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J K LAKSHMI CEMENT, SIROHI, RAJASTHAN
19TH National Award For Excellence In Energy Management-2018
Presented By:-
Pradip Kr. Ghara, Sr. Mgr. (Elect.)
Kanish Kr. Singh, Asst. Mgr (Process)(EM-13473)
Brief Introduction of JKLCL – Sirohi, Rajasthan
19TH National Award For Excellence In Energy Management-2018
ISO 9001 ISO 14001 OHSAS 18001 ISO 50001
53 GRADE 43 GRADE PPC GRADE
RMC AAC BLOCK POP
Products Manufactured Here .
PRO+ GRADE
PLANTYEAR OF
COMMISSIONING
INSTALLED CAPACITY
(TPD)
PRESENT
STATUS
(TPD)
KILN-1 1982 1500 4500
KILN-2 1995 2500 5000
KILN-3 1996 2500 5000
Journey Towards Up gradation……..
Established
in Aug1982
with 0.5
MTPA
capacity.
Unit – II
Commissioned
in 1995 with
0.9 MTPA
capacity.
Unit – III
Commissioned
in 1996 with 0.9
MTPA capacity.
Present Cement
Production
Capacity 4.64
MTPA.
Year(April March)
Specific Energy ConsumptionRedn. in SEC Over
previous years
ElectricalThermal Elect. Thermal
Kwh/Ton of Cement(excl. Crusher)
KCal/kg of clinker
% %
2014-2015 76.46 704 3.03
2015–16 77.62 677* (- 1.52)** 3.84
2016–17 77.73 699 (- 0.14) ** (- 3.25)
2017-18 75.87 697 2.39*** 0.286
** Increased because of Less PPC production and increase in Ball Mill run hrs
* Reduced due to easy burning material from mines
*** SEC up to clinker reduced for energy saving in SPRS, VRM & more PPC
production
Energy Performance Since 2014……
A Comparison with National & International Benchmark
Thermal Energy Consumption (Kcal/KG Clinker)
600
650
700
750
660684
704677
699 697
Kca
l/
Kg
C
LIN
KE
R
• Reference : CII Energy Benchmarking study carried out at JKLC in May,2018
A Comparison with National & International Benchmark
Electrical Energy Consumption(Unit/ton cement )
60
65
70
75
80
International
Benchmark
National
Benchmark
2014-15 2015-16 2016-17 2017-18
65
65.67
76.4677.62 77.73
75.87
KW
H/
MT
C
EM
EN
T
• Reference : CII Energy Benchmarking study carried out at JKLC in May,2018
Electrical Energy Consumption(For Raw Grinding Section)
0
5
10
15
20
JKLC
U-I VRM
JKLC
U-II VRM
JKLC
U-III VRM
COUNTRY
BEST
12.21 9.87 9.6713.3
KW
H/
MT
M
AT
ER
IAL
• Reference : CII Energy Benchmarking study carried out at JKLC in May,2018
Incl: Main drive, Mill Fan, Classifier & Reject Elevator Power
Electrical Energy Consumption(For Clinkerization)
• Due to High PH Fan Power due to High Pressure Drop Across PH
0
5
10
15
20
2523.09 22.2 21.61 24.5
16.92
KW
H/
MT
C
LIN
KE
R
• Reference : CII Energy Benchmarking study carried out at JKLC in May,2018
Electrical Energy Consumption(Up to Clinkerization)
0
10
20
30
40
50
60
JKLC U-I JKLC U-II JKLC U-III OVERALL
JKLC
COUNTRY
BEST
52.45
44.85 44.61 47.143.32
KW
H/
MT
C
LIN
KE
R
Kca
l /
Kg
of
Clin
ker
A Comparison Thermal Energy Consumption with Plants in same
cluster (Kcal/Kg of Clinker)
650
660
670
680
690
700
710
720
JKLC CII
CLUSTER
FIGURE
A B C
697694
720
687
676
Kca
l/
Kg
C
LIN
KE
R
A Comparison Electrical Energy Consumption with Plants in
same cluster (Unit/ton cement )
73
74
75
76
77
78
JKLC A B C
75.87
77.38
75.53
74.73
KW
H/
MT
C
EM
EN
T
• To Reduce Pressure drop From Mill O/L to Fan I/L In
VRM(0.2Kwh/t of material)
• To reduce Pressure drop across Cyclone of VRM(1 Kwh/T material)
• Installation of Pre-Grinder in Cement Mills.
