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Trouble shooting issues Some case studies
DIPPT – Di iso propyl phenoxy thiourea
NH
O
C
S
NH2
1-(2,6-diisopropyl-4-phenoxyphenyl)thiourea
Stage III
Reaction scheme
NH2
Br2,Conc.HCl
Chloro benzene
NH2
2,6 DIPA 2,6 DIPBA.HBr
(Bromination)
HBr
OH KOH,CuCO3
Br
( Bromo compound + Phenol Ether)
NH2
O
+ KBr + H20
2,6 DIPPA
NaSCN
Conc.HCl
NH
O
C
S
NH2
(Aniline to Thiourea)
2,6 DIPPT
+
NaCl
92%
76%
63%
Raw MaterialsStage IRaw materials Equ
2,6 DIPA 1.00 Conc.HCl 1.25 Bromine 1.10
Stage II
Raw materials Equ
Stage I 1.00 48% Caustic lye 1.20 Phenol 1.50 KOH(88%) 1.45 CuCO3 0.027
Stage III
Raw materials Equ
Stage II 1.00Conc.HCl 1.15NaSCN 1.20
Brief processStage I
Azetropic distillation of water Temperature - 100 - 1050 c
Addition of Conc. HCl (1. 25 equ) Temp - 30-400c
RM charging2,6 DIPA + Chloro benzene
Addition of Bromine (1.10 equ) Temp -600 c , Maintenance - 3 hrs
IPC Check complies
Cool to 50c and filtered, HPLC purity > 99 %, Yield – 92 %
N2 purging to remove excess bromine at 600 c
Stage II
Distillation of water Toluene layer + 88% KOH (1.45 equ) + Phenol (1.50 equ) Temp - 1100c
Neutralisation of HBr2,6 DIPA. HBr (Stage I) + 48% caustic lye (1.20 equ) Temp - RT
Distillation of toluene and DMF charging Temperature- 150-1550c
Toluene extraction
CUCO3 (0.027 equ) charging Temp - 150-1550c Maintenance – until IPC complies
Vacuum distillation of DMF Temp - 700c
Workup
Addition of Water , Dil. KOH solution Temp - 700c , pH > 12
Xylene charging at 700c
Hyflow Filtration & Layer separation Temp - 700c
Stage II in xylene HPLC purity – Stage II – 93%, Stage I – 1% , 2,6 DIPA – 3% Yield – 76%
Stage III RM charging
(Stage II in xylene) + NaSCN (1.20 equ)
Addition of Conc. HCl (1.15 equ) Temp – 95-100 0c
Distillation of water and maintenance Temp – 100-105 0c
IPC Check complies
Vacuum Distillation of water traces Temp - 70 0c
Cool to 200c and filtered, HPLC purity >98% Yield – 63%
Issue formed
Ist batch
Operational issues like raw material handling, utility issues observed
Stage I, II, III material isolated with expected yield and purity
II nd batch
Operational issues rectified
Stage II material isolated with unknown impurities ( ~ 3 - 4%) and not able to eliminate
Stage III material also failed in purity due to unknown impurities ( ~ 3 - 4%) and purification trials failured
Way Forward – Operational issues to be rectified
Impurity Identified
The LCMS analysis confirms the impurity was N-haloamine of Stage I (DIPBA) and stage II (DIPPA).
NHBr
Br
N ,4-dibromo-2,6-diisopropylaniline
NHBr
O
N -bromo-2,6-diisopropyl-4-phenoxyaniline
Route cause
The free bromine (Br2) present in the stage I was the major source for the impurities formation.
