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Strand Casting II TUESDAY MORNING, APRIL 15, 1975 The Strand Casting II session convened at 9:00 am. The chair- men were G. S. Lucenti, Algoma Steel Corporati.on, Sault Ste. Marie, Ontario, Canada, and N. L. Samways, Jones 81 Laughlin Steel Corporation, Aliquippa, Pennsylvania.

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Strand Casting II

TUESDAY MORNING, APRIL 15, 1975

The Strand Casting II session convened at 9:00 am. The chair- men were G. S. Lucenti, Algoma Steel Corporati.on, Sault Ste. Marie, Ontario, Canada, and N. L. Samways, Jones 81 Laughlin Steel Corporation, Aliquippa, Pennsylvania.

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CONTINUANCE CASTER MAINTENANCE

TtIE KEY TO QUALITY AND TONS PER HOUR

H. N. Hubbard, Jr., Division Superintendent -

S t e e l Producing, Gary Works

G. W. Hodges, Ass i s t an t Superintendent - Continuous Caster , Gary Works

United S t a t e s S t e e l Corporation

The Continuous Slab Caster a t Gary began opera t ion i n Apr i l , 1967, and on Ju ly 29, 1974, the f i v e m i l l i o n ton milestone was passed. The experience gained i n operat ing t h i s machine has i d e n t i f i e d numerous problems and t h e so lu t ions ap- p l i ed have provided a broad base of t echn ica l knowledge and operat ing p r a c t i c e which w i l l be of g r e a t value in t h e design and opera t ion of f u t u r e United S t a t e s S t e e l Casters . It is our purpose here t o r e l a t e the experiences i n maintaining the f a c i l i t y , which w i l l demonstrate t h e enormous importance t h a t t h e rnaintenance function has i n a c a s t e r operat ion and the s i g n i f i c a n t improvements i n produc- t i v i t y which l a y i n t h i s a rea .

. The machine was designed and b u i l t t o provide long s l a b s of various gauges and widths f o r the new 84" Hot S t r i p M i l l , which a l s o began operat ion i n 1967. Design and operat ing parameters were es tabl i shed through operat ion of a l a r g e s c a l e p i l o t p lan t a t t h e South Works of U. S. S t e e l , and included innovations i n higher cas t ing r a t e s , unlimited sequence cas t ing c a p a b i l i t y , and in- l ine s l a b s i z ing .

One of t h e t h r e e 210-ton v e s s e l s a t Gary Works' No. 1 BOP Shop is reserved t o feed steel sequen t i a l ly t o the c a s t e r v i a one of two h o i s t bays located a t the nor th end of t h e two BOP teeming a i s l e s (Exhibit 1 ) . Two posi t ioning c a r s above t h e cas t ing line move the l a d l e s over the tundish during cas t ing . The c a s t e r has 25-ton tundishes equipped with s l i d i n g ga te systems. Drives on each of two tundish c a r s g ive t h e c a p a b i l i t y of changing tundishes during cas t ing . The production is s l a b s of t e n and under carbon steel known t o the t r ade a s USS Riband, which can be 100-percent open poured.

The machine (Exhibit 2) is a s t r a i g h t mold-type c a s t e r with a bend f o r hori- zonta l withdrawal, designed t o c a s t s l a b s 9.3-inches th ick by 55 t o 76 inches wide a t speeds up t o 76-inches per minute. There i s a 45-foot v e r t i c a l rack and curve with a 40-foot r ad ius . The t o t a l confinement is 123-feet. An in- l ine reheat furnace and seven s tand r o l l i n g m i l l reduce t h e s l ab c ross sec t ion t o a s small a s 5.25-inches th ick and 30-inches wide. The r o l l e d s l abs a r e torch c u t t o length and water cooled during t r a n s f e r t o t h e adjacent shipping f a c i l i t i e s .

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History of Start-Ue

O P a a t b n a t Gary began i n April of 1967, using the 55-inch wide mold. The f i r s t heat was successfully cas t . However, succeeding hea t s brought t o l i g h t a problem comaon t o a l l continuous-contlnuous ca s t e r s , t ha t of pos i t ive l a d l e open- ing and ladle-stream control . It was desi rable t o use the same l a d l e f o r teeming ingots a s was used fo r the ca s t e r , therefore , exot ic r e f r ac to r i e s and air-cooled rods were avoided. The teeming l a d l e rigging had t o be redesigned f o r more s ta- b i l i t y and an eight-inch stopper head and sleeves used. The w e l l was t o be six- inches deep with a 45' s i de slope, and a template was developed t o insure proper configuration. A complete maintenance check l is t was made, covering a l l points of l a d l e make-up t o cross check workmanship. Final ly , a shoe hook was hung from a service crane in t h e cas t ing tower t ha t could be swung over the r igging gooseneck adjacent t o the plunger, which could p u l l the stopper open a s a l a s t r e so r t . This proved t o be invaluable i n years t o come and several runs of between 1800 and 2000 hea t s without a f a i l u r e t o open have been made.

