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1
21st National Award for Excellence in Energy Management - 2020
(Thermal Power Stations)
GMR Warora Energy Limited (GWEL)(A 2X300 MW Thermal Power Plant )
Team Member Details:
1. Mr. Mreenal Sharma -Manager
2. Mr. Edwin Williams S - Associate Manager
3. Ms. Pratiksha K Sharma - Manager
2
21st National Award for Excellence in Energy Management - 2020
(Thermal Power Stations)
Presentation Flow :
1. GWEL - At a Glance
2. Energy Management Policy
3. Energy Consumption Over-view
4. Reduction in Sp. Energy Consumption
5. Benchmarking of Energy Consumption
6. Energy Saving projects implemented in FY 2017-18, FY 2018-19 & FY 2019-20
7. Innovative Projects implemented in FY 2019-20
8. Utilization of Renewable Energy
9. Utilization of Waste
10. GHG Inventorization
11. Environment Management-Water
12. Best Practices – Non Energy Efficiency
13. Green Supply Chain Management at GWEL
14. Team work, Employee Involvement & Monitoring
15. Implementation of ISO 50001 at GWEL
16. Long Term Vision on Energy Efficiency
17. Awards & Accolades
18. Learnings from CII/Other Award Program
19. Major Achievement
3
1.1 GMR Group –Values & Beliefs
1. GWEL – At a Glance
Vision
“GMR Group will be an institution in
perpetuity that will build
entrepreneurial organization making a
difference to society through creation
of value.”
Mission
“By 2020, GMR Energy wants to be the most
profitable and one of the leading Integrated
Energy Companies in India and derive value by
• Diversifying strategically across Energy
value chain
• Being a preferred employer
• Being socially responsible”
1.2 Plant Synopsis & Technical Schematic
GWEL Plant Synopsis Technical Schematic
*DNH PPA of 200 MW got Expired on 30.06.2020
4
1. GWEL – At a Glance
1.3 Certificates:
GWEL Follows
“Auditable System Based Approach”
Driven by
Plan
Do
Check
Act
Approach
Deployement
Learning
Integration
5
2. GWEL – Energy Management Policy
2.1 Energy Policy-GWEL:
GWEL is committed to be the Most Energy Efficient and Integrated Energy Utility in the world
Efficient
Management
and usage of
Energy
Adoption of
Best Practices
& Continual
Upgradation
Training &
Knowledge
sharing to raise
awareness
Setting of Energy
Objectives &
Targets
Internal & External
Energy Audits &
Improvement
Initiatives
Compliance with
all legal
requirements
6
3. Energy Consumption Overview
3.1 Plant Performance – FY-19-20
2 x 300 MWCapacity
4138.79 MusGeneration
78.53 %Plant Load Factor
90.65 %Availability
97.77 %Deemed Availability
2322 Kcal/KwhGross Heat Rate
8.23 %Auxiliary Power Consumption
0.14 %DM Water Consumption
2.34 m3/MWhRaw Water
Consumption
0.13 ml/KWhSpecific Oil
Consumption
7
4.1 Year-wise Reduction in Specific Energy Consumption
4. Reduction in Specific Energy Consumption
9.2
8.6
8.2
8.2 8.2
80.1
82.0
86.8
83.4
86.6
76
78
80
82
84
86
88
7.6
8.0
8.4
8.8
9.2
9.6
2015-16 2016-17 2017-18 2018-19 2019-20
Auxiliary Power Consumption - %
APC-% Loading Factor-%
23
26
23
08
22
98
23
21
23
24
80.1
82.0
86.8
83.4
86.6
76
78
80
82
84
86
88
2280
2300
2320
2340
2015-16 2016-17 2017-18 2018-19 2019-20
Gross Heat Rate - (kCal / kWh of Gen)
Gross Heat Rate - (kCal / kWh) Loading Factor-%
*Improvement w.r.t Baseline Year FY 2015-16
99
98
98 99
98
95
86 8289
91
0
20
40
60
80
100
2015-16 2016-17 2017-18 2018-19 2019-20
Plant Availability- (%)
Deemed Availability-% Availability-%
KPI%
Improvement*Reason for Deviation
Heat Rate 0.1 %
1. Machine aging impact as U1
COH deferred from past 2
years & conducted in Aug-
19. Achieved Heat Rate
improvement of 47 Kcal/Kwh
& APC improvement of 0.5%
2. U2 COH also deferred from
last year, same planned in
Dec-2020
3. Heat Rate & APC effected
because of parameter
deviation due to frequent
schedule revisions
4. GCV Deterioration
APC 10.5 %
8
5. Benchmarking of Energy Consumption
5.1 Benchmarking Strategies
Design Performance
PG Test Results
Interdepartmental Benchmarking
Performance after Modification
Past Best Achieved
Benchmarking with Thermal Power Stations
of Similar Capacity & Technology
International benchmarking with strategic Investor –
Tenaga
Site Visits to Similar capacity plants in the
region like
Reliance VIPL Butibori
Dhariwal Power Station
Sharing of Best practices & incorporating the learnings through
Participation in various Forums like Paper
presentations, Awards, Workshops etc
Adoption of World Class Best Practices by Cross-
Sector benchmarking like with our Airport Businesses - Best
Maintenance Practices for HVAC
Internal
Benchmarking
External
Benchmarking
GWEL uses Benchmarking tool to discover best performance being achieved
Within company
With competitor &
With entirely different industry also.