1.Reaction of Sodium hypobromite with amine (in stage II – HBr neutralisation)
2 NaOH + Br2 NaBr + NaOBr1.
2. NaOBr + RNH2 + H2O RNHBr +NaOH + H2O
+ H2O
2. Reaction of Hypobromous acid with amine (in stage II – HBr neutralisation)1. Br2 + H2O HOBr
2. HOBr + RNH2 RNHBr + H2O
+ HBr
Corrective action ( Quenching of free bromine)
1.The free bromine trapped in the stage I wet cake was quenched by treating with Sodium bisulfite solution ( introduced in stage I isolation)Br2 + 3NaHSO3 2NaBr + NaHSO4 + H2O + 2 SO2
2.The Bromine free stage I then treated with 48% caustic lye in stage II process to neutralise the trapped HBr
HBr + NaOH NaBr + H2O
The Impurities formed in 2nd batch and not in first batch – why ?.
In the Ist batch, due to lot of issues in utility operations and raw material (Br2) handling the certain quantity of bromine was liberated and not trapped in the stage I .
Therefore there is no purity issues observed.
In the second batch, the operational issues are rectified. Due to that stage I material was trapped with Bromine and this free bromineleads to the formation of above described impurities.
Preventive actionThe Bromine equivalent was reduced form 1.10 to 1.05 which was sufficient for the reaction completion.
Conclusion
The importance of negative experiments and the exact workup process was clearly evident from the above issue.
Key person
Who identified & corrected the issue
Dr G.V .Raj , Former Director & Board member - NACL
EL2- LSN 2779699
O
O O
tert-butyl 3-methoxy-2-propylbenzoate
HO
O OH
3-hydroxy-2-propylbenzoic acid
Stage II Stage III
Reaction scheme
OO
O O
2,3-Dimethoxy benzoic acid
tertiary butyl ester
O
O O
n-PrMgCl,
HO
O OH
3-hydroxy-2-propylbenzoic acid
48%HBr,CH3COOH
(Methoxy to propyl)
( Methoxy to hydroxy)
THF
95 - 98 %
82 - 87%
tert-butyl 3-methoxy-2-propylbenzoate
( Ester to Acid )
Raw MaterialsStage II
Raw materials Equ
2,3 Dimethoxy benzoic acid tertiary butyl ester (Stage I) 1 .00 n-PrMgCl 1.20THF 4.56VAcetic acid 1.30
Stage IIIRaw materials Equ
Stage II 1 .0048% HBr 7.28Acetic acid 15.93
Brief processStage II
RM chargingStage I + THF
Addition of n-PrMgCl (1. 20 equ) Temp - - 25 to - 300c Time – 2 hrs
Maintenance Temp - - 15 to -200c
Time - 2hrs
IPC Check complies
Addition of Acetic acid (1. 30 equ) Temp - - 15 to - 200c Time – 1 hr
Workup Addition of water
Temp - 25 to 300c Time – 30 mins
Charging of MTBETemp - 25 to 300c Layer
separation Back extraction of Aqu. layer
with MTBETemp - 25 to 300c
Water wash and brine solution wash of org. layerTemp - 25 to 300c Vacuum distn of org.layer
Temp - 45 to 500cHPLC purity – 90 to 95 %
Yield – 95 - 98%
Stage III RM chargingStage II + Acetic acid ( 15.93
equ)
Addition of 48% HBr( 7.28 equ) Temp - - 25 to - 280c Time – 20 mins
Maintenance Temp - 115 to 1200c
Time – 22 – 24 hrs
IPC Check complies
Addition of water and MTBETemp - 25 to 300c
Time – 30 mins
Workup
Layer separation
Back extraction of Aqu. layer
with MTBETemp - 25 to 300c
Water wash and brine solution wash of org. layer Temp - 25 to 300c
Vacuum distn of org.layerTemp - 45 to 500c
Chasing with n-Hexane
Temp - 45 to 500c Charging of n – Hexane at RT
Cool to 50c and filtered, HPLC purity > 98 %,Yield – 82 – 87%
Issue formedLab batch
No issues observed in yield & purity of stage II reaction in lab trails
Plant batchIn stage II reaction the un reactive Stage I - ~ 7% in IPC and isolated product also (Limit – NMT – 0.50 % )
The stage II plant material (which contains ~ 7% of stage I ) converted in to stage II in lab with good yield & purity by adding excess n-PrMgCl in THF
When the same concept repeated in plant the reaction was not proceeding and material failed in purity with ~ 5% of stage I (Limit – NMT – 0.50 % )
The stage II Plant material (5% stage I content) converted in to stage III . Isolated material failured in purity due to ~ 5 % un known impurity content
The failured stage II material converted in to stage III and endup with ~ 5% of un known impurity in the isolated material
Impurity identified
The LCMS analysis confirms the impurity was 2,3 di hydroxy benzoic acid
HO
HO
O OH
2,3-dihydroxybenzoic acid
Route cause
It formed from the ~ 5% stage I (in stage II material) reacted with48% HBr in acetic acid in stage III reaction
O
O
O O
Stage I
tert-butyl 2,3-dimethoxybenzoate
48%HBr
CH3COOH
HO
HO
O OH
2,3-dihydroxybenzoic acid
Corrective action ( pH variation)
The same thing repeated in plant and desired result obtained.