• To reduce pressure drop by 40 mmWc across down comer duct(0.5
Kwh/t of Clk)
• PH fan efficiency improvement by 5 %.(0.5 Kwh/t of Clk)
• Top cyclone efficiency improvement (3 kcal/Kg clk)
• Improving separator efficiency of Cement mill-1(0.3 Kwh/T cement)
Road Map to achieve the National / International Benchmark
Energy Benchmark study through CII-GBC, Hyderabad, May18.
❖Replacement of AQC fan with high efficient fan.
❖Installation of AQC boiler in Line-3
❖Reduce the pressure drop across Mill body in Raw mill-4
❖Replacement of conventional lights with Led(Ongoing).
❖ Installation of New Louver Ring in RM-2 in upcoming shut down
Road Map to achieve the National / International Benchmark
Energy saving Proposals based on Internal Audits
(SGA/CFT/KAIZEN/Technical cell
0.0877
0.0833
0.0747
0.09880.0940
0.06
0.07
0.08
0.09
0.1
0.11
0.12
Base Line (On PPC)-
PAT cycle-1
Target (On PPC)-PAT
cyce-1
Achieved(On PPC) PAT
cycle-1
Base Line(On OPC)-
PAT Cycle-2
Target(On OPC) PAT
cycle-2
MT
OE
/to
n p
rod
uct
PAT Performance
Target
Reduction
4.91%
Achieved
Reduction
14.82%
Target
Reduction
4.86%
PAT (Performance, Achieve & Trade)
Energy Conservation projects since 2015……
Sr.
No.DESCRIPTION UNITS
ZERO
INVESTMENT
WITH
INVESTMENT
ATOTAL PROJECT
IMPLEMENTEDNO.S 36 19
BTOTAL ELECTRICAL ENERGY
SAVINGS
MILLION
KWH6.23 7.33
CTOTAL THERMAL ENERGY
SAVING
MT OF
COAL16822 0
D TOTAL SAVING
I ELECTRICAL RS MILLION 47.69 60.98
II THERMAL RS MILLION 98.9 0
E TOTAL SAVINGS RS MILLION 146.59 60.98
F TOTAL INVESTMENT RS MILLION NIL 42.13
*All savings calculation is on per annum basis
Energy Efficiency Improvement Activities
Last Three Years Project ( 2015-16, 2016-17, 2017-18)
S.
No
List of Major Energy Saving Projects
(2015-2016)
Annual Saving Rs.
Million
Invest.
Made
Elect. ThermalRs.
Millions
01
Optimization of VRM by modification of
Nozzle ring and optimization of mill bed
height. (133 kW)
7.241 - -
02
Optimization of Coal Mill by grinding
media and modification of intermediate
diaphragm. (61 kW)
3.308 - -
03
Optimization of Kiln-3 Compressors
Operation by reducing the operating
pressure of Compressor. (15 kW)
0.89 -
04Modification in discharge circuit of Ball
mill and TCDRI VRM. (6.88 kW)0.374
Major Energy Saving Projects Zero Investment (2015-16)
S.
No
List of Major Energy Saving Projects
(2015-2016)
Annual Saving Rs.
Million
Invest.
Made
Elect. Thermal Rs.
Millions
05Replacement of 2 nos. of screw conveyors
with chain conveyors. (8 kW)0.494 - -
06Optimization of kiln operation.
(16630 MT Coal Saving /Annum)97.37 -
07
Replacement of 18 KW Analyzer water
pump with 5.5 KW water pump
(8 kW)
0.356 - -
Major Energy Saving Projects Zero Investment (2015-16)
S.
No
List of Major Energy Saving Projects
(2016-2017)
Annual Saving Rs.
Million
Invest.
Made
Elect. Thermal Rs.
