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Use of trolley Loca&on: Agro Engineering Works, Butwal-12, Rupandehi Process: Fabrica&on Before Operators used to throw work items items on the floor a7er drilling, grinding and other machining opera;ons. Another person had addi;onally collect those items for the next process. ACer Work items a7er drilling, grinding and other machining opera;ons are now directly placed on trolley (wheelbarrow). This is then easily taken to next process step. Costs/benefits Cost: NPR 70,000 Annual manpower saving: 150 man-days Savings: NPR 120,000 Payback: 7 months Contact: Dr M Balakrishnan [email protected] Mr Amar Manandhar [email protected] Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

Use of trolley news/METABUILD... · Use of trolley Locaon: Agro Engineering Works, Butwal-12, Rupandehi Process: Fabrica&on Before Operators used to throw work items items on the

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UseoftrolleyLoca&on: AgroEngineeringWorks,Butwal-12,RupandehiProcess: Fabrica&on

BeforeOperatorsusedtothrowworkitemsitemsonthefloora7erdrilling,grindingandothermachiningopera;ons.Anotherpersonhadaddi;onallycollectthoseitemsforthenextprocess.

ACerWorkitemsa7erdrilling,grindingandothermachiningopera;onsarenowdirectlyplacedontrolley(wheelbarrow).Thisistheneasilytakentonextprocessstep.

Costs/benefitsCost:NPR70,000Annualmanpowersaving:150man-daysSavings:NPR120,000Payback:7months

Contact: [email protected]@seednepal.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

SwitchoffWeldingMachineswhennotinuseLoca&on: OshinPowerServicePvt.Ltd.,Butwal,RupandehiProcess: Fabrica&on

BeforeThreeweldingmachinesontheshopfloorwereinopera9on.Theseweregenerallynotturnedoffwhennotinproduc9one.g.duringlunchbreak,orinbetweenjobs.Stand-bypower(loss)wasmeasuredtobe1.2kW

A@erAFerawarenesssessionforshopfloorteam;weldingoperatorsareawareoflossfromidlerunningweldingmachinesandtheworkshopsupervisornowswitchesoffthepowerlinetoworkshopduringlunchbreaktostopidlerunningofweldingmachines

Costs/benefitsCost:Nocost Annualelectricitysavings:540kWhAnnualsavings:NPR5,400 Payback:Immediate

Contact: [email protected]@seednepal.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

Energy Savings by insulating the curing tank

Location: Pioneer Electrocables, Biratnagar, Nepal

Process: Electrical Cable Manufacturing

Before

Two curing tanks with 16 kW electric heaters in each tanks are installed for curing of electrical cables. The tanks were not insulated and operation time was 6 hours consuming 192 kWh per batch.

After

Both tanks were insulated with glass wool and protected with metal cladding due to which operation time is reduced to 4 hours now consuming only 128 kWh per batch.

Costs/benefits

Cost: NPR 30,000 Annual savings: NPR 102,400

Payback: 3.5 months (160 batches/yr * 64 kWh/batch = 10240 kWh/yr)

Contact: Dr M Balakrishnan [email protected] Mr Amar B Manandhar [email protected]

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflecting the position of the European Union.

Improvedworkingcondi0ons-be4erillumina0onLoca&on: PioneerElectrocables,Biratnagar,NepalProcess: ElectricalCableManufacturing

BeforeLightswereplacedhighinceilingprovidinglowerillumina0onatworkingarea.

A<erHeightofsomelightsisreducedbysimplysuspendingthesefromchains.Halvingtheheightincreasesillumina1onby41mes!Over0me,remaininglightswillbeloweredtoprovideworkplaceillumina0on.

Costs/benefitsCost:NillAnnualsavings:Be4erworkingcondi0on,

increaseproduc0vityPayback:Immediate

Contact: DrMBalakrishnanmalini@metabuild-southasia.orgMrAmarBManandharamar@metabuild-southasia.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

Installa(onoftranslucentsheets

Loca&on: OshinPowerServicePvt.Ltd.,Butwal,RupandehiProcess: Ligh&ng

BeforeNaturallightwasnotfullyu(lisedattheworkplace.Someareaswereilluminatedbyusingfluorescentlampseveninday(me.