I n a matter of weeks, the c a s t e r ' s t a r t e d t o .put together the f i r s t continuous heat run and a s e l e c t r i c a l problems were corrected and the bugs worked out of the tundish s l i d ing ga te system, continwua runs were lengthened r a i s i ng the average heats per s t rand s t a r t t o three a f t e r four months of operation (Exhibit 3) . It became evident t ha t getking t h e c a e t e r s t a r t ed .was the most c r i t i c a l p a r t of the operation and was the most l i k e l y period f o r damage t o the mechanical e q u i p e n t i n the l i n e . The most ser ious problem found i n t h i s e a r l y period of operation w a s the containment-roll c l u s t e r design, which included back-up r o l l s throughout the l i n e (Exhibit 4).

During the f i r s t two years of operation, attempts were made t o u t i l i z e the 76- inch mold, but the bearing and r o l l f a i l u r e s , experienced with the 55-inch s lab , dccurred in cas t ing the 76-inch s l a b with increased frequency. Maintaining pro- duction thus d ic ta ted r e i n s t a l l a t i o n of the more dependable 55-inch mold. It was evident t ha t the wider s l ab and high cas t ing r a t e s found the weak points of the niachine very quickly.

In 1969, the e n t i r e curved rack and switch sec t ion was redesigned t o el iminate back-up r o l l s , permitting replacement with l a rger diameter r o l l s , spaced t o mini- mize rol l - to-rol l bulging of the s lab . Immediately, the average tonnage per month jumped from 30,000 t o 65,000 tons (Exhibit 5) and the average hea t s per strand s t a r t went from three t o seven.

Maintenance Hours Analysis

It became apparent that the containment and withdrawal r o l l requirements of the cas te r , with the 85-foot f e r r o s t a t i c head, ca l l ed f o r a number of changes i n de- s ign and maintenance t o achieve improvements ln r e l i a b i l i t y and productivi ty. Therefore, an analys is was made of the equipment which caused the majori ty of the maintenance hours during a repa i r turn (Exhibit 6). It should be noted t h a t these a r e not man hours, but maintenance hours, without adjustment f o r t o t a l p lan t schedule f luc tua t ions , and were developed on the bas i s of an average number of operating turns per week of 12.2 i n 1970 which l e f t 8.8 turns , o r 70.4 hours per week f o r maintenance. For comparative purposes, t h i s was converted t o r epa i r turn hours per heat cas t . The analys is indicated t ha t three areas , the f ixed curve, the v e r t i c a l rack and the torch carr iage accounted fo r the major por t ions of the maintenance work t o ' b e performed during the down turn.

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Even a f t e r redesigning, the f ixed curve rack required .97 hours of mainten- ance per heat c a s t which w a s t he f u l l down turn every week. The problem continued t o be both bearings and r o l l s . A program of upgrading of bearing design and changes in both r o l l ma te r i a l and r o l l su r face preparat ion were expedited, and gradual improvement was achieved. In add i t ion , r o l l gapping tolerances were tightened t o p lus o r minus .020 inches. I t was found t h a t r o l l s out of gap be- cause of bad bearings o r l o s t shims caused premature f a i l u r e s i n both up and down stream adjacent c l u s t e r s . Currently, every time t h e c a s t e r terminates both main- tenance and operat ing management inrmediately inspect t h e l i n e . Problem a reas a r e a l s o i d e n t i f i e d before termination by comparing i n t e r n a l q u a l i t y versus l i n e speed. For example, t o t a l s o l i d i f i c a t i o n i n t h e s l a b is ca lcula ted t o be 20 minutes be- low the mold, therefore , a t a cas t ing speed of 50-inches per minute, l i q u i d core would extend 83-feet below the mold. Problem c l u s t e r s above 83-feet could cause ghost l i n e s . The proximity of such ghost l i n e s t o t h e s l a b surface determines where, i n the l i n e , t h e problem l i e s . Problems imnediately below 83-feet could cause mid-thickness cracks and aggravate center l i n e segregation. A s speed v a r i e s , these condit ions appear and disappear with the end of l i q u i d core moving i n and ou t of the bad c l u s t e r . In t h e absence of s p e c i f i c problems i n t h e l i n e , main- tenance regaps sec t ions on a preventive r o t a t i o n bas i s . The n e t r e s u l t of these programs has been a reduction of maintenance hours per heat c a s t from .97 i n 1970 t o .25 f o r t h e f i r s t six months of 1974.