Millions
08
Optimization of Dam Ring Height in China VRM
(70 mm to 56 mm)
(110 kW )
6.19 -
09
Arresting of false air in pre-collector and
replacement of expansion joint in china VRM
(22 kW)
1.24 - -
10
Reduction in PH fan power consumption in Kiln-3
by arresting false air ingress
(30 kW )
1.84
11
Remove 35 BE1 Bucket elevator in precrusher
(Feeding belt discharge in vibrating screen instead
of bucket elevator)
(15 kW )
0.84
Major Energy Saving Projects Zero Investment (2016-17)
S.
No
List of Major Energy Saving Projects
(2016-2017)
Annual Saving Rs.
Million
Invest.
Made
Elect. Thermal Rs.
Millions
12
One air slide blower stopped in PH-1 VRM
(To be remove from group and interlock air
slide blower made it stand by for 2606 )
(7 kW)
0.41 - -
Major Energy Saving Projects Zero Investment (2016-17)
S.
No
List of Major Energy Saving Projects
(2017-2018)
Annual Saving Rs.
Million
Invest.
Made
Elect. Thermal Rs.
Millions
13Blended appron feeder and spillage conveyor
removal from the circuit (5 KW)0.28 - -
14Reduced power consumption in 10FN-1 Dust
collector Fan (18 KW)1.02 - -
15Reduce power consumption in Kiln-1 cooler
fans through optimization (15 KW)0.92 -
-
16
Saved Power consumption by reducing the
pressure drop across the dampers of Silo Top
Bag Filter Fan in Kin-2 (9 KW)
0.55 --
17
Reduced Power consumption in Kiln-1 CV
Fan by removing the damper as fan always
runs with VFD (10 KW)
0.62 --
18Optimization of cooling air in kiln-1 by
cleaning of grate plates (46 KW)2.82 - -
Major Energy Saving Projects Zero Investment (2017-18)
S.
No
List of Major Energy Saving Projects
(2017-2018)
Annual Saving
Rs. Million
Invest.
Made
Elect. Thermal Rs.
Millions
19Removal of Bag filter fan from dry fly ash
Circuit in CM-2 (9 KW)0.31 - -
20 False air Arresting in RM-4 (5 KW) 0.28 - -
21Optimization of separator BH DP in CM-1,
CM-3,CM-5,CM-6 (16 KW)0.91 - -
22Sphere slot of outlet diaphragm has been
blocked in cement mill-1 (25 KW)1.42 - -
23Modification Of Cheek Plate in CM-2 HRC
(10 KW)0.57 - -
Major Energy Saving Projects Zero Investment (2017-18)
S.
No
List of Major Energy Saving Projects
(2017-2018)
Annual Saving
Rs. Million
Invest.
Made
Elect
.
Thermal Rs.
Millions
24Modification in Pre crusher Circuit by removal of
Belt Conveyor 35-BC-3 (11 KW)0.56 - -
25Booster Fan Inlet Damper replaced by Distance
Piece in coal mill-1(3 KW)0.17 - -
26Pre crusher dust collector fan damper
Removal(35-FN-1 & 35-FN-2) (10 KW)1.02 - -
27Apron Feeder DC Drives replace with AC drives
in RM-2 (3 KW)0.17 - -
28
Reduction in Electrical & Heat Consumption by
Optimizing the Coal Conveying Volume in Kiln-
1(18 KW & 1 Kcal/Kg Clk)
1.11 1.53 -
29 VFD Installation in Tippler Bag filter fan (9 KW) 0.31 - -
30
Interconnection of RM-1 Compressor 36CP-3
with Raw Mill-4 Bag House Compressor 361CP-
1 (29 KW)
1.64 - -
Major Energy Saving Projects Zero Investment (2017-18)
S.
No
List of Major Energy Saving Projects
(2016-2017)
Annual Saving Rs.
Million
Invest.
Made
Elect. Thermal Rs.
