of the Cu
layer before the etchant
steps leads to variability
(pinholes, etc.)
Work produced in collaboration with
Suhas Bhandarkar @LLNL
IFT\P2017-020
Direct evidence show leaching chemicals
oxidize DU
• AES was carried out on DU in
various states
0%
10%
20%
30%
40%
50%
60%
70%
80%
0 200 400 600 800 1000 1200
ato
mic
pe
rce
nt
nanometers
3 hr exposure 72 hr exposure
0%
10%
20%
30%
40%
50%
60%
70%
80%
90%
100%
0 1000 2000 3000 4000 5000
ato
mic
pe
rce
nt
nanometers
Oxygen Uranium Copper
Before any type of chemical leach exposure
After exposure to NaOH for 3 and 72 hrs
IFT\P2017-020
0%
20%
40%
60%
80%
100%
0 20 40 60 80 100 120
CU
MU
LTA
TIV
E Y
IELD
part count
Unlined Overall Yield
Lined Overall Yield
With the current process the overall yield is
maintained while reducing the oxygen content
coat E-plate BM Mill Leach Overall
unlined 92% 98% 98% 100% 65% 52%
lined 89% 99% 99% 100% 94% 75%
Unlined
Lined
52%
75%
• Previous process overall yield for unlined
parts was 65% (45%)
**If we take high O
into account
Early issues with new process
IFT\P2017-020
50%
60%
70%
80%
90%
100%
110%
0 20 40 60 80 100 120
CU
MU
LTA
TIV
E Y
IELD
PART COUNT
Unlined Coat Yield
Lined Coat Yield
DU coater yield with U3 in-situ ion etching >90%
• Historically this has been an issue with DU hohlraums
– Cu liner exterior etching introduced in 2015, brought coater
yield up to 96%
– Currently we’re better than the ex-situ Cu etching if initial startup runs are ignored, >95% for linerless designs
Lined
Unlined
Coater issues early on
92%89%
IFT\P2017-020
Primary failure mode at the DU coating step is
mechanically related
Yield out of U3 is >90%6.5% fail due to coater issues (D4)
2% are dinged or scratched (D1)1.5% of parts have delamination (D2)
>1% fail due to embedded debris (D3)
101
13
0
20
40
60
80
100
120
Pass Fail
U3#dep.#step#Pass/Fail
2
2
1
8
0 2 4 6 8 10
D1() ding/scratched(
D2() delamination
D3() embedded(debris
D4() coater(failure
Detailed(look(at(coating(failures
IFT\P2017-020
50%
60%
70%
80%
90%
100%
110%
0 20 40 60 80 100 120
CU
MU
LTA
TIV
E Y
IELD
part count
Unlined Leach Yield
Lined Leach Yield
DU flaking away is the primary cause of failure
at the leaching step
Unlined
Lined
8
12
1
4
1
7
6
4
1
0 5 10 15
LC1 - DU flaking off (Large)
LC2 - DU flaking off…
LC3 - majority of DU missing
LC4 - Large area peeling
LC5 - DU cracking
LC6 - interior bubble*
LC7 - edge delamination
LC8 - black matte interior
LC9 - LEH deflection
Unlined Leach FC
65%
94%
Main failure mechanism (unlined)
400um
200um
IFT\P2017-020
Part position within the coater makes a
difference
0 5 10 15 20
Coating
Failure
E-plaitng
Failure
Back-
machine…
Mill Failure
Leach Failure
Failure position by position
Position-5 Position-4 Position-2 Position-1
84%
60%
86%
19%
0%
10%
20%
30%
40%
50%
60%
70%
80%
90%
100%
Position-1 Position-2 Position-4 Position-5
%Yield at leach step
Currently investigating:• Etch rate differences
• Coating flux differences
• Equipment
2
1
4
5
IFT\P2017-020
Blisters are another defect of concern
Cracks (LC-5) Interior bubble (LC-6)
Edge delamination (LC-7)
• 12% of parts have blisters
• Any type of defect that is
perceived as possibly flaking
away is rejected as it could land
on the capsule causing meteors
IFT\P2017-020
The rate of blister occurrence has not changed
with in-situ ion etching
• The addition of the in-situ ion etch has not increased the occurrence
of blister formation
• We are shipping more parts out with blisters now than in 2015
• 3.4x increase in DU demand in 2016 over 2015 levels
0
5
10
15
20
25
30
35
0 20 40 60 80 100 120
%o
f p
art
s th
at a
re b
list
ere
d
part count
M1 etched (old process)
U3 in-situ etched (new
process)
355
535
391
56
83
248
0
100
200
300
400
500
600
700
CY2014 CY2015 CY2016
ho
hlra
um
s sh
ipp
ed
Au components
DU components
IFT\P2017-020
Conclusions
• Low-Z elements such as oxygen reduce hohlraum
drive
• By introducing in-situ ion etching into our process we
have drastically reduced oxygen levels within the DU
layer
• No difference in bubble occurrences between old
and new process
• Biggest issue we’re currently facing is leach process
failures
– Part position dependency observed
• 3.4 times as many DU hohlraums shipped in 2016
over 2015 levels
IFT\P2017-020