2
Orbit First Quarter 1999 11 moco Exploration and Production’s Painter NGL /NRU Com ple x Ga s Processing Plant is located 10½ miles northea st of Evan ston, Wyom ing. Average daily throughput is approxi- mately 7.4 million cubic metres (260 million cubic feet) of natural gas, com- pose d of 800 ba rrels of conde nsa te, 8,000 to 14,000 ba rrels (depe nding on the operating mode) of natural gas liq- uids, 3.4 million cubic metres (120 mil- lion cubic feet) of hydrocarbon gas, and 3.4 million cubic metres (120 mil- lion cubic feet) of nitrogen. Current installation Painte r use s Bently Ne vad a 33 00/80 Six-Channel Rod Drop Monitors on three Hea t Pum ps an d four Residue Gas Compressors, a total of 44 cylinders.  Th e Ro d Drop Monitors are all pro- gramm ed for Average Rod Position. Twice a we ek, the Mecha nical Mai ntena nce depa r t- ment collects Rod Drop Monitor display values from ma chine s on its Processing Rep orting I nform a tion by Marlin Barnes Vibration Specialist Predict Team Painter Operation Center Amoco Exploration and Production e-ma il: ma rlin_ o_barne s@am oco.com Data Entry (PRI DE) route . Me cha nical Maintena nce a nd Predict Tea ms then analyze this information.  Th e Ben t ly Ne v ada 3300 S y s t em Monitor ha s a Dyna m ic Dat a Inte rface (DDI ) Comm unication Proce sso r option. The racks are connected togeth- er and are, in turn, connected via RS- 422 to a Dell Pen tium I I compu te r run - ning Ben tly Ne vad a’s Data Man ag er ® 2000 for Windows NT Software. This system provide s red und an t moni tori ng an d trending of the rod drop m onitor data. Case History Using a Rod Drop Monitor to prevent cylinder and piston/rod repair Figure 1. Cross section of Heat Pump Compressor. Amoco Ex ploration and Production’s Painter NGL/NR U Comple x Gas Processing Plant.

USING ROD DROP MONITOR TO PREVENT CYLINER AND PISTON~ROD REPAIR

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Orbit First Quarter 1999 11

moco Exploration and

Production’s PainterNGL/NRU Complex Gas

Processing Plant is located 10½ miles

northeast of Evanston, Wyoming.

Average daily throughput is approxi-

mately 7.4 million cubic metres (260

million cubic feet) of natural gas, com-

posed of 800 barrels of condensate,

8,000 to 14,000 barrels (depending on

the operating mode) of natural gas liq-

uids, 3.4 million cubic metres (120 mil-lion cubic feet) of hydrocarbon gas,

and 3.4 million cubic metres (120 mil-

lion cubic feet) of nitrogen.

Current installation

Painter uses Bently Nevada 3300/80

Six-Channel Rod Drop Monitors on

three Heat Pumps and four Residue

Gas Compressors, a

total of 44 cylinders.

 The Rod Drop

Monitors are all pro-

grammed for Average

Rod Position. Twice a

week, the Mechanical

Maintenance depart-

ment collects Rod

Drop Monitor display

values from machines

on its Processing

Reporting Information

by Marlin Barnes

Vibration Specialist

Predict Team

Painter Operation Center

Amoco Exploration and Production

e-mail: [email protected]

Data Entry (PRIDE) route. Mechanical

Maintenance and Predict Teams then

analyze this information.

 The Bently Nevada 3300 System

Monitor has a Dynamic Data Interface

(DDI) Communication Processor

option. The racks are connected togeth-

er and are, in turn, connected via RS-

422 to a Dell Pentium II computer run-

ning Bently Nevada’s Data Manager®

2000 for Windows NT Software. This

system provides redundant monitoring

and trending of the rod drop monitor

data.

Case History

Using a Rod Drop Monitor to

prevent cylinder and piston/rod repair

Figure 1. Cross section of Heat Pump Compressor.