In lab, Stage III of plant material treated with dil.caustic solution up to pH>12 in chilled condition to make it as sodium salt
The clear solution filtered through hyflow bed
The basified aqu.layer treated with dil.HCl at chilled condition up to pH - 5 Extracted with toluene
and stage III material isolated with passing quality
The impurity separated by further dil.HCl addition to aqu.layer up to pH - 2
The issue developed in plant batches only and not in lab trials - why?
For the project, the raw material n-PrMgCl received from the same manufacturer in two different packs (i) ~ 1kg for lab trials (ii) ~ 50 kg for plant batches.
For the lab trials the corresponding 1kg pack material only used. There is no issue in the reactivity of lab material.
The 50 kg pack material never used for lab trials and its reactivity never checked. So when it is used for plant batches , due to its poor reactivity ( poor purity) the reaction not proceeding well.
Preventive actionDue to this problem, commercial n-PrMgCl procured freshly and itsreactivity confirmed by IUT trials in lab. The remaining batches conducted withfresh commercial n-PrMgCl and no issues observed in yield and purity of stage II.
Conclusion
1.The importance of IUT trials for commercial raw materials was evident.
2. In process development ,negative experiments must be done to avoid this kind of issues.
Key person
Who identified & corrected the issue
Mr P. Satya Narayanan – Former GL, PHC, Ennore
Isouron
O
N
NH
C
O
NCH3
CH3
3-(5-tert-butylisoxazol-3-yl)-1,1-dimethylurea
Reaction scheme
O
N
CONH2
NaOCl,(C4H9)4NBr
(C4H9)4NCl,Tolune
O
N
NCO(Amide to isocyanate)
(CH3)2NH
(Isocyanate to urea)
O
N
NH C
O
NCH3H3C
(Isouron)
60 - 65%
5-isopropylisoxazole-3-carboxamide
3-(5-tert-butylisoxazol-3-yl)-1,1-dimethylurea
Raw Materials
Raw materials Equ
Carboxamide - 1.00 NaOCl - 1.00 TBAB - 0.04TBACl - 1.00Dimethyl amine - 1.10
Brief process RM charging
14% Aqu. NaOCl solution (1.00 equ)
Lot wise addition of Carboxamide Temp – 15 0c Time – 1 hr
Maintenance Time – 2 hrs Temp - 15 0c
Addition of TBAB (0.04 Equ) ,TBACl ( 1.00 equ) Temp – 15 0c
Maintenance Time – 30 mins
Temp - 15 0c Toluene charging
Temp – 15 0cAqu. Layer separation
Dimethyl amine gas purging in autoclave Temp - 700c, Time – 3 hrs, Pressure – 2 Kg
Work upN2 purging to remove excess DMA at 700c
Water wash of toluene layer Temp - RT
Dil.HCl (3%) wash at RT
Dil. NaOH (5%) wash @ RT
Water wash of toluene layer Temp - RT
Vacuum distillation of toluene Temp - 45 - 550c
Addition of waterTime – 60 mins
Temp – 45 -55 0c
Cool to 50c and filtered HPLC purity > 97 %, Yield – 60- 65 %
Issue formedLab batch Scale up batch
No issues observed in yield & purity in lab trails
No issues observed in yield
One particular known impurity formed more ( 1 % against the limit of 0.50% ) and material failed in specification
Impurity identified The LCMS analysis confirms the impurity was mono methylated product of Isouron.
