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Joe Pecht, Stefan Enjem, Jason Zion, Luis Garcia, Young Lee, Joe Van Hofwegen, Walter Freitag Initial Assembly Operation (Station 90) By moving the parts bins from the left side of the assembly cell to the areas in the proposed concept, the cycle time are reduced and the ergonomics of the station are improved. WORK FLOW IMPROVEMENTS DOWNTIME PROCESS TIME 0 10 20 30 40 50 60 90 100 110A 110B 120A 120B 130 140A 140B 150A 150B 160 170A 170B 180 190 200A 200B 205 210 230A 230B EOL Station Process Time (seconds) Direction of Assembly Manual Automated Project Mission Statement The purpose of this project is to increase the quantity of hydraulic motors produced per person per hour (QPH) at Valeo's production facility by 4% - 6%. This is done as specified by the customer, without sacrificing quality or safety. When the improvements are fully implemented, the team estimates a 9.5% improvement in motor output. All improvements are justified based on Valeo's 2-year payback standard. The areas of improvement are made in downtime, process time, procedures and improved workflow. Process Time Analysis The analysis of process times revealed that stations 90 was a major bottleneck - taking an average of 35.53 seconds per cycle. Station 90 is also the origin of the system. Station vs. Downtime The collection and analysis of downtime data indicate that the end of line tester and station 210 make up the major problematic stations. Design Concept for EOLT Changes An improved pneumatic coupling system was designed for the EOLT to reduce downtime due to misalignment and improve productivity. Pallet Flow Control & Failure Response The logic diagram (left) visualizes the program installed on the line. The program allows for better flow of pallets through the system and also designates operators to respond to module failures. Identifying Optimal Configuration Improvements in workflow were investigated using simulation techniques to identify alternative configurations for manpower, number of pallets, line speed, and queuing methods. Different alternatives were tested based on system performance to determine the best configurations for the line. PRODUCTIVITY IMPROVEMENT OF THE HYDRAULIC MOTOR ASSEMBLYLINE AT VALEO HDFS Hydraulically driven Fan System (above) - Used in high end vehicles like the Jeep Grand Cherokee, Dodge Viper, and Dodge Ram SRT-10 (below) for their increased trailer, towing capacity, reduced grill openings, improved fuel economy and reduced alternator loading. The power is derived from existing steering pump pressure. COST/BENEFIT ANALYSIS CONCLUSIONS By studying the system and analyzing various types of data, improvements were made in the areas of downtime, process time, procedures and workflow. Through the use of simulation, we are able to show an increase in productivity of the system by 9.5%. Optical Inspection (Station 210) To eliminate false rejects due to glare that interfered with optical validation, a solution was developed that involves repositioning the light source to the side and using a mirror that lets light through to the part but not back to the camera. FEA A Finite Element Analysis was used to determine the strength characteristics of the back off pins that are used in the EOLT design. Cost & Benefits An analysis of the upfront cost for the implementations and the benefits associated with overtime savings are shown below. Any costs associated with changes made to the system are justified through savings in overtime and will be paid back within 2 years. Note that this does not account for the profit from the increase in motor production. NPV Analysis The net present value for this productivity improvement project at Valeo is: Before After Station vs. Downtime 0 100 200 300 400 500 600 700 800 900 1000 EOLT Station 210 Station 140 Station 230 Station 200 Station 170 Station Downtime Before After ACKNOWLEDGMENTS Team Valeo would like to thank Mentor, Dr. Michael Kuhl; Coordinator, Dr. Paul Stiebitz; The entire Valeo Staff including Richard Guerin, Paul Vandeursen, James Ely, and the Valeo machine shop. R O C H E S T E R I N S T I T U T E O F T E C H N O L O G Y 1 8 2 9 RIT

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Page 1: PRODUCTIVITY IMPROVEMENT OF THE HYDRAULIC MOTOR ...edge.rit.edu/edge/OldEDGE/public/Archives/P04016/files/Valeo Poste… · Joe Pecht, Stefan Enjem, Jason Zion, Luis Garcia, Young

Joe Pecht, Stefan Enjem, Jason Zion, Luis Garcia, Young Lee, Joe Van Hofwegen, Walter Freitag

Initial Assembly Operation (Station 90)By moving the parts bins from the left side of the assembly cellto the areas in the proposed concept, the cycle time are reduced and the ergonomics of the station are improved.