The v e r t i c a l rack is a l s o a prime example of both redesigning and preventive maintenance. This a r e a a l s o required t h e f u l l down tu rn time f o r maintenance i n 1970. The backup r o l l s were removed from t h e c l u s t e r s i n 1972 and t h e same gap- ping program was i n s t i t u t e d a s i n the curved rack. This reduced t h e maintenance hours per heat c a s t from .97 i n 1970 t o .21 i n 1974. It is extremely important t h a t gap i n t h i s a rea be maintained t o p lus o r minus .020 inches.

The torch ca r r i age showed the most s i g n i f i c a n t improvement wi th a maintenance hours per heat c a s t reduction of from .97 t o -01. The problem was primari ly i n design o f - t h e d r ives and the re-designed equipment r equ i res only preventive maintenance.

The switch s e c t i o n required .68-hours per heat c a s t and s imi la r programs i n r o l l ma te r i a l , bearings and gapping reduced t h i s t o .18 hours per heat c a s t .

The furnace problem was.mainly burner coolers , furnace r o l l s and s c a l e re- mdval. Correction of these items reduced the maintenance hours per heat from .59 i n 1970 t o .13 i n 1974.

The pinch r o l l s were not redesigned. However, replacement of ex i s t ing r o l l s with USS Homestead-X steel work r o l l s , b e t t e r backup bear ings and an improved l u b r i c a t i o n system, reduced maintenance requirements from .45 t o .06 hours per heat c a s t . I n add i t ion , t h e pinch r o l l s a r e on a scheduled maintenance program where they a r e i n t e r n a l l y adjusted every 300,000 tons and replaced every 1,000,000 tons. This has el iminated .premature f a i l u r e s completely.

The t r a n s f e r bed requ i res a regular skid and dog replacement program which reduces major unscheduled breakdowns and t h e h o i s t s and t r a n s f e r c a r s a l s o re- ce ive preventive maintenance s u c h a s cleaning contac ts , l i m i t switches, lub r i - ca t ion , etc. The main improvement i n these a r e a s is t h a t r e p a i r work is done on a scheduled b a s i s and does n o t i n t e r f e r e with t h e operat ion of t h e c a s t e r .

The bend s e c t i o n improvment involved b e t t e r bearings and l u b r i c a t i o n systems. A preventive maintenance program of cleaning and p r e c i s e alignment has extended t h e average l i f e of t h i a component t o 800,000 tons between changes. The .03 maintenance

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hours per heat c a s t genera l ly involves the changing of t h e bottom outs ide r o l l which i s sub jec t t o heavy loads from cold head ends and cap o f f s .

Rolling M i l l r e p a i r hours exclude r o l l changes which have no t been a l imi t ing f a c t o r due t o exce l l en t r o l l l i f e , and the r e p a i r hours a r e general ly associated with e l e c t r i c a l problems. This i s a very c r i t i c a l piece of equipment because a m i l l stoppage can r e s u l t i n cobbles i n the m i l l - o r furnace and the p o s s i b i l i t y of a s tuck s l a b i n the l i n e . A preventive maintenance team, including supp l ie r se rv ice personnel, was es tabl ished to provide an e lec t r i ca l -e lec t ron ic i n t e r f a c e maintenance program. This team, which is a combination of an experienced elec- t r i c a l craftsman, an e l e c t r o n i c s p e c i a l i s t and an e l e c t r i c a l engineer t r a inee , has become invaluable during dovn turns f o r preventive maintenance and trouble shooting e l e c t r i c a l problems.

The mold o s c i l l a t o r l i f e is 800,000 tons , a f t e r which cams and cam followers must be replaced o r surface q u a l i t y w i l l be adversely af fec ted . Ef fec t ive main- tenance of the o s c i l l a t o r , including cam lubr ica t ion and c lean l iness , i s of the utmost importance t o high productivi ty and defect f r e e s l abs .

The frequency of breakouts has shown a reverse t r end , jumping from .04 t o

I .09 hours per heat cas t . This represents an increase i n breakout frequency from 0.52% i n 1970 t o 1.22% i n the f i r s t ha l f of 1974. This increase is pr imar i ly a t t r i b u t e d t o raw mate r i a l and associated BOP problems, and the trend has been reversed through improvements i n these areas . The 1974 year ly t o t a l was 0.72% of hea t s c a s t .