O
N
NH
C
O
NHCH3
1-(5-tert-butylisoxazol-3-yl)-3-methylurea
Route causeFrom the lab trials over look , it was confirmed that the more quantity of NaOCl used (instead of 1.00 equ , 1.05 equ used) leads to the impurity formation more in that particular scale up batch.
This happens due to some manual error in calculation and weighing.
Relation between excess NaOCl and particular impurity
Possible Mechanism (Hoffman rearrangement)
R C
O
NH2NaOCl R C
ON
H
Cl(i)
N-Chloro amide
(ii) R CO
N
H
Cl
N-Chloro amideR C
ON Cl
NaOH
NaOHH2O Na
(iii) R CO
N Cl N (C4H9)4 Cl R CO
NN (C4H9)4
Cl
R CO
NN (C4H9)4
Cl(iv) R C
O
N N (C4H9)4 Cl
NaCl
R N C O
(v) R N C O NHCH3
CH3R NH
O
N CH3H3C
Preventive actionThe excess NaOCl leads to the formation of impurity (mono methylatedProduct) was confirmed by done some more negative experiments. In all the cases the same result obtained.
Conclusion
Before the scale up batches the negative experiments should be done and data to be generated.
Acetic anhydride
CH3
O
O
O
H3C
Reaction scheme
H3C C
O
OH7000C
Under vacuumH2C C O H2O
Ketene1.
2. H2C C O H3C C
O
OH600c
CH3
O
O
O
H3C
88%
99%
Brief process The crude acetic acid (88%) was cracked under vacuum at 7000c in the furnace to produce ketene gas.
Ketene gas reacted with glacial acetic acid (99%) at 600c to form crude acetic anhydride (88 % of anhydride + 12% of acetic acid)
Continuous process
The crude acetic anhydride (88%) was purified to > 99% by atmospheric distillation
Batch process
Checking controlCrude acetic anhydride purity – online checking
Mixing the 25 ml of fresh sample + 25 ml of calcium chloride solution in stoppered measuring jar and shaked well.
After settling for 2-3 minutes the layers separated with definite values . Based on the values acetic anhydride content in the sample confirmed with standard chart
The pure acetic anhydride was checked by GC
Issue formedThe crude acetic anhydride plant operation was disturbed by heavy vacuum fluctuations
Column flooding i.e. non consistent vapor flow due to choke in the lines was suspected . The problem continued for 5 hours
After 5 hrs , when the crude acetic anhydride content checked by online sample it shows complete absence of acetic anhydride and only acetic acid present
The Dip level in production tank confirms ~ 1500 kgs of acetic anhydride converted in to acetic acid. Production stopped and plant was under shut down
Route causeBy visual inspection it was confirmed that the absorption tower temp ( where ketene gas reacted with acetic acid to form acetic anhydride at 600c ) reached 900c.
By checking the absorption tower it was confirmed that the condenser leak happened. Due to that water entered in to the system.
There by temperature raised from 60 to 900c and also the formed acetic anhydride converted in to acetic acid.
Why the root cause was not immediately identified ?
1. The online sample check for the acetic anhydride content was not done for 5hrs (to be checked for every one hr) due to the concentration focused on suspected column flooding only.
2. The absorption tower temperature scanner in the PLC system panel board not working properly i.e. it indicates the temperature around 600c by constant instead of the actual temperature (900c).
Conclusion1. Doing the basic things on constant basis particularly during the critical times was very important.
2. Doing the physical examination i.e visual checking was much more required especially during trouble shooting. Don’t rely on systems blindly.