Experiance Sharing for Best Maintenance-L.K.jain

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    EXPERIENCE SHARING

    ADOPTING BEST PRACTICES&

    MARCH TOWARDS ZEROFORCED OUTAGE

    By L.K.JAIN/NCR-OS

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    220 KV BREAKERS

    While opening of 220 kv breaker one pole gotstuck up in closed condition, two poles opened.

    Aux contacts operated and breaker open statuswas available

    One pole operating rod disengaged fromcoupling of interrupter

    Generator continued to operate drawing currentfrom one pole which was closed Immediate action was taken to isolate generator

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    ACTION PROPOSED

    CARE TO BE TAKEN DURING ERECTIONSTAGE/OVERHAULING STAGE( To be

    included in FQA Check list) Breaker to be overhauled after 10 years of

    operation to over cum problems of pole

    stucking, contacts bouncing

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    OPERATION OF220/400 KVBREAKER DURING FOGGY SEASON

    Whenever any running unit desynchronized orbeing synchronized in foggy weather, it should

    not be delayed as 220/400 kv asynchronousvoltage appears across breaker terminals andsituation becomes worse in foggy weather ,itmay lead to flash over across pole insulators

    If there is delay line isolator should be openedor unit excitation should be made off

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    ICT OVERLOADING SCHEME

    To avoid ICTs Tripping on over current due totripping of other ICT,to avoid total black outEngg./OS developed current sensing over loadscheme

    On sensing overloading of ICT it will give tripcommand to two unit after time delay

    Scheme has been implemented at DGPS/DADRI

    COAL & AuGPS It is proposed that scheme may be implemented

    to other stations where ICTs are provided

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    FAULTS IN SWITCHYARD

    Unit trips have been reported due toswitchyard faults caused due to hanging

    metal wires/metallic threads of Kites It is proposed to carry out daily walk downsurvey to detect such incidences andcorrective action be taken

    Switchyard gantries and insulators bechecked

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    HOUSE LOAD OPERATION OF GASTURBINES V94.2

    High Frequency -51.5 HZ, Time delay-2/3 sec Low Frequency -47.5 HZ, Time delay-2sec Unit 220KV C.B opens, which initiates change of

    load mode to speed mode and sudden loadthrow off is taken care and GT continue to runat set speed with available house load

    220 KV Switch yard is connected to 400 KV

    S/yard through ICTS with 220/400kv C.B

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    In case of Grid disturbance /opening of 400/220 KVC.B of ICTS Power evacuation is Interrupted

    Gas Turbines continue to operate in load control atload set point and load rejection /House load operationdoes not take place and GT Trips on Mechanical overspeed which is very dangerous for Gas Turbines

    It is mandatory to go for inspection of combustionchambers for checking intactness of CC Tiles, whichrequires outage of Unit for 20-24 Hrs

    It reduces Machine availability/Generation loss andUnit is not available in time of crisis

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    In past Gas Turbines Tripped on actual over speed

    during Grid disturbance

    On 10.10.95 at 22.49Hrs-GT#3

    On 12.01.96 -GT#3,GT#4

    On JAN 97Running GT Tripped

    On 06.07.05 GT#2/ GT#4 Speed reached up to54.62/54.50 HZ

    GT#1/GT#3 Survived on house load but reached tohigher speed(220 KV Railway feeders helped inachieving house load operation)

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    ON 06.07.05 During Grid DisturbanceICT3/4 tripped at 01.23.43/01.23.46hrs prior to trip Frequencywas around 50.50H

    TIME GT#2 GT#4

    01.23.48 50.66 50.53

    01.23.49 53.48 52.54

    01.23.50 53.48 52.54

    01.23.52 54.62 54.71

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    ACTION PROPOSED

    House load operation settings 51.5Hz with time delayof 2/3 sec be reviewed. These setting were in Pre

    ABT Regime when freq use to very high

    In present scenario frequency does not reach up to

    51.5 HZ. It is proposed to keep time delay as 100 m sec.

    which will change control to speed mode from loadmode without any delay.

    Lower side setting at 47.5 HZ may be kept as earlier.

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    Speed signal at 53.0 HZ be initiated to tripGas Turbine to avoid actual over speeding. Corporate guide lines have also been

    issued to introduce speed sensing tripbefore mechanical over speed device trip.

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    ACTION TAKEN

    Matter was referred to Engineering byNCROS.

    After approval it was implemented at site It is proposed to review schemes of other

    gas stations to safely change over to

    house load in case of Grid disturbances

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    POWER TRANSFORMERS

    Lowering of setting of start of oil coolingfans/ Pumps to keep better cooling

    Mostly start is taken from breakercontacts, but if it is taken from tempsensing it will result in saving of AuxPower

    Replacement of Fuses with MCBs to avoidsingle phase operation of pumps/fans

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    Tripping of L.V.Transformers throughthermister sensing

    At Dadri Gas Power Station, Dry type castresign transformer are installed.