Using these analyses and a systematic approach t o problem solving, redesign and preventive maintenance, the average a c t u a l operating turns per week has in- creased from 12.2 i n 1970 t o 15.1 during the f i r s t s i x months of 1974. Scheduled tu rns were approximately t h e same i n both periods.

Continuous-Continuous Operation

I n conjunction wi th more ava i l ab le operat ing hours, it was necessary t o in- crease t h e production r a t e . This could be done i n two ways, increasing t h e speed o r increasing the average length of the continuous-continuous runs. Several a t - tempts were made t o increase the average speed but t h e f l e x i b i l i t y t o compensate f o r furnace timing, temperature va r ia t ions , and off-analysis hea t s was s u f f i c i e n t l y reduced t h a t an increase i n breakout frequency resu l t ed . Higher cas t ing speeds a l s o increased i n t e r n a l problems, when the line was not i n good condit ion.

The advantage of continuous-cdntinuous cas t ing i s demonstrated by i t s e f f e c t on c a s t e r productivi ty. The maximum increase i n annual tonnage of a continuous cas- ter occurs between a s i n g l e heat c a s t and ten hea t s c a s t per s t rand s t a r t (Exhibit 7). For example, the p l o t of average number of hea t s per s t rand s t a r t versus an- nual production f o r a s i n g l e s t rand s l a b c a s t e r wi th a 210-ton hea t s i z e , a f i f t y minute heat time and an average t u r n around time between c a s t s of one hour and f o r t y minutes denoted by curve "A" can increase i ts annual capaci ty by over 600,000 tons by cas t ing t e n heat s t r i n g s . From ten heats t o twenty heat s t r i n g s the pick up t o tonnage i s 150,000 tons. Curve "B" represents the same c a s t e r with t h e heat time reduced t o f o r t y minutes. I n this case , an annual increase in tonnage of over 1,000,000 tons is rea l i zed between one and t e n sequent ia l hea t s per s t r and-s ta r t . Both curves "A" and "B" represent f i f t y weeks per year and nineteen turns per week operation. Any new c a s t e r should be designed t o continuous-continuous c a s t a mini- mum of ten hea t s cycles , i f steel production is ava i l ab le and the t o t a l p lan t balance permits .

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I n 1969 and 1970, e v e r y c a s t i n g c y c l e was s t a r t e d w i t h a t u n d i s h c a p a b l e o f c a s t i n g f o u r t e e n h e a t s . The average h e a t s p e r s t r a n d s t a r t was a c t u a l l y 7.9. I n o r d e r t o a t t a i n t h e t e n h e a t s p e r s t r a n d start , i t was n e c e s s a r y t o develop equipment t o s c h e d u l e a t l e a s t twenty h e a t s p e r s t r a n d start . T h i s was ach ieved d u r i n g 1971 and 1972.

T h i s approach l e d t o t h e n e x t s t u d y , which was t o a n a l y z e t h e r e a s o n s f o r i n t e r r u p t i o n s of c a s t i n g r u n s shown i n E x h i b i t 8. The r e a s o n s f o r t e r m i n a t i o n o f a c o n t i n u o u s . r u n were a s s i g n e d r e s p o n s i b i l i t y between BOP f u r n a c e and l a d l e , and f o r c a s t e r equipment, q u a l i t y and b r e a k o u t s f o r t h e c a s t e r . For example, 2.6 h e a t s o u t of e v e r y 100 h e a t s c a s t i n 1971 r e s u l t e d i n t e r m i n a t i o n s o f c o n s e c u t i v e r u n s because of BOP f u r n a c e r e s p o n s i b i l i t y . These f u r n a c e pro- blems r e s u l t e d from a number of r e a s o n s , such a s too h o t , l a t e , s c r a p c h a r g e r down, e t c . The l a d l e was r e s p o n s i b l e f o r 1.2% which b r i n g s t h e t o t a l BOP res- p o n s i b i l i t y t o 3.82 i n 1971 and t h e t r e n d shows improvement each y e a r t o 2.8% i n 1974. Terminat ion r e s p o n s i b i l i t y f o r t h e c a s t e r , i f s i m i l a r l y broken down between equipment, q u a l i t y and b r e a k o u t s , shows a n over a l l r e d u c t i o n . However, s i n c e t h i s paper i s devoted t o maintenance o f t h e c a s t e r , we w i l l examine o n l y t h a t pe rcen tage which i n v o l v e s c a s t e r equipment ( E x h i b i t 9 ) .

