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18th National Award For Excellence In Energy Management-2017
CAPTIVE POWER PLANT (9x135 MW)
VEDANTA LIMITED, JHARSUGUDA
GROUP PHILOSOPHY
Entrepreneurship
Innovation
Excellence
Integrity
Respect
Trust
Care
Core Purpose “Vedanta is a globally diversified
natural resources company with low
cost operations. We empower our
people to drive excellence and
innovation to create value for our
stakeholders. We demonstrate world-
class standards of governance, safety,
sustainability & social responsibility”
IMPLEMENTATION OF MANAGEMENT SYSTEMS
• Quality management ISO 9001:2008
• Environment management ISO 14001:2004
• Energy management ISO 50001:2011
• Asset Management ISO 55001:2014
• Occupational Health and safety management
OHSAS 18001:2007
• Par-Excellence by QCFI 5S
Installation of CAAQMS for continuous air quality monitoring
Biomedical Deep burial
pit
High Concentration
Slurry Disposal
(HCSD) -1st In Odisha
Co –Combustion
of Anode Butt in CPP with
due permission from CPCB
Real Time Data
Acquisition system
Weather monitoring station with solar panels
ENVIRONMENTAL PROJECTS
CARBON FOOT PRINT ACTIVITIES
Year Scope 1 emissions
CO2e (MT) Scope 2 emissions
CO2e (MT) Scope 3 emissions
CO2e (MT) CO2e MT Mitigation*
2013 - 14 9760105 2484 102634 9865223 Baseline Year
2014 - 15 9986049 27,134 117,702 9986193
2015 - 16 10568356 8,403 321,478 10568685
2016 - 17 15098803 45942 399815 15544560
2017 - 18 5% reduction 5% reduction 5% reduction 5% reduction
Efforts towards GHG emission reduction: Adoption of new technology. Stepping in towards renewable energy sources. Creating awareness among employees and stakeholders. Reduction in no. of light vehicle by 50%. Vehicle with aging less than 3 years only allowed &
ensuring PUC certificate for every vehicle. Increasing the loadability in transportation to reduce carbon emission.
Source: AT Kearney Report
BENCHMARKING
1.90%
1.20%
3% 2.9%
0.00%
0.50%
1.00%
1.50%
2.00%
2.50%
3.00%
3.50%
Player 2International
Player 1National
Player 3 National
JSG 1215 Actual
Δ SHR value - JSG 1215 (% of Design SHR)
8% 9.08% 9.50% 9.68%
0%
2%
4%
6%
8%
10%
12%
Player 1International
Player 2National
Player 3 National
JSG 1215 Actual
APC Value - JSG 1215 (% of generation)
Unit : gms/Kwh
Design : 789
Units in
Commissioning
Stage
REDUCTION IN SEC
a) Commissioning of Ultra
filtration
b) Turbine Overhauling
c) Replacements of Turbine
Drain Valves
d) Operational Improvements
a) CT fills design modification
b) HFO to LDO gun conversion.
c) APH O/H, Soft Touch Seals Installation & Basket
design modification.
d) Turbine Seal Checking & Rectification
e) Condenser Cleaning
f) Operational Improvements
g) FGET temp reduction.
2730 2679 2463 2442 2418 2442 2421 2451 2400
2009-10 2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17 Target 17-18
STATION HEAT RATE (Kcal/kwhr) PG test Value : 2400
REDUCTION IN SEC
Benchmarking : 2.00
a) Zero Discharge.
b) Improvement of COC
c ) Recirculation of Ash-
pond Sedimentation water
d) Reduction in Steam
Leakages & Blow Downs
a) Commissioning of ETP-2 for
CT Blow-Down
b) Commissioning of Ultrafiltration for DM
c) Modification Compressor
Return Line
a)Reuse of Blow Downs in fire fighting
b) Installation of ETP-1 & 90% west
water reuse inside the plant.
C)Recycling of Ash pond retention
water.