    For monitoring of excessive heating , windingtemperature High Alarm & Trip System isprovided to prevent transformer fromexcessive heating & leading to failure.

    Temperature monitoring relays are inenergized conditions, when heat is generatedResistance of Thermister increases & relaydrops and normally close, contact givesAlarm/ Trip as the case way be.

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    PROBLEM FACED

    Temperature monitoring relays onvarious transformer Panel started

    failing & Alarm of High Winding

    Temperature use to appear.

    In past at 2-3 instances, running Unit

    tripped due to mal operation of relay

    (relay failure).

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    IMMEDIATE ACTION TAKEN

    Faulty relays replaced with New

    Relays which were of imported

    origin. OEM is Siemens Germany.

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    BEST MAINTENANCE PRACTICES

    Reason for failure of relay was analyses

    in depth. It was observed that there areTwo Nos. 5 Watt resistor on P.C.B. of

    relay which is generating heat &

    damaging card. Following steps were

    taken to over come problem.

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    STEP 1

    Holes were made in relay body for

    proper heat dissipation to over come

    the problem of excessive heating.

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    STEP 2

    Resistances were taken out & fixed

    on relay body so that even heat

    generated does not effect the card &

    mal oper-ation / failure of relay can

    be avoided.

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    STEP 3

    Modification in Alarm & Trip circuit

    were made as follows-

    a. One trip relay contact was hooked up in

    parallel to Alarm Relay.

    b

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    b. One NC contact of Alarm Relay

    connected in series to trip contact Now

    trip command will be activated whenboth relays sense High Temperature.

    Failure/ mal function of individual relay

    will not give trip signal.

    c. Failure of any relay will give alarm

    signal &relay can be attended while equipment

    is

    Ci it Di f T f Wi di

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    Circuit Diagram of Transformer Winding

    Temperature Alarm/ Trip Relays

    ORIGINAL SCHEME

    Ci it Di f T f Wi di

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    Circuit Diagram of Transformer Winding

    Temperature Alarm/ Trip Relays

    MODIFIED SCHEME

    b difi i h d

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    Above modification has removedchances of tripping of unit due to mal

    operation of relay.

    Failure rate of relay has been

    brought to Zero since lasts threeyears. It is a special relay and not

    available in India. It is being

    procured for SAG.

    Cost of Relay is Rs 15000/

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    OTHER ISSUES

    Looping of neutral/DC supply at contactorterminals DOUBLE D.C supply to D.C Seal oil pumps with

    Diode coupling

    Separate A.C supply to two AC seal oil pumps D.C drive supply circuit to be housed in

    separate panel to keep system available in caseof fire in A.C Seal oil panel

    Double D.C Control supply to Switch gearswhere DC control supply is used

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    PROBLEMS FACED - REMEDIES

    In seal oil panel, control supply forA.C. Seal oil pump is 240 voltsA.C. Neutral of control circuit werelooped at contactor coil terminal.

    In case of failure of any contactorcoil, while replacing coil loopingused to get open and both A.C.Pumps used to trip.

    To over come this problem,two wires looped at contactorcoils were crimped in one lug,which eliminated problem of

    disconnection of neutral andproblem of tripping of bothA.C. Seal oil pumps wassolved.

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    SPARKING, PITTING ON SLIPRINGS OF GENERATOR

    GT GENERATOR OF 131 MW ARE AIR COOLED.ROTOR EXICITATION CURRENT IS FEDTHROUGH 8NOS CARBON BRUSHES EACH ON+VE, -VE SLIP RINGS

    In spite of proper preventive maintenancesparking started & fire parabola started on slip

    ring assembly, Unit was stopped immediately

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    DAMEGED CAUSED

    It resulted in pitting on slip ring and Brushholders, carbon brushes also damaged

    Following failure took place UNIT YEAR OUTAGE HRS GT#3 1993 10HRS GT#2 1999 08HRS Rated current is 846amp.each brush share about

    106amp. Rated current of brush is 150amp.

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    ANALYSIS OF PROBLEM

    After checking brush holders it wasobserved that for most of the brush

    holders current lead was found burnt,which can be due to excessive currentflow

    It was decided to measure D.C.Current ofeach brush for all four generators throughD.C.Tong tester on daily basis to see thecurrent loading pattern on brushes

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    OBSERVATION

    It was observed that current on somebrushes increased beyond 175 amp due toreduction of current on some brushes

    Inspire of adjustment problem continued Brush which takes high current use to fail

    at lead which use to increase current onother brushes and failure use to take placein cascade fashion