The breakdown of c a s t i n g equipment shows t h e s l i d e g a t e svstem t o be r e s - p o n s i b l e f o r 1.1 t e r m i n a t i o n s f o r every 100 h e a t s c a s t . T h i s 1.1 r e p r e s e n t s 36 t e r m i n a t e d r u n s i n 1971. A s t h e con t inuous runs became l o n g e r , t h e i n c r e a s e i n exposure t ime of t h e s l i d e g a t e sys tem t o t h e r a d i a t i o n o f the. l i q u i d s t e e l i n tile mold caused numerous problems. A program w a s developed i n c o n j u n c t i o n w i t h t h e s u p p l i e r t o improve t h e r e l i a b i l i t y of t h e system w i t h h e a v i e r s l i d e s and s p r i n g s , however, t h e major c a u s e o f f a i l u r e s could b e t r a c e d ' b a c k t o maintenance workmanship. A s p e c i a l check l ist was developed t h a t . h a d t o be s i g n e d by t h e m i l l w r i g h t making t h e checks d u r i n g assembly. A l l f a c t o r s of a g a t e f a i l u r e were i n v e s t i g a t e d l i k e a s e r i o u s a c c i d e n t and a formal r e p o r t p repared . The n e t r e s u l t was. a d e c r e a s e ' i n t e r m i n a t i o n s t o .55: i n 1974, r e p r e s e n t i n g o n l y 1 3 t e r m i n a t i o n s f o r t h e six-month p e r i o d .

The second most f r e q u e n t r e a s o n f o r premature t e r m i n a t i o n s which accounted f o r .3% of h e a t s c a s t , o r e l e v e n o c c u r r e n c e s i n 1971, was t u n d i s h problems. Th is was p r i m a r i l y a s s o c i a t e d w i t h premature l i n i n g f a i l u r e . F a i l u r e s oc- c u r r e d i n t h e pour pad a r e a due t o t h e c o n s t a n t impingement of t h e s t e e l s t r eam on t h e pour b lock which l i t e r a l l y d r i l l e d a h o l e i n t h e pour pad. The pad i s now c o n s t r u c t e d o f a n 18"xl8"x9" deep b lock of Alumina-Chromia pre- f i r e d b r i c k . T h i s material w i t h s t a n d s s t ream e r o s i o n much b e t t e r than t h e 90% alumina b lock used p r e v i o u s l y , however, we do n o t r e c o m e n t t h i s m a t e r i a l f o r b a t c h c a s t e r s because of s p a l l i n g c h a r a c t i s t i c s dur ing c o o l i n g and h e a t i n g The i n c r e a s e d i n c i d e n c e of t u n d i s h i n 1972 and 1973 cor responds t o a t t e m p t s t o i n c r e a s e t u n d i s h l i f e t o 30 h e a t s . T h i s problem r e s o l v e d i t s e l f i n t h e l a t t e r p a r t of 1972 when t h e f i r s t t u n d i s h was changed dur ing c a s t i n g , e l i m i n a t i n g t u n d i s h l i f e as a l i m i t i n g f a c t o r .

The t h i r d most f r e q u e n t c a u s e of t e r m i n a t i o n s was t h e t o r c h c a r r i a g e . Th is p i e c e of equipment a l s o showed poor performance i n t h e maintenance s t u d y . Redesign of t h i s equipment reduced t h e f requency o f .2% of h e a t s c a s t t o none.

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The Rolling M i l l accounted fo r eight terminations in 1911 which was .2X of heats cas t . These were largely e l e c t r i c a l problems and were corrected by a pre- vemtive maintenance program on e l e c t r i c a l contactors and control adjustment every week. Hydraulics were very l i t t le problem a f t e r the i n i t i a l leaks were corrected. This program eliminated mill-caused terminations fo r the l a s t two years.

Pinch r o l l t ewlna t ions were mostly associated with broken r o l l s and bad bearings. With the improvements previously discussed and scheduled replacement, premature f a i l u r e s ceased t o be a problem.

The t ransfe r bed caused terminations when s labs could not be cooled and had t o be run.out hot where handling became a serious problem. Strengthening of the s t ruc ture a t both '&try and exit ends, p lus addi t ional e l e c t r i c a l s a f e guards have resulted. in t h e indicated improvement.

In 1972 furnace and ho is t problems c r ea t ed \ the i r share of terminations, a l l of which were corrected with increased emphasis on preventive maintenance.