This information is then used to identify
Opportunities for Improvement
9
95.7
99.2
98.3
97.8
99.2
97.8
93.0
90.6
92.8 91.5 85.4 91.7 86.8 94.8
85.9 82.1 88.890.6
2014-15 2015-16 2016-17 2017-18 2018-19 2019-20
Availability–%
Deemed Availability Target Actual Availability
5.2 Internal Benchmarking of Key Performance Indicators (KPI’s)
68.8
76.2
70.5
71.3
74.1
78
.5
86.4 85.1
85.3
85.7 85.2 85.9
2014-15 2015-16 2016-17 2017-18 2018-19 2019-20
Plant Load Factor–%
Actual Availability Target
9.3
9.2
8.6
8.2
3
8.2
8.2
9.1 8.7 8.5 8.5
8.0 8.0
2014-15 2015-16 2016-17 2017-18 2018-19 2019-20
Auxiliary Power Consumption–%
Actual Availability Target
2340
2325
2306
2297
2320
2323
2342
2327 2325
2300
2295 2305
2014-15 2015-16 2016-17 2017-18 2018-19 2019-20
Heat Rate–Kcal/Kwh
Actual Heat Rate Target
2.1
5
0.3
3
0.2
7
0.1
3
0.1
3
0.1
0
0.1
3
2.50
0.89 0.59
0.34 0.36 0.11 0.07
2013-14 2014-15 2015-16 2016-17 2017-18 2018-19 2019-20
SOC–ml/Kwh
SOC Target
2.3
0.5
0.4
0.2
0.2
0.1
0.1
3.0
1.0
0.5 0.4 0.2 0.2 0.2
2013-14 2014-15 2015-16 2016-17 2017-18 2018-19 2019-20
DM Make-up–%
DM Water-% Target
Low Availability & PLF is on account of Coal Shortage & Customer Curtailment. However, GWEL has maintained Machine Availability of 98 % Increase in Heat Rate is on account of Machine Aging & Low Loading factor due to Coal Shortage, Customer Curtailment. 41% of the Time PLF
was less than 80%. U-1 COH done in Aug-2019 & achieved 47 Kcal/Kwh of Heat Rate & 0.18% of APC improvement. U2 COH Planned in Dec-20 Increase in SOC is due to COH; U-2 COH Planned in Dec-2020
5. Benchmarking of Energy Consumption
10
5.3 External Benchmarking with Competitors of Similar Capacity & Technology (FY 2019-20)
5. Benchmarking of Energy Consumption
GWEL achieved the Best Heat Rate, SOC & DM make-up %
95.35
97.7
93.7494.99
91.33
97.80
RPGDhariwal
RelianceRosa
JSWRatnagiri
LancoKorba
DTPSDahanu
GWEL
Availability-%
64.157.3
74.6566.04
76.22 78.53
RPGDhariwal
RelianceRosa
JSWRatnagiri
LancoKorba
DTPSDahanu
GWEL
Plant Load Factor-%
7.91 8.05 8.37 8.409.58
8.23
RPGDhariwal
RelianceRosa
JSWRatnagiri
LancoKorba
DTPSDahanu
GWEL
Auxiliary Power Consumption-%
2353 23442368
2427
2323
RPGDhariwal
RelianceRosa
JSWRatnagiri
LancoKorba
GWEL
Heat Rate-Kcal/Kwh
0.18
0.11
0.14 0.15 0.14 0.13
RPGDhariwal
RelianceRosa
JSWRatnagiri
LancoKorba
DTPSDahanu
GWEL
Specific Oil Consumption-ml/Kwh
0.380.31
0.56
0.270.31
0.14
RPGDhariwal
RelianceRosa
JSWRatnagiri
LancoKorba
DTPSDahanu
GWEL
DM Make-Up-%
11
Plan Do
Act Check
Adoption of New Technologies
Renewable Energy Projects
Energy Conservation projects implementation
Green Supply Chain Management
Evaluation of Energy Performance
Internal & External Energy Audits
Evaluation of Vendors / Suppliers
Benchmarking of Performances
Energy Objectives & Targets
Separate budget for Energy Conservation
Participation in Various Forums & Awards
Training & Knowledge Sharing
Best Operation & Maintenance Practices
Energy Conservation projects for Stakeholders
& CSR
Sustenance Monitoring
Approach
5. Energy Benchmarking
5.4 National & Global Benchmark : Short-Term/Long-Term Target
National Benchmark Global Benchmark
Aux power consumption of the unit % 8.11 % (Dahanu) 7.50% ( TNB Janamanjung)
Gross heat rate (Kcal/kWh) 2273 2280
GWEL achieved Lowest(Best Achieved)
Heat Rate of 2282 Kcal/Kwh & APC of 7.53% at 100% PLF
&
APC-7.16% in Winter & 7.53% in Summer
5.5 Roadmap to achieve National / Global Benchmark : Approach
12
S.No Project Description Status Target Date Annual Expected Benefit
1Installation of Vibro Feeder in Second Stream Conveyor-BCN-2A
Under Finalization Stage November-2020 221.29 Million Kcal
2Installation of 5 MW Floating Solar Plant at Reservoir
Technical Vetting Under Progress December-2020 21.60 Million kWh
3 Unit-2 COH Planned in Dec-2020 COH planned in Dec-20 December-20201.86 Million kWh
92045 Million Kcal
4Six Sigma project taken for Reduction in Start-up Oil consumption by 20% by adopting various operational strategies & new technologies
Under Progress November-2020 454.18 Million Kcal
5Utilisation of fluidized air for hopper instead of hopper heater in ESP
Project Under Study December-2020 3.24 Million kWh
6
Cooling Tower Performance Improvement Programme (Existing Cooling Tower Drift eliminator & Fill replacement, CW line modification etc)
2 Cells Completed,2 Under Progress,PO Placed for 4 more
December-2020 35045 Million Kcal
7
AHP fly ash silo existing 3 no. Conventional HORN antenna type radar level transmitter to be replaced by new DROP antenna radar level transmitter
Procurement Under Progress October-2020 0.131 Million kWh
8Intelligent flow controller (IFC) installation in Compressed Air System.
Procurement Under Progress November-2020 0.23 Million kWh
9CFD Analysis of Flue gas duct-Economiser outlet to APH Inlet
Planned in COH in FY-20-21 December-2020 0.60 Million kWh
10Application of Anti-erosion Coating in ID fan 2A and 2B Impeller
Planned in COH in FY-20-21 December-2020 0.90 Million kWh
11Cooling tower fan motor to gearbox metallic shaft to be changed with carbon fiber shaft
Vendor Exploring Under Progress January-2020 1.05 Million kWh
12 VFD installation for Induced draft Fans Planned in COH in FY-20-21 December-2020 3.56 Million kWh
Total Expected Benefits : Electrical Energy : 33.17 Million kWh Thermal Energy : 127225 Million KCal
5.6 Future Plans towards Energy Conservation – FY-20-21
5. Energy Benchmarking – Action Plan
13
6.1 Energy Conservation Projects implemented in last 3 FY’s
6. Summary of Energy Saving Projects
Financial Year
No. of
Projects
Implemented
Savings Achieved Expenditure
DoneElectricity Coal Oil
Lakh kWh MT Kl Lakh
FY 2017-18 18 133.88 9142 102 264
FY 2018-19 20 230.94 1168 165 31*
FY 2019-20 22 237.84 53752 41 862
Total 60 602.65 64062 308 1157
* Investment done in Previous FY
14
6a. Energy Saving projects implemented in FY 2017-18
S.No. Title of ProjectAnnual Electrical
Saving (kWh)
Annual Thermal Saving
Total Annual Savings
(Rs million)
Investment Made
(Rs million)
Payback (Months)
1Reduction in Start up/Shut down Cycle Time through implementation of various measures.
0 101.64 kl 4.228 0.00 0.0
2 Heat rate improvement programme from 2308 to <2300 kCal/kWh. 0 9142 MT 30.727 0.705 0.3
3Power factor improvement at all Balance of plant loads by installing capacitor banks (Installed in Stacker LT MCC bus section and Bunker MCC).