A?erIndustryhasinstalledtwotranslucentsheetsontheroof.Theworkplaceiswellilluminatedbynaturallightandnowthereisnoneedtousethreefluorescentlampsduringtheday.

Costs/benefitsCost:NPR2,200 Annualelectricitysaving346kWhAnnualsavings:NPR3,460 Payback:8months

Contact: [email protected]@seednepal.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

RepairofCapacitorBankLoca&on: AgroEngineeringWorks,Butwal,RupandehiProcess: PowerFactorImprovement

BeforeOutofthenineinstalledcapacitors(of15kVArra;ngeach)incapacitorbank,fourwerenotfunc;oning;onewasdamaged,twowerehavingproblemwithcontactorandthefourthonewasmalfunc;oning.Therecordedpowerfactorwasonly0.88

ABerOnecapacitorisrepaired,connectorsoftwocapacitorsarerepaired,MCBforconnec;onofoncecapacitorisrepairedandonecapacitorisreplaced.Averagepowerfactorisimprovedto0.99

Costs/benefitsCost:NPR10,000 Demandreduc;on:10.5kVA/monthAnnualsavings:NPR31,500 Payback:4months

Contact: [email protected]@seednepal.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

PowerFactorImprovementLoca1on: InterTechPvt.Ltd.,Butwal-12,RupandehiProcess: Fabrica1onandGalvanizing

Before Grid supply to the industry had poor power factor. The recorded average power factor was 0.48

AFerThecompanyhasinstalledanAutoma3cPowerFactorController(APFC)of98kVArra3nginlinewiththemainpanel.Nowthecompanyismaintainingpowerfactorof0.99

Costs/benefitsCostforAPFCinstalla3on:NPR150,000Reduc3onofdemandcharge:31kVA/monthAnnualsaving:NPR93,000/year Payback:1.7years

Contact: [email protected]@seednepal.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

Improvementininsula0onofsteampipelinesLoca&on: HulasWireIndustries,Biratnagar,NepalProcess: Surfacetreatment

BeforeInsula0oninthesteampipelineswasdamagedleadingtoheatlossandhigherfuelconsump0on.Thesurfacetemperatureofsteampipewas55°Ccontribu0ngtoheatlossofaround16,000kCal/hr.Addi0onally,processtankwithfluxsolu0oncouldnotaGaindesiredtemperature(couldreachonlyaround66°C)fromsuppliedsteam.

A>erThepipelineisinsulatedwithglasswoolandcoveredwithjutesacktoreducesteampipetemperatureto35°Candcorrespondingheatlossreducedtoaround6,000kCal/hr.Withlesseropera0ng0me,85°Ctemperatureoffluxsolu0onisnowaGained.

Costs/benefitsCost:NPR30,000Annualsavings:NPR209,000Payback:1.7months (5264litresofFOi.e.,~3%)

Contact: DrMBalakrishnanmalini@metabuild-southasia.orgMrAmarBManandharamar@metabuild-southasia.org

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflec@ng the posi@on of the European Union.

Fuel Savings by reducing the Furnace opening

Location: Pashupati Iron & Steel, Biratnagar, Nepal

Process: Rerolling Mill

Before

The company is using furnace oil (FO) fired furnace to heat the billet before rerolling it to make TMT bars. The opening of the feeding door in the furnace was 15 cm contributing to 1,056 kCal of heat loss per hour

After

The height of door is lowered by 7.5 cm by manually setting the door hangers to minimize heat loss

Costs/benefits

Cost: Nil Annual savings: NPR 21,440

Payback: Immediate (536 kg of Furnace oil)

Contact: Dr M Balakrishnan [email protected] Mr Amar B Manandhar [email protected]

Disclaimer: This document has been produced with the financial assistance of the European Union. The contents of this document are the sole responsibility of TERI and can under no circumstances be regarded as reflecting the position of the European Union.