2.76
2.45
2.11 2.14 2.20 2.19 2.16 2
2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17 Target17-18
Specific Raw Water Consumption (m3/MWh)
Units in
Commissioning
Stage
REDUCTION IN SEC
a) Reduction of Forced Outage
b) Optimization of Cold Startup
c) Improved Operational Controls
a) Reduction of Forced Outages
b) Availability of Mills and Feeders
c) Installation of Air Blasters
d) Reduction in Bunker Choking
3.67
0.8
0.21 0.09 0.09 0.11 0.08 0.12 0.05
2009-10 2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17 Target 17-18
Specific oil consumption(ml/kwh)
a) BFP recirculation valve design
modification
b) CT Fans Blades design modification
c) Optimization of Compressor Running Hrs
d) CW pump Interconnection
e) Installation of Natural roof Ventilation
Fans
a) Replacement of Existing Dryers with
Energy efficient dryers
Units in
Commissioning
Stage
a) Installation of Additional
Compressors
a) Installation of New ID
fans
a) Truck Tripler
Commissioning
a) Ultra filtration
Commissioning
REDUCTION IN SEC
a) Energy Efficient
Motor installation.
a) Lighting
Modification.
a) CW interconnection.
b) APH seal
design modification
(4 no.s)
9.82% 10.14% 10.24% 9.84% 9.63% 9.66% 9.58% 9.81% 9.25%
0.00%
5.00%
10.00%
15.00%
2009-10 2010-11 2011-12 2012-13 2013-14 2014-15 2015-16 2016-17 Target 17-18
APC PG test Value: 9.59%
Sl.No. Projects for FY 2014-15 Total Annual
Savings(Rs Million ) Investment Made
(Rs million)
1 APH Soft touch seal replacement for 5 unit 20.85 1.5
2 APH basket replacement in 1 unit 4.7 11.4
3 Operational optimization by maintaining Main steam pressure, Main steam temp etc.@ near design values
20.4 0
4 CT fan Blade Replacement & angle changing (5 fans) 1.9 1.7
5 CW pump impeller coating in 2 pumps 0.42 0.514
6 Condenser bullet cleaning in 4 units 6.53 0.76
7 APC reduction in Power transformer in all units 1.23 0
8 Increase in belt utilization in coal handling plant 1.85 0
9 Leakage arresting of clarifier storage tank 0.07 0
10 Reducing heat loss through condensate drain 2.22 0.03
11 Usage of portable hydro pump instead of BFP 0.18 0.85
Total 60.35 16.75
ENERGY SAVING PROJECTS
Sl.No. Projects for FY 2015-16 Total Annual Savings(Rs Million )
Investment Made (Rs million)
13 Cooling Tower fills design modification for one Unit 3.91 7.0
14 APH seal replacement(4 no.s) 4.05 0.6
15 Condenser chemical cleaning 1.3 0
16 CW interconnection 0.53 1.4
17 BFP recirculation valve design modification 1.77 1.4 18 Energy efficient driers 0.04 0
Total 11.6 10.4
ENERGY SAVING PROJECTS
Sl.No. Projects for FY 2016-17 Total Annual Savings(Rs Million )
Investment Made (Rs million)
19 Cooling Tower fills design modification 119.8 56.0
20 APH seal design modification(4 no.s) 3.7 0.6 21 CW pump interconnection 1.3 0
22 BFP recirculation valve design modification 0.7 1.4 23 HFO to LDO Gun replacement 1.8 1.4
24 Turbine overhauling 53.9 31.37 Total 181.2 89.77
Project Synopsis:
Turbine was running on high turbine rotor expansion. To maintain
Turbine Expansion within limits, turbine inlet temperatures are
reduced. Reduction in turbine inlet temperature has resulted in
increase in specific coal consumption.
High Turbine Differential Expansion in Unit#2 attributed to a
deviation in SCC by 6.28 g/kwh (18.83 Kcal/kwh)
Turbine LPDE Reduction
Actions Taken :
Unit #2 shut down taken .
Turbine Front bearing pedestal guide blocks inspection & correction to
increase the HIP Turbine Casing Expansion
Unit #2 2010 Before Project After Project
CE (mm) 20.1 17.1 20.05
LPDE (mm) 6.3 7.4 6.5
Benefits:
1. Turbine healthiness & Reliability has improved
2. Achieved Reduction in SCC by 6.28 gm/kwh which is financial
savings of Rs 1.07 Crores
DE(H)
DE (L)
LP T
GENERATOR
CE 1
CE 2
HP T IP T
INNOVATIVE PROJECT-1
Manufacturer recommends battery life of 5 years, at room temperature of 27 deg C.
Battery room temp. was above 33 deg C resulting in reduction Battery bank life .
Air flow coming from ECU duct was restricted due to Fire proof false ceiling & Continuously running Battery room exhaust fans.
ECU duct extension done for proper circulation of air. Battery room exhaust fan timer installed & Room Sealing Cost savings for 22 battery banks Rs 60,50,000
Cost savings of Exhaust fan Rs 287000
INNOVATIVE PROJECT-2
Replacement of CT fills has been done with new design incorporating following improvements.
Flute size change from 17 mm to 19mm to avoid choking in rain zone. Increase in total height from 1675mm to 1800mm to increase surface area. Total height is split in 4 layers for ease of handling and maintenance.