537506 1.613 0.00 0.0
4 Air Handling Unit power optimization in ESP control room. 13500 0.041 0.00 0.05 Optimization of ESP Power through Power Saver Mode 5873499 17.620 0.00 0.06 Further optimization of CW Pump running hours 3334915 10.005 0.00 0.07 Further optimization of CT Fan running hours 332507 0.998 0.00 0.08 Optimization of CEP output through VFD* 323499 0.970 0.00 0.09 Optimization of LDO Pump output through VFD* 3848 0.012 0.00 0.0
10 Optimization of Mill Seal Air Fan output of U-I & II through VFD 57237 0.172 0.27 18.9
11 Optimization of Hotwell M/U Pump output through VFD* 6966 0.021 0.00 0.012 Optimization of MGF Feed Pump output through VFD* 8399 0.025 0.00 0.0
13 Optimization of BA Conditioning Pump through VFD * 62972 0.189 0.00 0.0
14 Plant wide LED installation (Phase-I & II) 141255 0.424 24.84 703.4
15 Optimization of ACW Pump running hours 837056 2.511 0.00 0.0
16 Optimization of ECP Pumps output through VFD * 61221 0.184 0.00 0.0
17 Optimization of Raw Water Pumps output through VFD * 437708 1.313 0.00 0.0
18
Reduction in Auxiliary Power Consumption due to Loading factor improvement, Heat rate improvement, Energy deviation analysis (EnMS), Optimization of excess air, Attending ESP, APH & duct leakages and other miscellaneous steps.
1355612 4.067 0.63 1.9
Total 133876999142 MT
102 Kl75.12 26.45
* Investment done in Previous FY
6a. EnCon Projects of FY 2017-18
15
S.No Title of ProjectAnnual
Electrical Saving (kWh)
Annual Thermal Saving
Total Annual Savings
(Rs million)
Investment Made
(Rs million)
Payback (Months)
1 Make up of Cooling Tower fore-bay by gravity and Minimization of Pump Operation 257180 0.772 0.51 8.0
2 Replacement of Existing conventional light with LED’s throughout plant-Phase-II* 1720357 5.161 1.86 4.3
3 Degassifier water usage through gravity to CT forebay 106537 0.320 0.26 9.64 Installation of VFD in AHP CCW Pump 82832.28 0.248 0.27 12.8
5Installation of roof transparent sheet at AHP compressor house for daytime illumination
4380 0.013 0.02 13.7
6 Single Engine operation of Locomotives 37.05 Kl 2.698 0.00 0.0
7Running of 1 no. of Air washer pump with 100% discharge open instead of 2 pumps with 50% discharge open
120888 0.363 0.00 0.0
8 Energy Saving opportunity in Mill-F LOP 87768 0.263 0.00 0.09 Condensate dumping from LP Heater-4 for reduction in blow down hours 511 MT 1.897 0.03 0.2
10 CW blowdown line connection from CW return line 657 MT 2.438 0.03 0.111 Utility Pump Operation Optimization 11548 0.035 0.00 0.0
12FD fan servomechanism operating fork link modification for better control over blade pitch.
86052 0.258 0.02 0.9
13 Installation of Motion Sensor in Washrooms 1051 0.003 0.002 7.614 Oil Consumption Optimization by improving operational philosophy 107 Kl 5.590 0.00 0.015 CHP Operational Optimization 381400 1.144 0.00 0.016 Optimization of CW/ACW Pump & CT Fan running hours 5886583 17.660 0.00 0.017 Optimization of Pump & Fan output through VFD* 2562600 7.688 0.00 0.018 Optimization of ESP Power through Power Saver Mode 10423162 31.269 0.00 0.019 Reduction in Diesel Consumption in CHP by adopting best operating practices 21 Kl 1.494 0.00 0.0
20
Capacitor bank installation in1. AHP LT MCC section-A & B 2. DM plant MCC section-A3. CHP LT MCC bus section-A & B 4. Bunker LT MCC bus section-A5. Stacker LT MCC bus section 6. WT LT MCC bus section-A & B
1361214 4.084 0.10 0.3
Total 230935521168 MT
165 Kl83.398 3.09
* Investment done in Previous FY
6b. Energy Saving projects implemented in FY 2018-19
6b. EnCon Projects of FY 2018-19
16
6c. EnCon Projects of FY 2019-20
6c. Energy Saving projects implemented in FY 2019-20
S.No Title of ProjectAnnual
Electrical Saving (kWh)
Annual Thermal Saving
Total Annual Savings
(Rs million)
Investment Made
(Rs million)
Payback (Months)
1 Reduction in Windage losses by Improvement in H2 Purity 929097.60 2.787 0.020 0.1
2Energy Conservation by Use of Rain Water Harvested from WTP area building roof tops as Cooling Water Makeup in CW Fore bay
3846.31 0.017 0.033 22.9
3 Reduction in Diesel Consumption by installation of Vibro-feeder in Truck Hopper 27 Kl 1.969 1.86 11.34 Auto Closure of Valves during Black-out to avoid Diaphragm Rupture 14 Kl 0.716 0.00 0.05 Improvement in Yard losses by 51 Kcal by adopting best operational strategies 37175 129.168 0.500 0.0
6Fan Power Consumption Optimization by attending Flue gas duct Leakages & Fan Impellar Coating
2065562.92 6.197 10.76 20.8
7 Heat Rate Improvement Through CT Fills Replacement & Condenser Cleaning 3505 Tonn 12.177 16.06 15.88 Heat Rate Improvement by Turbine Overhauling 6659 Tonn 23.136 40.71 21.1
9Boiler Efficiency improvement by attending duct leakages, Valves Servicing, Coal Mill Orifice adjustment
6413 Tonn 22.284 16.13 8.7
10Stopping of Ferric Chloride dosing pump by providing Ferric Chloride Tank By-pass discharge line for gravity dosing
5390.00 0.016 0.002 1.5
11 Alternate Street Lights in Service after 11 PM inside PTS 8820 0.026 0.02 6.812 Auto Operation of Lamps in CW pump house 876 0.003 0.004 18.313 CSU Screw Conveyor Bypass Modification Work 2409 0.007 0.01 8.314 Installation of Advanced Drift Eliminator in Cooling Tower 8900 0.040 0.09 28.015 Transparent sheet cladding in RO-DM Plant & Bunker floor to reduce lighting load 10950 0.033 0.03 11.0
16Replacement of Conventional exhaust fans with energy efficient exhaust fans at washrooms
4555 0.014 0.0208 18
17 To provide CT make up by gravity without CT make up pump pumping* 416268 1.249 0.00 0.0
18Replacement of Existing conventional lightings with LED’s throughout the plant-Phase-II*
3225190 9.676 0.00 0.0
19 Degassifier water usage through gravity to CT forebay* 140770 0.422 0.00 0.020 Optimization of CW/ACW Pump & CT Fan running hours 4177098 12.531 0.00 0.021 Optimization of Pump & Fan output through VFD* 2472930 7.419 0.00 0.022 Optimization of ESP Power through Power Saver Mode 10311368 30.934 0.00 0.0
23784029.9953752 Ton
41 Kl260.82 86.23* Investment done in Previous FY
17
6.2 Absolute savings achieved & Investment made:
225.9
359.8
590.7
828.6
0100200300400500600700800900
2016-17 2017-18 2018-19 2019-20
Energy Savings (Lakh kWh/year)
15691
24833
26001
79753
10000
30000
50000
70000
90000
2016-17 2017-18 2018-19 2019-20
Coal Savings(MT/year)
1349
2101 2934
5539
0
1000
2000
3000
4000
5000
6000
2016-17 2017-18 2018-19 2019-20
Financial Benefits(Lakh Rs/year)
84
349
380
1242
0
500
1000
1500
2016-17 2017-18 2018-19 2019-20
Investment made(Lakh Rs/year)