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    ACTION PLAN

    It was decided to increase nos. of brushesfrom 8 to 12 brushes by fixing 4 nos.addition brushes on slip rings due to thismodification current on brushes reducedto 50-60 amps. Failure rate reduced tozero

    no failure took place after year2000 No brush lead failure observed

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    OTHER ISSUES

    Use of DC Control supply for future project. Ithas advantage of survival of drives from trippingin case of heavy voltage dips

    Alternately we can use A.C control supply fromUPS System. Improvement in Environment for L.T/H.T

    Switchgears & Excitation panels by providing A.CSystem

    CT SWGR/OFF Site areas are mostly neglectedAreas

    Compressor MCC should be in separate room toavoid excessive noise and heat effect

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    ACHIEVEMENTS OF NCR OS AFTERSTRENGTHNING

    After Reorganization of OS-NCR more stress was givenfor Station support to improve operationalperformance,Improve quality of Overhauls and render

    ALL ASSISTANCE needed by Stations. OS-NCR took lead and Station support group/Maint

    Management& efficiency group reviewed all pasttripping and started their involvement in all

    overhaul/inspection activities ,Efficiency activities Apart From Routine activities some specific contributions

    are as follows

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    RECTIFICATION OF WRONG C.T.CONNECTION AT AuGPS

    GT#2,3,4 Tripped on Generator Diff. Protectionon faults outside its zone in the Year 2003-4,Total 07 Tripping were observed

    Site took up matter with M/S M.H.I whosuggested to Demagnetize CTs to remove effectof saturation

    MHI asked for detailed testing of CTs andreplacement of C.T which would have cost Rs23.0 lakh

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    RECTIFICATION OF WRONG C.T.CONNECTION AT AuGPS

    NCR OS decided to witness Demagnetization test ofGT#4 which was under shutdown in March 05

    During Demagnetization test it was observed that

    class1.0 CT was used for Gen. Diff protection instead ofclass PS,which was root cause for spurious trip

    C.T, connections were normalized and C.Ts tested formagnetizing current and found O.K

    C.T connections were checked in GT#2,3 and foundnormal

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    RECTIFICATION OF WRONG C.T.CONNECTION

    During Testing of C.Ts of other Units forMagnetizing current , deviation has beenobserved from original curves

    It is being studied and matter will be discussedwith Engg.

    If signs of deteoration is observed, than C.Tswill be required to be replaced

    It is proposed to refer matter to OEM M/SMELCO JAPAN

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    DYNAMIC TESTING OF GENERATOR/EXCITATION SYSTEM AT AuGPS

    Dynamic testing of Generator protection system ,ieSCC/OCC was not in practice since 1997 at Gas Stations

    As per recent OS guidelines it should be done during

    recommissioning after overhauling to eliminate false tripsafter overhauls

    At AuGPS this test was not done after initialcommissioning. Matter was taken up with M/S MHIJAPAN by site for GT#4 , M/S MHI offered for testing

    which involved financial implication of 7.8 millionYen with time schedule of 8 days

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    DYNAMIC TESTING OF GENERATOR/EXCITATION SYSTEM AT AuGPS

    NCR OS and SITE studied the excitation system anddecision was taken to carryout SCC/OCC Tests withoutOEM supervision for GT#4 in April05

    After detailed study procedure was made for interlockingand manual operation of Excitation system

    To save Time required for testing, preparations weredone in advance and Excitation system was tested in

    manual mode before rolling of machine

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    DYNAMIC TESTING OF GENERATOR/EXCITATION SYSTEM AT AuGPS

    During GT#4 commissioning SCC/OCC was donesuccessfully in April 05 in record period of 6.30 Hrs

    SCC/OCC Tests were also carried out in GT#2 afteroverhauling on 05.08.05 SCC/OCC Tests are to be done at ANGPS/ DGPS/ FGPS Sites are making procedure for conducting above tests

    Test will be carried out in coming capital overhauls atNCR stations

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    TESTING /TUNNING OF AVR&LIMITORS

    As per OS guidelines testing/tunings ofAVR/Limiters to be checked for correct operationof Excitation system

    At ANGPP it is not done since commissioning At AuGPS it was also not done since

    commissioning

    matter was discussed in March ORTatAuGPS,andit was decided to get one Unit tuned byOEM,GT#2 was checked by OEM in Aug05,

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    TESTING /TUNNING OF AVR&LIMITORS

    Next Units will be tuned/checked by Site/NCROS without OEM supervision

    DGPS has completed checking in OEMsupervision FGPS to check limiters/AVR Tuning Testing has to be included in scope of work

    during overhauling

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    CONCLUSION

    Best Maintenance Practices resulted in Eliminationof Problem.

    Identification of problems and their immediateresolution will help in improvement in system,

    thereby marching towards ZERO forced outage We must adopt transparency in Unit trip analysisand problems should be analyzed and referred toOS/ Engg for concurrence of any modification

    It will motivated all of us to think for bestpractices/aiming for ZERO forced outages

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    THANKINGYOU