This leads to vacuum improvement of 1 kpa with a saving of 22 lacs /Unit/month.
PROCESS IMPROVEMENT-1
BEFORE AFTER
Energy saving
21 kcal
AVR panel should be maintained within 28 Deg C for long life of components like Thyristor and PCB.
Existing ventilation system
Two AVR Panel Exhaust fan in Each Thyristor panel
One 3 Ton tower AC & two no of 1.5 Ton Split AC.
Installed duct for exhaust air removal from room, switching off 2 Split Acs & exhaust fans .
BELLOW Energy saving
143.27 KW
BEFORE AFTER
PROCESS IMPROVEMENT-2
PROCESS IMPROVEMENT-3
CT fan Motors & Seal Air Fan motors were running at partial load, as high capacity motor was installed.
2 CT fan Motors were replaced with 110 KW (down from 132 kW)
Energy saving of 6 kW/motor
2 Seal air fan motors were replaced with132 KW which was removed from CT fan motor instead of 160 KW motors
Energy saving of 8 kW/motor
Energy saving
14 kWhr
PROCESS IMPROVEMENT-4
BEFORE – 50 kWhr AFTER – 46 kWhr
Installation of Mechanical seal on Auxiliary cooling water pump
Installation of mechanical seal by
1. Replacing gland packing in auxiliary cooling water pump to ensure the better sealing
2. Reduce the auxiliary power consumption of 4 units by improving the friction between
stationary and rotary parts
Energy saving
4 KWhr
LP Turbine
PROCESS IMPROVEMENT-5
Condenser flood test:
It’s a proven method to detect the condenser tube leakages in unit overhauling / shut down maintenance .
For condenser flood test –channel support needs to be installed to avoid spring deflection due to overload of condenser filled with 5 meter height.
In order to improve the manpower productivity and lesser shut down time we developed a Height adjustable screw supports and has been installed for condenser flood test
Improvement in Operational Practices
Implementation of Asset Optimisation & war room concept
Development and Implementation of Innovative and Breakthrough Energy Efficiency Improvement Projects
Implementation of Six Sigma Projects,Quality circle, Autonomous maintenance & Kaizen Projects
Daily Monitoring of Specific Consumptions
Idea generation drive and implementing best out of it.
Energy Managment system ISO 50001 implemented in 2012 & re-certification done in the year of 2015.
FOCUS ON ENCON EFFORTS
Projects
RO Installation
Installation of VFD Drives
Addition of New CT Cells
Recommendation of energy Audit
Solar Lighting
Vapour Absorption Chiller
Energy efficient Motor replacement
Rain Water Harvesting
FUTURE ENCON PROJECTS
Integrated Energy Meters reports
MES
Energy Efficient Procurement
E-CER (Capex) Energy Impact Assessment
ENERGY REPORTING & IT ENABLEMENT
IT as a Strength
• CPP has been declared as “Par excellence” unit for 3-year back to back by QCFI.
• CPP achieved “Par Excellence” award for 5S performance and best presentation in National 5S conclave.
• Autonomous Maintenance: Total 10 Sub zones taken in CPP. 03 subzones are certified by QCFI (Score: >80%) in autonomous maintenance and qualified for level 2.
5S
• 54 QC teams are operational with 100% participation Including both direct & indirect employees.
• One of the CPP teams received gold award in CCQC 2016 and Excellence in LQC category in NCQC 2016. QC
• Wave-6 drive has started with 5 top priority projects worth Rs.9.41 crores with 50 employees.
• One of the CPP teams received gold award in CCQC 2016 & Par-Excellence in Six-Sigma category in NCQC 2016.
Six Sigma
• Total 121 Kaizen Projects completed in FY 2016-17.
• CPP received gold award in CCQC and Par Excellence in NCQC 2016.
• One of the CPP teams received gold award in CCQC 2016 and Excellence award in NCQC-2016 & one team received silver award in CCQC 2016.
Kaizen
BUSINESS EXCELLENCE
PEOPLE FOCUS In
stan
t R
eco
gnit
ion
Shabash Card
Au
dit
Sco
rin
g B
ased
Kaizen Rolling Trophy Fo
r V
L Em
plo
yee
s
Employee of the Month
Bas
ed o
n A
ud
it s
core
s
Quality Circle Rolling Trophy
Awards/Recognition
Men
tori
ng
“V-Connect Program
Inte
ract
ion
“LSIP” Program
Enga
gem
ent
Proud parents
Lear
nin
g “WILP”
(BS,MS & MBA program) with bitt’s Pilani
Employee engagements