Cumulative Benefits Achieved
***All savings are w.r.t Baseline Year FY 2015-16. Absolute Savings considered for FY-19-20
***All savings achieved audited by Management Assurance Group (MAG) Audit.
FYEnergy Savings
(Lakh kWh/year)
Coal
Savings
(Ton/year)
Oil Savings
(kl/year)
Financial Benefits
(Lakh Rs./year)
Investment
made-Year wise
(Lakh Rs./year)
2016-17 225.90 15691 403 1349 84
2017-18 359.78 24833 505 2101 264
2018-19 590.72 26001 670 2934 31
2019-20 828.56 79753 711 5539 862
Cumulative 828.56 79753 711 5539 1242
6. Summary of Energy Saving Projects-Benefits
18
7.1 : Make up of Cooling Tower fore-bay through gravity and Minimization of Pump Operation
Replicability : YES
7. Key Project implemented in FY 2018-19
Results Achieved: Reduction in APC as shown below
Project Trigger: Through Quarterly Internal Energy Audit
Implementation:
Earlier, 2 out of 3 pumps used to run for 16-20 Hrs per day to cater CT make-up
requirement by taking suction from RGSF sump & discharge to CT fore-bay
Now, Separate line laid from existing RGSF bed outlet channel to CT make-up
pump discharge header.
This line is providing make-up water through Gravitational Head without
Pumping & giving huge saving in terms of energy consumption by pump
Reduction in Running Hours of Pump by 50% achieved.
0
500
1000
1500
2000
2500
3000CT Make-Up Pump Power Consumption
Description
CT M/u Pump Running-Considering 2 Pumps
RunningSavings
Daily Run Hours
Energy Consumption
Hrs Mwh %
Before Gravity Make up
38.43 2.11
After Gravity Make up
17.75 0.98
Savings/Day 20.68 1.14 53.81%
Project Implemented
System Modification
19
7a : Reduction in Auxiliary Power & Diesel Consumption by Installation of Vibro-feeder in Belt Conveyor
Replicability : YES
7. Innovative Projects implemented in FY 2019-20
Solution Implementation:
Vibration Feeding technology with controlled feeding rate was explored to mitigate
the problem of high diesel consumption, Partial loading & belt wear.
Vibro-feeder with Rack & Pinion Gate arrangement (RPG) was installed at BCN-2B
Truck hopper which eliminated Poclain usage by directly pushing coal through
dozer & RPG helped in even loading of belt by controlled feeding.
New & Innovative approach with high risk & high cost involvement for coarse duty
material handling & is First time implemented for CHP Conveyor belt at National Level
by GWEL.
300
600
Before After
Improvement in Belt Coal Feeding Rate-TPH
15.4311.63
3.8
Before After Saving
Reduction in Diesel Consumption-Ltr / 100 MT Coal Crushed
10965282648
27004
FY-18-19 FY-19-20 Saving
Reduction in Diesel Consumption-Ltr
Impact :
Reduction in Diesel Consumption by 25%
Belt Loading improved from 300 to 600 TPH & wear & tear reduced
Problem Description:
Alternate coal arranged from nearby mines due to severe coal shortage & same was
transported through truck to plant & stored in truck hopper yard & then moved to truck
hopper for loading conveyor belt with help of dozer & poclain.
This led to increase in diesel & Energy consumption due to frequent handling of
coal through Dozer & Poclain & partial loading of conveyor belt due to inconsistent
feeding through truck hopper leading to coal spillage, belt running out & reducing life
of Conveyor.
Vibro Feeder
SOP for Vibro Feeder
20
7b : Reduction in Auxiliary Power Consumption by reducing Turbine Cooling Time
Replicability : YES
7. Innovative Projects implemented in FY 2019-20
Problem Description:
Annual overhaul is essential activity for plant up-keepment & consumes energy while
turbine on barring gear & during maintenance.
AOH is planned activity of approx. 25 days, out of which 10 days is taken for Turbine
Natural Cooling before the temperature of turbine components (FSMT) reaches at
level that allows maintenance work to begin and stop all turbine auxiliaries.
This high cooling time leads to increase in unit downtime & running auxiliaries
of turbine contributes to power consumption.
Solution Implementation:
The process was first analyzed in Numerical Simulations for various cooling conditions
for mitigating any risk of stress
On load Cooling - Turbine is fed with live steam at lower pressure & temperature
under “sliding conditions” to decrease temperature of its components during on load.
Off Load Cooling - This cooling process starts immediately after shut down by
maintaining partial vacuum in turbine and continued until temperature of components
reaches the desirable level.
Very fine Cooling adjustments are required for avoiding any parameter deviation.
Modification done at site for turbine cooling.
GWEL is first plant to implement this cooling procedure for SEC machine in India
Joint protocol signed with SEC (OEM) for SOP developed by GWEL.
Impact :
Electrical Energy Saving - 36535.5 KWh
Revenue generation by Increase in Unit Availability - Rs. 6.4 Crs
SOP was shared with peer plants and achieved desired results
160 53
Turbine Cooling Time Reduction-Hrs
Before After
Numerical Simulations
Modification
OEM Joint Protocol
21
7c : Reduction in Generator Windage losses by Improvement in H2 Purity
Replicability : YES
7. Innovative Projects implemented in FY 2019-20
Impact :
Generator Windage losses improved by 57 KW
Improved purity from 95% to 98% which is best in SEC supplied unit in India
Problem Description:
At GWEL, design hydrogen purity is 99% but same not achieved since
commissioning & maintaining at around 95%. This is an inherent issue in all
Chinese supplied machine in India.
Less Hydrogen purity contributes to Energy losses & same is a disastrous Safety
threat as well
Solution Implementation:
Adopted Six Sigma methodology blended with Strategical tools for improving
Hydrogen purity
I-MR chart - To identify when the process goes out of control and also to indicate
where to focus for source of assignable cause
Normality test - To check data consistency
Kano Model – Identification of CTQ
Fish Bone & Cause & Effect Matrix – Identification of probable causes &
Recommended action.
Total 5 number of improvement initiatives has been implemented
263.86
56.93
206.93
Before Reduction After
Windage Losses Reduction-Kwh
98.2
95.7 96.595.2 95.1
GWEL RosaPower
Dhariwal JSWRatnagiri
ReliancePower
Hydrogen Purity Comparison with Peers-%
9598
Before After
Hydrogen Purity Improvement-%
22
8. Use of Renewable Energy / ENCON measures
8.1 : Renewable Energy Projects at GWEL
(150 nos.) on TG Building, Ware House, CW Pump House,
AHP Compressor House by replacing motor operated fans.