WORK FLOW IMPROVEMENTS

DOWNTIME

PROCESS TIME

0

10

20

30

40

50

60

90 100

110A

110B

120A

120B 13

0

140A

140B

150A

150B 16

0

170A

170B 18

0

190

200A

200B 20

5

210

230A

230B

EOL

Station

Proc

ess

Tim

e (s

econ

ds)

Direction of Assembly

Manual

Automated

Project Mission StatementThe purpose of this project is to increase the quantity of hydraulic motors produced per person per hour(QPH) at Valeo's production facility by 4% - 6%. This is done as specified by the customer, without sacrificingquality or safety. When the improvements are fully implemented, the team estimates a 9.5% improvement in motor output. All improvements are justified based on Valeo's 2-year payback standard. The areas of improvement are made in downtime, process time, procedures and improved workflow.

Process Time AnalysisThe analysis of process times revealed that stations 90 was a major bottleneck - taking an average of 35.53 seconds per cycle. Station 90 is also the origin of the system.

Station vs. DowntimeThe collection and analysis of downtime data indicatethat the end of line tester and station 210 make up the major problematic stations.

Design Concept for EOLT ChangesAn improved pneumatic coupling system was designedfor the EOLT to reduce downtime due to misalignmentand improve productivity.

Pallet Flow Control & Failure ResponseThe logic diagram (left) visualizes the program installed on the line. The program allows for better flow of pallets through the system and also designates operators to respond to module failures.

Identifying Optimal ConfigurationImprovements in workflow were investigated using simulation techniques to identify alternative configurationsfor manpower, number of pallets, line speed, and queuing methods. Different alternatives were tested based on system performance to determine the best configurations for the line.

PRODUCTIVITY IMPROVEMENT OF THE HYDRAULICMOTOR ASSEMBLYLINE AT VALEO

HDFSHydraulically driven Fan System (above) - Used in highend vehicles like the Jeep Grand Cherokee, Dodge Viper, and Dodge Ram SRT-10 (below) for their increased trailer, towing capacity, reduced grill openings, improved fuel economy and reduced alternator loading. The power is derived from existing steering pump pressure.

COST/BENEFIT ANALYSIS

CONCLUSIONSBy studying the system and analyzing various types of data, improvements were made in the areas of downtime, process time, procedures and workflow. Through the use of simulation, we are able to show an increase in productivity of the systemby 9.5%.

Optical Inspection (Station 210)To eliminate false rejects due to glare that interfered withoptical validation, a solution was developed that involves repositioning the light source to the side and using a mirror that lets light through to the part but not back to the camera.

FEAA Finite Element Analysis was used to determine the strength characteristics of the back off pinsthat are used in the EOLT design.

Cost & BenefitsAn analysis of the upfront cost for the implementations and the benefits associated with overtime savings are shown below. Any costs associated with changes made to the system are justified through savings in overtime and will be paid back within 2 years. Note that this does not account for the profit from the increase in motor production.

NPV AnalysisThe net present value for this productivity improvement project at Valeo is:

Before After

Station vs. Downtime

0

100

200

300

400

500

600

700

800

900

1000

EOLT Station 210 Station 140 Station 230 Station 200 Station 170

Station

Dow

ntim

e

Before After

ACKNOWLEDGMENTSTeam Valeo would like to thank Mentor, Dr. Michael Kuhl; Coordinator, Dr. Paul Stiebitz; The entire Valeo Staff includingRichard Guerin, Paul Vandeursen, James Ely, and the Valeo machine shop.

ROC

HE

STER

INSTITUTE OF TEC

HN

OL

OG

Y

1 82 9 •

R I T• •