Amoco Exploration and Production’s Painter NGL/NRU Comple x Gas Processing Plant.

Page 2: USING ROD DROP MONITOR TO PREVENT CYLINER AND PISTON~ROD REPAIR

8/12/2019 USING ROD DROP MONITOR TO PREVENT CYLINER AND PISTON~ROD REPAIR

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12 Orbit First Quarter 1999

Avoiding cylinder

and piston/rod repair

 There have been several instances

where use of this data has prevented an

expensive cylinder and piston/rod

repair, while maximizing the runtime of 

the piston rider bands. The #1 cylinder

on the #1 Heat Pump is one such exam-

ple. On May 16, 1996, during preven-

tive maintenance of the compressor, thepiston-to-cylinder liner clearance was

1.9 mm (0.075 inch). On April 11, 1997

during a partial plant shutdown, the pis-

ton-to-liner clearance had decreased to

1.6 mm (0.063 inch). Figure 2A shows

a Rod Drop Monitor reading change of 

approximately 0.31 mm (0.012 inch)

during this time period. The monitor

channel was “hot zeroed,” and new

alarm setpoints were entered.

 The cylinder #1 channel went into

“Alert” alarm in late December 1997.

On January 16, 1998, the piston-to-

liner clearance was checked through a

head end discharge valve port and was

1.40 mm (0.055 inch). Figure 2B

shows additional data from the PRIDE

route, which indicates a 0.69 mm

(0.027 inch) change. A review of the

data suggested the discrepancy was

probably due to the difficulty of mak-

ing measurements through the dis-

charge port. The monitor was hot

zeroed again and alarm setpoints were

entered, based on the new clearance.

 The Rod Drop Monitor channel for

the #1 cylinder went into “Alert” alarm

again in early May 1998. A work order

was written for another measurement

of piston-to-liner clearance. The com-pressor was removed from service on

 June 4, 1998, and the piston-to-liner

clearance was again checked through a

head end discharge port. This time the

clearance was 0.38 mm (0.015 inch).

Figure 2C shows a 0.53 mm (0.021

inch) change during this period.

Conclusions

Getting a precise measurement of pis-ton-to-liner clearance through the dis-

charge valve port is difficult under the

best of circumstances. Although one of 

the measurements was radically differ-

ent, the total change in piston-to-liner

clearance between May 16, 1996 and

 June 4, 1998, 1.52 mm (0.060 inch),

agreed with the PRIDE route Rod Drop

Monitor readings during this same peri-

od. The plots presented a clear trend of 

wear that could be used to pre-

dict wear rates and the effects

of modifications to the process,

lubrication, etc. Proper installa-

tion of the monitor system and

confirmation of its operation is

very important, though.

Confidence in the system must

be established before it can be

used effectively.

 The compressor was out-of-

service for eight hours; the total

cost of the repair parts, labor,

and production loss was

$10,600. If the piston had con-

tacted the cylinder liner enough

to require liner replacement and

piston/piston rod repair, a conservative

estimate of the repair cost/production

loss would be $54,000.

Postscript: Based on PRIDE data rod

drop trend and Data Manager rod drop

trend of the #4 cylinder on the #4

Residue Gas Compressor, Painter

Operations and Maintenance supervi-

sors were advised on June 29,1998 that

the piston-to-liner clearance needed to

be checked. Hydrocarbon gas sales

nominations were changed to reflect

the necessary reduction of inlet gas

rates and downtime was scheduled for

checking piston-to-liner clearance.

Clearance was measured through a

head end discharge valve port on July

1. Clearance was found to be within

0.013 mm (0.005 inch) of the recom-

mended minimum. Since the machine

was down and cold, and nominations

reflected the unit being out of service

all day, the piston rings and rider bands

were replaced. Painter Operations and

Maintenance considered this another

save. Cylinder liner, piston, and piston

rod repair and unplanned production

loss were again avoided.

Figure 2.

Average Rod Drop, Heat Pump #1, Cylinder 1.