Solar water heater of capacity 1000 LPD installed
at Associate employee township.
Solar Water Heater in Permanent Township
installed for 150 Families
Translucent sheet cladding in CHP belt conveyors,
Compressor House, RO-DM to reduce lighting load
Pipe light in Stores & Warehouse.
Wind operated Cooling
Fans
Solar Water Heater for
Associates
Solar Water Heater for
Township
Translucent sheet
cladding
Pipe-lighting
Renewable
Energy
Utilization
Roof Top Rainwater
Harvesting
Roof Top Rain Water Harvesting from all buildings.
Rainwater HarvestingDeep Aquifer Recharge by Rainwater Harvesting in
Plant & Colony
23
8. Use of Renewable Energy / ENCON measures
8.2 : Savings achieved through Onsite Renewable Energy Projects
2015-16 2016-17 2017-18 2018-19 2019-20No. of Project
Implemented2 1 1 3 3
Total Capacity - MW 1Total Power Savings
Lakh KWh80.70
% Share 0.20Cumulative Savings
(Rs Lakh)16.93 25.63 38.76 68.20 242.09
RPO Obligation Nil
8.3 : Renewable Energy Projects under Implementation at GWEL
Key Highlights:
05 MW Internal Grid connected Floating Solar Installation on Plant reservoir
Contract Finalization completed, project execution by Nov-2020
Payment through POS (Pay out of Savings) Scheme to ESCO.
Electricity generated to be fed as internal APC throughout the plant.
24
9. Environment Management-Ash Utilization
9.1 : Utilization of Ash Generated
Distribution of Areas of Ash Utilization
Sr No. Particulars UoM 2017-18 2018-19 2019-20
1Ash Utilized in manufacturing of cement/ concrete others similar products
% 83% 68% 53%
2 Ash Utilized in Fly Ash Bricks % 6% 0% 14%
3 Ash Utilized in Mine Filling % 0% 9% 2%
4 Ash Utilized for Road Pavements % 3% 4% 26%
5Ash Utilized in Brick Manufacturing ( from Bottom Ash)
% 8% 13% 4%
6 Ash Utilized in Bottom Ash Mine Filling % 0% 4% 0%
7Ash Utilized Bottom Ash for Road Pavements
% 0% 2% 0%
8 Expenditure on Ash Utilization (annual)INR
(Lakhs)0.25 0 828
Ash Utilization at GWEL is 100% of the Total Ash Generated
66
87
104109 106
2015-16 2016-17 2017-18 2018-19 2019-20
Year-wise Ash Utilization - %
7.60 8.43 8.82
4.86 4.54 3.82
2017-18 2018-19 2019-20
Ash Generated Vs Ash Stock-Lakh MT
Ash Generated Ash Stock
1010
80
Ash Handling Method
Wet Semi Dry Dry
10-%- Through Slurry Pumps
80%-Through Bulkers
10%-Through Ash Conditioners & Dumpers
Utilization of Ash at GWEL
25
9. Utilization of Waste
9.2 : Utilization of Waste Water for Low End Applications
Application of RO-DM Plant waste water in AHP for
Makeup water to ash slurry pump & flushing water pump
Floor Cleaning in AHP & Boiler Area
B.A. Dust conditioner pump water tank filling
Bulker washing spray system
Cleaning of pipe racks
Water sprinkling arrangement at Ash Pond
Fountain at FA silo area
Application of RO-DM Plant waste water in CHP for
Sprinkling in Coal Yard
Dust Suppression System
Application of CW Blowdown water as
Make-up for Firefighting system
Other downstream requirements after ERS
Application of Domestic waste water for
Development of Green belt
Application of Waste Water in AHP
Application of Waste Water in CHP
Application of Domestic Waste Water for Greenbelt
9.3 : Utilization of Organic waste for Manure production in Plant & Colony
All the organic waste generated at Plant & Colony is used for
the production of manure through Bio composter.
The manure generated is utilized for vegetables and fruit
bearing plants planted inside plant premises & in Colony.
26
10. Environment Management-Emission
10.1 GHG Inventorisation
GMR Sustainability Report
Every year GMR group publishes its sustainability report for public.
It is available on the following link: Scope-1 Emission
https://www.gmrgroup.in/energy/
Best Practices for Maintaining Emission Level within Norm
Current Control: GWEL is having Low Nox Burner installed since design stage
with Nox value within norms limit
GWEL is having 100% Ash Utilization
Coal Blending through Automated Software to minimize
emission & maximize efficiency. PM within norms limit
Real time Ash monitoring system installed
Transportation of ash through jumbo bags by train mode
Future Control: FGD Implementation by 2021- Contract finalization
completed, Project Execution will start from Nov-2020
5 MW Floating Solar Installation- Contract finalization
completed, Project Execution by- Nov-2020
AAC (Aerated Autoclave Concrete ) block manufacturing unit
installation for further enhancement of Ash Utilization
727 739 7341200
2017-18 2018-19 2019-20
SOx Emissions-mg/Nm3
276 265 264300
2017-18 2018-19 2020-21
NOx Emissions-mg/Nm3
46 45 4550
2017-18 2018-19 2020-21
Particulate Matter-mg/Nm3909 918 919
2017-18 2018-19 2020-21
CO2 Emission-Ton/KW
10.2 PAT Cycle-II Compliance
PAT Cycle-II - Energy Consumption Target & Actual - Registration No.-TPP0149MH
Energy Consumption & Production for
Baseline Year 2014-15
Target Net Heat Rate for
Assessment Year 2018-19
Actual Net Heat Rate Achieved for
Assessment Year 2018-19
Net Heat Rate
(Kcal/Kwh)
Net Product Output
(Million Units)Net Heat Rate (Kcal/Kwh)
2581.52 3277.35 2554.62 2524.24
Operating Station NHR achieved with Normalization in FY 2018-19 : 2524.24 kCal/kWh
Number of Escerts to Sell : 9956 Price of Escerts to sell : Rs. 1 Crores
27
11. Environment Management
11.1 Specific Water Consumption
3.82.4 2.3 2.4 2.2 2.3
3.5
2.21
FY 2014-15 FY 2015-16 FY 2016-17 FY 2017-18* FY 2018-19 FY 2019-20
Specific Water Consumption (m3/MWh)
Specific Water Consumption CPCB Limit
0.50.37
0.19 0.15 0.12 0.14
FY 2014-15 FY 2015-16 FY 2016-17 FY 2017-18 FY 2018-19 FY 2019-20
DM Water Consumption (%)
GWEL is a Zero Liquid Discharge Plant
Zero Liquid Discharge Scheme
S
N
o
Waste
Generation
Area
Generation PointCollection
PointTreatment Process
Application of treated
waterPhoto
1Pre-
Treatment
Plant
PT & ERS clarifier
Sludge
Handling
System
Sludge pit- Sludge Thickener-
Centrifuge Feed tank-
Centrifuge- Sludge Transfer point
Water recycled to
Reservoir
Solid Sludge separated
disposed to Ash dykeRGSF Back washSupernatant
tankPhysical Settlement of impurities
2RO-DM
Plant
RO & UF Reject/
MGF Backwash/ DM
Regeneration waste
Effluent
Collection
(EC) Pit
Acid and Alkali treatment
scheme for Neutralization
Ash handling plant
Coal handling plant
3
Circulating
Water
System
Cooling Tower
Blowdown
CW
Blowdown
tank & Dead
Storage for
Fire Water
System
Effluent recovery system (ERS),
wherein water is passed through
Clarifier- MGF- UF- RO system
Fire Fighting System
make up
Stored in ERS Clarified
water storage tank for
downstream
applications
4Domestic
Waste
Various domestic
waste generation
points
Collection
sump of STP
Collection sump- Collection
chamber- FBR (Fluidized Bed
Reactor)- Tube settler- Clarifier
storage tank- Filter Press
Green belt development
and landscaping
28
11. Environment Management
11.2 Best Practices in Water Management
Dedicated Water SCADA for Water
consumption accounting &
balancing.