Miscellaneous terminations consis t of disconnect f a i l u r e s , t o t a l power f a i l u r e s , water problems, bleeders, man re la ted problems, e t c . The program de- 1 creased the t o t a l percent of terminations per heat ca s t from 2.6 t o 1.2 from

1 1971 to 1974. The log of reasons fo r terminations is kept up current ly on a I dai ly bas i s and is used t o pinpoint problem areas a s they develop, and t o sche-

dule maintenance work on down turns.

During 1972, the subject of BOP furnace cornpatability with the continuous cas te r became a grea t concern. The 55-inch mold, then in use, slowed down the output of the BOP because of the 564ninute pour-time required t o feed the caeter .

I The 76-inch mold was even worse because the pour-time of 38-minutes necess i ta ted the use of two furnaces to feed the cas te r . Development of an intermediate mold s i z e was c lear ly indicated and the present standard 9 .3~64 inch mold was the re- s u l t . Early f ea r s of the i n a b i l i t y to r o l l the very narrow production from the 64-inch a s ca s t s lab were not realized and the casting r a t e fo r the 64-inch mold was a perfect match fo r one BOP furnace output a t Gary.

Two t r i a l production periods were scheduled and the experience gained was used in mold development and redesigning of r o l l s and bearing arrangements. The r o l l s i n the area of t he greates t f a i l u r e frequencies w e r e shortened by one foo t , decreasing both r o l l def lect ion and the range of s e l f alignment needed i n the bearing s e t s . The replacement of the longer r o l l s is progressing on an a s nece- ssary bas i s and maintenahce requirement decreases a r e continuing.

The average number of heats per strand s t a r t s tead i ly improved through 1972. The r e a l break through f o r Gary's Caster occurred on October 18, 1972, when the f i r s t tundish change was made without in terrupt ion of the casting s t r i ng . The technique requires precise coordination and control because the ro l l ing m i l l must adjust fo r each change i n casting r a t e , and the m i l l control cannot be maintained i f the casting l i n e stops. Therefore, the speed i s gradually reduced to five- inches per minute by a s e r i e s of tundish s l i d e ga te changes u n t i l the f i n a l shut off is made with a f u l l mold. The f i ve inches per minute is maintained i n both cas te r and m i l l f o r approximately t h i r t y seconds u n t i l the tundishes a r e switched and casting continues. The elapsed time of the interrupt ion of s t e e l flow in to the mold is usually l e s s than f i f t e e n seconds.

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With t h i s new procedure the only l imi t ing f a c t o r t o cas t ing i n d e f i n i t l y is mold l i f e . f n December, 1972, United S t a t e s S t e e l , Gary Works nearly doubled the previous world's record f o r a s i n g l e s t rand s l a b c a s t e r by continuously cas t ing 22,391 n e t tons of steel in one s t r i n g , The s t r i n g consisted of 107 heats , c a s t over 82 hours and 15 minutes and was f i n a l l y terminated by a cold heat . On June 23, 1973, the 124 hea t s were c a s t f o r 26,276 tons i n 99-hours and two minutes and on December 19, 1973, the c a s t e r shat tered i ts previous record by continuous- continuous cas t ing 132 hea t s , o r 27,983 n e t tons during an 108-hour and twenty- f i v e minute period (Exhibit 10). The c a s t e r output approximated 5.2 m i l e s of c a s t s l a b which, a f t e r in- l ine r o l l i n g , produced 48,300 f e e t , o r 9 . 1 m i l e s of s ized s l abs . Thirty-eight d i f f e r e n t sec t ion changes were made producing 1,208 s l a b s 4O-feet long. Seventy-nine s l i d e g a t e nozzle changes were made and t h e through put during the run was 258.3 tons pe r b u r o

Many b e n e f i t s were derived from the tundish changing capabi l i ty . The number of h e a t s per s t rand s t a r t jumped from an average of eleven t o an average of 16. The average monthly production jumped up over 90,000 tons. The fewer terminations and s t a r t ups resu l t ed in a s i g n i f i c a n t reduction of in r o l l and bearing damage. The philosphy t h a t cold head ends in start ups and t a i l ends i n terminations do most of t h e damage t o cas t ing l i n e s is t rue . The expected l i f e of the various segments of the l i n e improved. For asample, t h e bend sect ion, which had an average l i f e of 500,000 tons of steel c a s t , has, i n t h e l a s t two replacements, l a s t e d over 800,000 tons. The colicept of s t a r t i n g the c a s t e r up Monday morning and running continuously u n t i l Friday e i g h t was now a p o s s i b i l i t y .

