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Palo Verde Nuclear Generating Station
DiscussionRelief Request
HPSI 3B5/22/08
Enclosure 2
Discussion Topics
• Overview of Reason for Request• Pump Description• Maintenance Performed 3R14• Problem Description / Repairs Performed
2
• Problem Description / Repairs Performed• Code Requirements• Current Plant Status• Proposed Pump Demonstration Testing• Basis for Relief Request
Overview of Reason for Request
• High Pressure Safety Injection Pump 3B – New Pump Seal Installed – Installation Difficulties Required Replacement– Bearing Replacement Performed
• Code Requires Full Flow Test
3
– Normally Conducted Open Vessel (Reactor Defueled)– Unit 3 Approaching Mode 4 When Discovered
• Request Deviation from Full Flow Test– Conduct Maxi Flow Test Approx 80% Full Flow– No Impact to Pump Flow Characteristics during Maintenance– Full Flow Test Conducted this Outage– Plant not in Optimal Alignment to conduct Full Flow Test
Pump Description
• High Pressure Safety Injection Pump– Centrifugal Pump
– Ingersol – Rand Model 4X11CA-8
PM being performed to Upgrade Seal
4
– PM being performed to Upgrade Seal
– Pump Performance Acceptable Prior to Refuel
– Post Maintenance Full Flow Test Acceptable Results
Maintenance Performed 3R14
• 4/25-4/30/09 – Scheduled PM
– Removal/replacement of mechanical seal
• 5/3 – Initial Fill - Outboard Mech Seal Leak
5
– Small Piece of Carbon Material Found
– Reassembled outboard seal/bearing
– ISLT and Section XI testing completed
satisfactorily
Maintenance Performed 3R14
• 5/6 – 5/19 HPSI ‘B’ Pump Sat Idle
• 5/19 – Started HPSI ‘B’ for SIT fills.
– Observed Leakage from outboard seal
– Initially ~ ½ gpm
6
Initially ½ gpm
– Reduced to ~ 1 drop/sec at End of 4 hrs
7
8
Repairs Performed
• Entered Level “B” Troubleshooting Plan
– OEM Vendor Support
– Determined Cause of Seal Leakage –Improper Alignment of Seal Faces
9
Improper Alignment of Seal Faces
– Outboard Seal Damaged Due to Misalignment
– Thrust Bearing (damaged during removal)
• Performed repairs to HPSI ‘B’ outboard seal w/ replacement of thrust bearing
Code Requirements
• ASME OM Code 2001 Edition through 2003 Addenda
• ISTB-3310 Effect of Pump Replacement, Repair, and Maintenance on Reference ValuesIf R f V l S t f V l M h
10
• If Reference Value or Set of Values May have been effected by repair or replacement– Bearing Replacement May Affect
• New Reference Values shall be determined– By a Comprehensive or Group A Test Run– Prior to declaring pump operable
Current Plant ConditionsAt Time of Determining Retest
• Reactor Reassembly Complete
• Primary Plant Solid
• Drawing a Bubble in the Pressurizer
11
• RCP Sweeps in Progress
• Normal Full Flow Test Conducted with– Fuel Off Loaded
– Reactor Vessel Open
Proposed Pump Demonstration Testing
• 2 Hour Run– Verify Correct Seal Operation– Change Bearing Oil– Collect vibration data
Additi l 2 h R (1 dditi l
12
• Additional 2 hour Run (1 additional as a minimum)– Vibration measured and analyzed at each point
• Utilize “Max Recirc” Flow Alignment– At least 750 gpm versus 1040 gpm design– Acceptable in Mode 5
Basis for Relief Request
• New Bearing is Only Cause for Comprehensive Flow Test
• No Change to Pump Characteristics
• Successful Comprehensive Flow Test
13
Successful Comprehensive Flow Test Performed this Refuel Outage
• Vibration Data at Min Flow Generally worse than Full Flow
• Testing Under Current Plant Conditions Not Typical Configuration for Full Flow Testing