32 Flowmeters installed plantwide
Key Benefits :
Area-wise Water consumption &
cost accounting
Specific water consumption
Monitoring
Identification of Water Wastage
Automated Reports
Real Time Dashboard & Trend
Alarm for increase in Water
Consumption above base value
WaterSaving-317314 m3
At Plant:
Deep Aquifer Recharge:
Plant-wide storm water drains
connected to Rain water
harvesting pond.
Annual Rain Water
Harvesting of 8.6 Lac m3.
Rooftop Rain Water Harvesting:
Rain water harvesting from
building roof tops & used as
cooling tower makeup .
Fresh Water Saving of
13140.46 m3/Annum
At Colony:
Water collection from Building
Rooftop & drains for Deep Aquifer
Recharge
External Water Audit by CII Triveni
Water Institute.
Plant overall water balance
Opportunities for Water
Conservation
8 Nos. of recommendations given &
all implemented resulted in
significant water saving
Internal Audit:- Through CIPs -
Continual Improvement Plan
Every year CIPs being taken
through Cross-functional team for
internal assessment of water
resources & conservation by
internal audits,
Water Saving of 1.94 Lac m3 has
been achieved through CIPs
Awareness on Scientific
Watershed Management for
improving water condition in
draught areas
RO Water ATM installed in 14
Villages for providing Safe
drinking water in fluoride zone
Check Dams construction
Pond deepening at nearby
villages
2 Nos. KT Weir restored
More than 285 acre land
brought under irrigation
Water SCADA Rain Water Harvesting Water Audit Water-Beyond the Fence
29
12. Best Practices in Plant-Non Energy Efficiency
12.1 Best Practices – Non-Energy Efficiency
Biodiversity
Friendly Habitat for
Floras & Faunas
Afforestation
Green GWEL
Flexibility
Sale of 10 MW of
Power saved through
APC in Market
Asset Management
GWEL is Certified with
Asset Management
System
Digitisation-
”Digital GWEL”
Project SARATHI –
Digital Platform for
Becoming Paperless
Regulatory Market
with Fixed tariff
Sustenance by
Agility & Innovation
First Plant to
Materialize this
Opportunity for
Revenue Generation
Revenue Generation
– 7.58 Crs
27 Process Digitized
with PDCA approach
Digital Logbook
Near Miss, Incidents
IMS Internal Audits
Waste Management
Vehicle Gate Pass
Agency Gate Pass
Agency Evaluation
HIRA ….. ETC
Increase in no. of
various bird species like
Indian pond heron,
Indian roller, etc
Various varieties of fruit
bearing & forest species
plants like Danima,
Eycaliptus, Golichowli,
Conocorophous,
Jamun, Amla etc
41% of the total
Plant area is
covered under
Green Belt against
norm of 33%
Total 200250 No. of
Plants has been
planted in plant area.
Plantation has been
done in nearby
villages under CSR
activity.
AMS Helped in
Performance & Cost
improvements
Management of risk
Enhanced stakeholder
confidence
AMS implementation by
Asset System Manual
AMS Procedures
Work Instructions and
Manuals
Identification of
Significant Assets by
Asset Risk register
30
12. Best Practices in Plant-Non Energy Efficiency
12.1 Best Practices – Non-Energy Efficiency
Nirmal Jeevan
InitiativeSocial Responsibility
Power Sale
Optimization Model
Reliability Centered
Maintenance
Online Monitoring
System for Ash &
Density
Data analysis tool to
generate innovative
solutions to Cope
with dynamic &
regulated scenario
for correct decision
making for
profitability
improvement
1. Online Ash & Moisture
Content Analyzer –
Provides instantaneous,
continuous, on-belt
measurement of Ash
and Moisture in coal
2. Online Ash Density
Meter - for Continuous
Online monitoring of
water content to
optimized on water
consumption
Employees Wellbeing is
of Paramount
Importance
Various Wellbeing
Initiatives being taken
Fun Run
Kausalika
Tournaments
Celebrations
Open Air Movie
Outbound Trainings
Yoga & Mindfulness
Heath Awareness
Infrastructure support to
Govt Schools
Kid Smart Centers
Transportation Facility
for students
Health Clinics & Camps
Construction of
Iindividual Sanitory
Lavoratory
Vocational Training
Center
Tailoring centers for
women
Farmers Training
Community Libraries
Drain Construction
Best in class Maintenance
Methodologies adopted for
100% reliability
Vibration Analysis
Lube Oil Analysis - Wear
Debris, NAS, TAN
Infrared Thermography
Dissolved Gas Analysis
Motor Current Signature
Analysis
At GWEL we follow Six
Sigma based approach
for Chronic issues.
WellnessBeyond The Fence-
CSRResearch
Maintenance &
ReliabilityNew Technology
Education
Health Hygiene & Sanitation
Empowerment & Livelihood
Community Development
31
13.1 Initiatives taken in Supply Chain to Reduce Energy Consumption
SN Projects Implemented at GWEL End
1Evaluation Format for Significant Energy consuming
equipment's/ Auxiliaries for vendors.
2
Procurement of Energy Efficient, free of hazardous
materials , repairable and made of modular
components and highly recyclable electronics.
3Identification of local suppliers/ vendors for improved
logistics.
4Integration of energy efficiency with the procurement
process and policy.