Caster U t i l i z a t i o n

'6he object ive of t h e maintenance improvement progrrnns and extended cas t ing s t r i n g s a r e increased product iv i ty and caetao u t i l i z a t i o n , The latter r e f e r s t o a very important s t a t i s t i c which i r s t h e percent of time t h a t l i q u i d steel i s ac tua l ly i n the mold. Exhibit 11 shows the r e l a t i v e posi t ions of severa l Ameri- can Slab Casters f o r 1973 based on AfSf repor ts . The emphasis on continuous- continuous operat ion pays o f f handsomely f%a u t i l i z a t i o n of a s i n g l e s t rand machine and the p o t e n t i a l of t h e same continuous-conthuoum operat ion of independent multi-strand machinee is unl imited,

The in ten t ion of cas t ing unt i l something breaks a l s o presents a d i f f e r e n t challenge t o t h e maintenance man becaure every c a s t e r or iented termination w i l l e i t h e r d i r e c t l y o r i n d i r e c t l y be h i s r e spons ib i l i ty . H e must approach each re- p a i r o r replacement with the a t t i t u d e that he cannot re-repair o r make adjust- f

mente f o r 20,000 t o 30,000 tone. The eechedding of all major jobs i n t o a l imi ted down period and coordination of the jobs on mul t ip le e levat ions is no s m a l l task. For t h i s reason, the preoent emphasis is upon improving maintenance h o i s t s , ex- t r a c t i o n of r o l l c l u s t e r s , ease of gapping, etc. The number of turns required t o make rou t ine replacements, r a t h e r than t o patch u p . f a i l u r e s , has become t h e l i m i t - ing fac to r .

The major problem confronting the Gary- Caster today is the del ivery of steel a t t h e proper time, temperature and analysfe t o the cas t ing machine. Problems with substandard raw materials, both i n the BOP and Blas t Furnace, have eeriouely a f fec ted BOP turn down performances, Varisue program of ecrap eegregation, hot metal desu l fu r iza t i sn and s u i n g are ia e f f e c t cu r ren t ly t o minimize these problems.

It has been our purpose t o emphasize the importance of e f f e c t i v e maintanance prsgrame t o t h e continued Improvement i n product iv i ty of the Gary Caster, and to d e t a i l t h e approaches and methods ueed a d t b rerulte obtained. The ryr tamat ic

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' e l i m i n a t i o n , t o t h e ex t en t p o s s i b l e , o f r e c u r r e n t , product ion-l imit ing equipment f a i l u r e s and the ex tens ion of normal l i f e , through redes ign , of machine component: has been undertaken whi le maintaining product ion a t a h igh level.

The unique n a t u r e of t h e f a c i l i t y made s o l u t i o n of some of t h e problems t ed ious and expensive, and t h e r e was no way t o eva lua t e much of t h e redesigned equipment o t h e r than t o i n s t a l l i t and run i t , no t ing shortcomings and c o r r e c t i n g as ind ica t ed . A l l opera t ing and most of the planned c a s t e r s i n e x i s t e n c e were v i s i t e d and t h e comparison of methods has never ceased.

The previous ly mentioned p i l o t p l a n t was operated u n t i l 1971, and methods anc m a t e r i a l s t r i a l s t h e r e were inva luab le , a s were t h e exhaus t ive rests and t r i a l s run in t h e Applied Research Laboratory of United S t a t e s S t e e l a t Monroeville, Pennsylvania. The importance of t h e engineering work I3yolved i n t h e redes ign and new equipment cannot be over-emphasized.

The p a r t i c i p a t i o n of a l l s t a f f and s e r v i c e groups on t h e Gary Works team can a l s o be c l a s s i f i e d a s unique. Each group - from Medical t o Metal lurgy - has con t r ibu ted t o a t t a i n i n g and maintaining t h e c u r r e n t l e v e l s of r e l i a b i l i t y and q u a l i t y , and continued p a r t i c i p a t i o n w i l l r e s u l t i n f u r t h e r improvement. The p r i d e i n any record performance by t h e c a s t e r is genuinely r e f l e c t e d p l a n t wide.

The most s i g n i f i c a n t c o n t r i b u t i o n s t o t h e success of t h e ope ra t ion have come from t h e crews themselves - t h e opera t ing and maintenance men and t h e f r o n t - l i n e superv isors . A s a group, they adopted a can-do a t t i t u d e very e a r l y i n t h e start- up and through t h e y e a r s have implemented t h e changes and pe r f ec t ed r ev i sed methods wi th eagerness. While many have p a r t i c i p a t e d i n and been rewarded through t h e Employee Suggestion P lan , many i d e a s have simply evolved and proven succes s fu l .