5 Refurbishment of spares
6Energy Management System and Water Management
system
7 Condition Monitoring of Equipment's
8Recycling of Waste generated within the Plant &
Colony
9
Companies vision for Green Supply Chain
Management communication to Suppliers through
policy
13. Green Supply Chain Management at GWEL
GWEL is committed to be the “Most Energy Efficient Unit” along-with “Minimizing Carbon Foot Print” in
all direct/indirect processes by adopting “Green Supply Chain Management”
Projects Implemented at Suppliers End
Sr No.Projects Implemented by
GWEL for SuppliersBenefits Achieved to Suppliers
1 Eco-Friendly Packaging SystemMinimization of impact of Supply Chain on
Environment
2Supplier Evaluation Program &
Feedback for Improvement
Awareness on Safety, Energy & Environment
leading to resource conservation & reduction
in carbon foot print
3 Training & Awareness Program
• Efficient Resource Management
• Energy conservation measures at their
premises
4
Encouragement for adopting
EnMS-ISO 50001 & Purchase
preferred from ISO 50001 supplier
Suppliers are adopting ISO-50001 & has
helped to improve efficiency and reduced
production cost
5
Energy Efficiency Audits for
Supplier-Implementation of
Equipment Performance
Evaluation Format
• Helped Potential vendors to gain
competitive advantage over competitors
• Market Opportunities for Potential Vendors
6Encouragement & Support for
Green Logistics
Reduction in transportation cost & carbon foot
7Sharing of Energy Conservation
opportunities with Vendors
Energy Conservation projects implementation
by Vendors thus reduction in carbon foot-print
Total Investment Made- 2 Lacs
32
Centralized Energy Management System
Real Time Comparison of HT & LT Equipment’s Auxiliary Power
consumption in EMS system for both Units, BOP, AHP & CHP
Auto Reports Generation for Energy Consumption on Daily/
Monthly and FY basis
Trending for better Analysis of Energy Consumption
System Upgraded for
Availability of Plant-wide Equipment's with Rating >75KW
Availability of Alarm, Auto SMS & Mail Facility
14.1 Monitoring of Energy Consumption
14. Team work, Employee Involvement & Monitoring
Energy Measurement Process & Validation:
Electrical Energy(KWh) Thermal Energy- Coal Thermal Energy- LDO Thermal Energy- HSD
Installing Energy Meters and
Monitoring online through
EMS
Accuracy Class of Energy
meters : 0.5
Calibration Schedule in form
of SAP notification.
As Fired Coal Weighment
through Coal Feeders.
Coal feeder Integrator recorded
in DCS.
Accuracy Class : +/- 0.2%
Calibration Schedule in form of
SAP notification.
LDO tank oil level & the
difference of the tank level
with respect the calibration
charts is monitored.
LDO tank oil level Transmitters
are calibrated on regular basis
HSD tank oil level & the
difference of the tank level
with respect to calibration
chart is monitored.
HSD tank oil levels are
Monitored on regular basis
33
14.2 Daily MIS Reports for Monitoring of Energy Consumption
Daily Energy Deviation Report Daily APC Break up Report
Daily Heat Rate Report
Daily & Monthly Plant Performance Report
Equipment Performance Test
Daily Water Consumption Monitoring Report
14. Team work, Employee Involvement & Monitoring
Dashboards for Sustenance Monitoring
Daily Parameter Excursion Report Cooling Tower Performance Test
34
14.3 Trainings & Workshops related to Energy Conservation
Internal & External Trainings and Workshops related to Energy Conservation
Sr.No Program Name & details Organized By
1 Six Sigma Training to All Employees for Structured Methodology of Energy Efficiency Optimization M/s KPMG
2 Workshop on Opportunities for Energy Saving in Thermal Power Plant M/s NPC
3 Workshop on Energy Audit Process for effective Energy auditing M/s NPC
4 Understanding the best practices of Energy Management System M/s EU India
5 CII Energy Efficiency Summit M/s CII
6 National Boiler Work Shop M/s NPC-Visakhapatnam
7 O&M conference on best practices by NTPC M/s NTPC
8 Overview of PAT Scheme: Achievements & prospects M/s BEE
9 Regional Workshop on PAT Scheme M/s BEE
10 Strategies & Best Practices on Energy Efficiency, Conservation & Management for Sustainability” by CII M/s CII Nagpur
11 Workshop on "Advanced Training Program on Energy Efficiency" by CII M/s CII Hyderabad
12 Workshop on "RCM & Streamlining the Maintenance Processes for Better Productivity & Energy Efficiency" by CII M/s CII Nagpur
13 Workshop on Induced Draft Cooling Tower Performance Enhancement In-house
14 In-house Workshop on Plant Performance Monitoring-(Boiler Efficiency, Heat Rate, Cooling Tower, Pump, Fans) In-house
15 Knowledge Sharing Session on "Operational SOP for Auxiliary Power Consumption Reduction at GWEL" In-house
16 Training on Energy Management System (ISO 50001) & Energy Conservation awareness for all stakeholders In-house
17 In-house Workshop on Learning from Failures in Thermal Power Plants In-house
18 In-house Workshop on Learning from COH in Thermal Power Plants In-house
14. Team work, Employee Involvement & Monitoring
35
14.4 GWEL – Celebration of Energy Conservation Week
Display of Energy Conservation Posters
EC Training for GWEL Employees and Associate employees
EC Programme for Children of nearby village schools
Competitions based on EC for Employees, Associates, family members etc
EC programme for family members
Felicitation of Winners
14.5 GWEL –Training & Awareness to Associates
14.6 GWEL – Web based Portals for Creating Awareness
EnMS (ISO 50001) Web Portal in GMR intranet EnMS (ISO 50001) web page in GMR intranetKnowledge Management Portal in Intranet
14. Team work, Employee Involvement & Monitoring
36
14.7 Involvement of Employees in Energy Conservation
Formation of Energy Management Cell under ISO-50001.
Objectives of EMC :
Monitoring of Specific Energy Consumption
Energy Audit (Internal & External) Recommendation
implementation status review
Discussion on Energy Conservation Projects
Identification of New Energy Conservation Initiatives
Members of EMC : Plant Head (Chairperson), O&M Head, Head
of EMC, EMC members (Energy Managers & Auditors)
Total Energy Managers- 21 Energy Auditors- 18
Appointment of Energy Leaders
Appointed throughout the plant & township
Monitoring of Energy consumption in their area
Reporting of Energy (Electrical, Thermal, Air, Water
wastage)
Identification of energy saving opportunities.
Monthly Localized Energy Audits through Checklist
Total 23 Energy leaders appointed.
EMC MOM
Monthly Energy Leader Checklist
14. Team work, Employee Involvement & Monitoring
37
14.8 Projects implemented through Kaizen ( Workers and Supervisor level)
At Supervisor Level At Workmen Level
Stopping of Ferric Chloride dosing pump by providing
Ferric Chloride Tank By-pass discharge line for gravity
dosing
Auto Operation of Lamps in CW pump house by Day-
Night Sensor
CSU Screw Conveyor Bypass Modification Work for
stopping Motor
Installation of roof transparent sheet at RO-DM for
daytime illumination
Replacement of Conventional exhaust fans with energy
efficient exhaust fans at washrooms.
Utilization of EC Pit water for floor cleaning instead of
fresh water
Saving of power consumption in PTS by modification of
Connection to keep Alternate Street Lights in Service
after 11 PM inside PTS
Reduction in Auxiliary Power Consumption in
Compressor House by identifying and attending air
leakages.
14.9 Expenditure towards EnCon Projects
• - Implementation of few projects of FY 2016-17 was already started in FY 2015-16. Budget of these projects is considered in FY 2015-16.
• - Implementation of LED projects of FY 2018-19 was already started in FY 2017-18. Budget of this projects is considered in FY 2017-18
321.85 324.61
84.27
264.45
30.87
862.30
2014-15 2015-16 2016-17* 2017-18 2018-19* 2019-20
Expenditure towards EnCon Projects – In lakhs
% Investment on Turnover in FY 2019-20 : 0.47%
14. Team work, Employee Involvement & Monitoring
38
14.10 Major Area of Concern in Energy Efficiency & Reliability
One out of 3 PPA which was contributing to 37% of Station export capacity got expired in June-20 which has significantly affect performance in terms of Efficiency & Profitability due to absence of new market opportunity
PPA Expiry
Plant PLF is getting affected due to Coal Quality & Quantity Constraint & same is affecting station Performance
Coal Issue
Impact of Machine aging on Plant Performance
Machine Aging
FGD installation will result in increase in plant Auxiliary Power Consumption
Increase in APC due to FGD
Fund availability major constraint for Technological Upgradation
Fund Availability
Increase in worldwide Renewable Energy portfolio is necessity for tackling Climate change issues but same may affect Plant PLF which will effect performance
Increase in Renewable Energy Portfolio
14. Team work, Employee Involvement & Monitoring
39
15.1 Implementation of ISO 50001
15. Implementation of ISO 50001 at GWEL
Setting Clear Energy Objectives & Targets
Formation of Energy Management Cell
Monitoring-Measurement-Analysis of Significant energy
use & consumption by Equipment’s/
Processes
Generation of Daily Energy Deviation
Generation of Non-Conformities
Corrective and Preventive Actions
Internal & External Energy Audits
Management of Energy Conservation
Programmes
Reviews at various levels and frequencies
Sustenance of Results
Integration of Energy Conservation to GWEL Objectives & Targets Monitoring through Daily Energy Deviation Report & Deviation
Closure by CAPA Closure Mechanism
40
15.2 GWEL – Management of Energy Conservation Program
SAP Z5 Notification for Implementation of Energy
Conservation Project
Identification
• Identification through Internal/ External Audits, RCA or CAPA for
Energy deviations etc.
•Energy Conservation Plan(EC Plan) raising & Approval
•Notification in SAP- Z5 category for approval of MA & Head-O&M
Implementation
•EC Plan Implementation Plan is Reviewed & Approved by
Steering committee headed by Plant Head
Completion
•Post Completion of EC Plan, Completion along with
Benefits will be certified by the Steering committee
Effectiveness
•Actual savings achieved to be furnished against expected
after 1 month of project completion.
•Status of EC plans will be monitored on Weekly/ Monthly
reviews.
15. Implementation of ISO 50001 at GWEL
Total 160 Energy Conservation SIP’s implemented in last 6 FY’s. Digitalization-Journey of Project Implementation
Identification Implementation Completion Effectiveness
41
16. Long Term Vision on EE
16.1 Long Term Target of Energy Efficiency
GWEL is committed to become the Most Energy Efficient Utility in the World
Our vision is to make use of all form of energy resources most efficiently, minimize the impact of our operationson Environment & conserve the Scarce Natural Resources
For that at GWEL we follow following Practices
Setting of Energy Objectives & Targets
Efficient Management and Usage of Energy
Adoption of Best Practices & Innovative Technologies
Internal & External Energy Audits & implementation of Improvement measures
Compliance with all legal requirements
Training & Knowledge sharing to raise awareness
Technological Upgradation
• Flexibility of inclusion ofNew Technologies inExisting System
Financial Support
• Availability of Pay Outof Saving Facility foradoption of NewTechnologies
Supplier Engagement
• Active Involvement ofSuppliers in GWELsGreen Supply ChainManagement
Challenges- Most Energy Efficient Utility
42
17. Awards & Accolades
BEE-National Energy Conservation Award-2017 CII National Award for Excellence in Energy Management-2018 & 2019
13th State Level Award for Excellence in Energy Conservation & Management by MEDA for the year 2018
IMC Ramkrishna Bajaj National Quality Award2017
Global Performance Excellence Award 2018-World Class BSC 5 Star 2019Sword of Honour 2019
Best Boiler Award 2019
Quality Circle Award
43
18. Learnings from CII/Other Award Program
To learn about the best practices adopted from best performing companies.
Facilitate adoption of similar projects at our unit, leading to enormous saving viz.
Intelligent Flow Controller
Airtron AC Energy Saver
An Opportunity to interact & network with individuals and companies of repute for further strengthening
Energy Efficiency System
Information about Latest market trends & innovative products for Energy Efficiency .
To identify strengths and opportunities to excel, based on a comprehensive and rigorous assessment by
experts.
18. Learning from CII/Other Award Program
44
19. Major Achievements
19. Completion of Capital Over-hauling in Record 37 Days
COH is an essential activity for Equipment up-keepment & usually carried once in 5 year or as per running condition
As per industry-wide practice, complete Over-haul activity for a Chinese unit takes approx. 45 days from Unit Shutdown to Sync
This contributes to approx. 12% of availability loss & hence major loss of revenue
From Past few years, GWEL was already facing availability & revenue loss due to Coal Shortage, hence it was essential to
maximize our availability as COH was also due for Performance improvement
Hence, GWEL took this as a Challenge to reduce COH timing without compromising to equipment maintenance
Cross Functional Team was formed & detailed study was carried out for identification of OFIs
Action Plan Result
Critical path for major time
consuming activities
Four major time consuming activities
identified
Previous overhaul repetitive jobs 2 Repetitive Jobs Identified
Activities which can be eliminated 1 Activity identified for Elimination
Parallel activities 3 Activities identified for Paralleling
New maintenance practices 3 New Maintenance Practices
identified
Other Plant site visits during their
overhauling
Best Practices from other plant
Turbine Cooling Time Reduction-
Major time consuming activity
Reduction by 4.2 Days by On-load &
Off-load cooling methodology- First
time for any Chinese unit
U-1 COH Completed in Record 37 days with
Zero Safety incidence
100% Completion of Planned Activities
Achieved Desired Result
Unit Heat Rate Improvement-47 Kcal/Kwh
APC Improvement – 0.2%
45
Team Member Details:
1. Mr. Mreenal Sharma -Manager - 8390903673 [email protected]
2. Mr. Edwin Williams S -Associate Manager - 8390903673 [email protected]
3. Ms. Pratiksha K Sharma -Manager - 8380098446 [email protected]