The Gary Machine was t h e f i r s t of a k ind , i n both t h e equipment provided f o r continuous-continuous c a s t i n g and in t h e in - l i ne r o l l i n g f a c i l i t i e s . The des ign speeds and l eng th of runs equated t o a tons-per hour c a p a b i l i t y which was f a r i n excess of most e x i s t i n g machines, on a pe r s t r a n d b a s i s , and t h e very e a r l y successes i n t h e ope ra t ion proved many of t h e t h e o r i e s regard ing non-stop c a s t i n g were v a l i d . The one cons is tency i n a l l t h e problems was t h a t a systematic and d e t a i l e d a n a l y s i s was r equ i r ed i f any improvement was t o be made. Quick and p a r t i a l remedies changed t h i n g s , b u t o f t e n f o r t h e worse, and some s h o r t c u t s t o g e t a machine back in ope ra t ion quick ly were d i s a s t r o u s . Any high product ion c a s t e r must be designed and b u i l t w i th maintenance e f f i c i e n c y as a primary parameter.

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t.4 t.4 ul

EHEATING f URNACE

C O N T I N U O U S C A S T E 7

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SCHEMATIC OF PRINCIPLE OPERATING COMPONENTS

LADLE HOIST TROLLEY 1 A LADLE P0SITK)NING CARS

Exhibit 1

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CURRENT CASTING LINE

0 4 DRIVEN ROLLS

DISCHARGE SECTION

VERTICAL RACK

Exhibit 2

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AVERAGE NUMBER OF HEATS PER STRAND START -1

Exhibit 3

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ORIGINAL CASTING LINE

0- DRIVEN ROLLS

VERTICAL RACK

P I N C H ROLLS

Exhibit 4

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AVERAGE TONS OF SLABS PRODUCED BW MONTH

Exhibit 5 , '

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DOWN TURN REPAIR HOURS PER HEAT CAST YEAR OF 1970 VERSUS FIRST SIX MWM OF 1974

Exhibit 6

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TONNAGE EFFECT OF CONTINUOUS-CONIINUOUS CASTINC

APPROXIMATE ANNUAL PRODUCTION (MILLION TONS)

CURVE "A" 50 MINUTE HEAT TIME AND 50 WEEK OPERATION

CURVE "B" 40 MINUTE HEAT TlME AND 50 WEEK OPERATION

Exhibit 7

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TERMINATIONS BY CAUSE - PERCENT OF HEATS CAST YEARS OF 1971, 1972, 1973 AND F I R S T S I X MONTHS OF 1974

Exhibit 8

REASON

BOP FURNACE

BOP LADLE

TOTAL BOP

CASTER EQUIPMENT

CASTER QUALITY

CASTER BREAK -OUTS

TOTAL CASTER

TOTAL BOP AND CASTER

DETAIL OF TERMINATIONS CAUSED BY CASTER EQUIPMENT - PERCENT OF HEATS CAST YEARS O F 1971, 1972, 1973 AND F I R S T S I X MONTHS OF 1974

Exhibit 9

PERCENT OF HEATS CAST

TORCH AND CARRIAGE

PINCH ROLLS

TRANSFER BED

197 1

2.6

1.2

3.8

2.6

01

.7

3.4

7.2

1972

2.7 .

-8

3.5

2 06

03

lo1

4.0

7.5

1973

2 -0

.8

2.8 -

1 e7

.2

l 9

2 8

5.6

1st. 6 MONTHS 1974

2 -0

l 8

2 e8

1.2

-2

1 -2

2.6

5.4

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,WORLD RECORD SINGLE STRAND CONTINUOUS-CONTINUOUS SLAB CASTING CYCLE

DATES - DECEMBER 14, 15, 16, 17, 18, 19, 1973

TOTAL TIME STEEL IN THE MOLD - 108 HOURS, 25 MINUTES

FEET CAST - 27,434 (5 .2 MILES))

HEATS CAST - 132

TONS CAST - 27,983

TUNDISHES USED - 8 (7 CHANGES)

NOZZLE CHANGES - . SECTION CHANGES -

FEET ROLLED - 48,300 (9 .1 MILES)

TOMS PER HOUR - 258.3

NUHBER OF 40 FOOT SLABS - 1.208

Exhibit 10

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COMPARISON OF UTILIZATION OF CONTINUOUS SLAB CASTERS IN THE UNITED STATES

Exhibit 71