Millions
31Reduce pressure drop across Bag House Fan
inlet damper in Raw Mill-4 (12 KW)0.68 - -
32
Reduce power consumption of Kiln-2
andKiln-3 Blaster compressor by optimization
of Blaster Operating freq. & compressor
loading-unloading pressure (55 KW)
3.38 - -
33Interconnection of Kiln-2 PH blaster compr
with Kiln-2 inlet seal compr (22 KW)1.35 - -
34
Interconnection of Kiln-1 PH Blaster compr
with 3 nos. of other compr (KGG; Cooler
Blaster & Chemical Lab) (25 KW)
1.54 - -
35Optimization of CM-1,CM-3,CM-5,CM-6 Bag
house system (34 KW)1.91 - -
36 CM-1 CA Fan I/L Damper Removal (22KW) 1.25 - -
Major Energy Saving Projects Zero Investment (2017-18)
*All savings calculation is on per annum Basis
Major Energy Saving Projects With Investment
Since 2015…..
Total Projects Implemented : 19
Total Electrical Energy Saving : 7.33 Million KWH
Total Thermal Saving : 0 MT of Coal
Total Savings in Rs :
Electrical : Rs. 60.98 Million
Thermal : Rs. 0 Million
Total Savings : Rs. 60.98 Million
Total Investment : Rs. 42.13 million
S.
No
List of Major Energy Saving Projects
(2015-2016)
Annual Saving Rs.
Million
Invest.
Made
Elect Thermal Rs.
Millions
01Installation of 02 Nos. of 75 KW VFD’s in Pre
Crusher Bag filter Fans. (10 kW)0.54 0.50
02Installation of 650 KW SPRS in Fly Ash Drier
Fan. (10 kW)0.30 1.05
03Modification in 465 KW Kiln-2 CV Fan SPRS
system. (42 kW )2.47 0.80
04Replacement of 50 Nos. CFL 15 W to LED
lamp 7W in colony (0.17 kW )0.01 0.0035
Major Energy Saving Projects With Investment (2015-16)
S.
No
List of Major Energy Saving Projects
(2016-2017)
Annual Saving Rs.
Million
Invest.
Made
Elect Thermal Rs.
Millions
05Replacement of 27 Nos. 40W Tube lights to 20
nos. LED 7 in ADM Building (0.94 kW )0.003 0.002
06Installation of high efficient fan with VFD in
cement mill-1 (60 kW)3.39 02
07Re-Routing of dry fly ash transportation line.
(60 kW)1.84 2.9
08Kiln inlet riser duct modification in kiln-1
(60 kW)3.68 1.2
09Modification of Raw Mill -2 by CFD of
Cyclones and duct (60 kW)3.38 0.6
Major Energy Saving Projects With Investment (2016-17)
S.
No
List of Major Energy Saving Projects
(2016-2017)
Annual Saving Rs.
Million
Invest.
Made
Elect Thermal Rs.
Millions
10Modification of Raw Mill -3 by CFD of
Cyclones and duct. (60 kW)3.38 0.6
11
Installation of IGBT based digital SPRS in
place of thyrister based analolouge SPRS in
raw mill-3 (50 kW)
2.81 2.7
12Installation of recirculation damper in CM-2
Stack (12 kW)0.68 0.2
1323 nos 150 watt HPSV street light lamp replace
with 40 watt LED lamp. (2.5 kW)0.072 0.1
Major Energy Saving Projects With Investment (2016-17)
S.
No
List of Major Energy Saving Projects
(2016-2017)
Annual Saving Rs.
Million
Invest.
Made
Elect Thermal Rs.
Millions
14735 nos. 36 watt fluroscent tube rod replace
with 22 watt LED tube rod. (10.2 kW)0.291 0.3
1520 nos. 150watt HPSV street light lamp replace
with 60 watt LED lamp. (1.8 kW)0.051 0.1
Major Energy Saving Projects With Investment (2016-17)
S.
No
List of Major Energy Saving Projects
(2017-2018)
Annual Saving Rs.
Million
Invest.
Made
Elect Thermal Rs.
Millions
16417 Nos. Conventional HPSV Lights replaced
with Energy Efficient LED lights (33 KW)1.13 - 2.2
17
Installation of HOT Air Recirculation in Kiln-2
to increase the Green Power Generation
(Through WHRS) (9500 Units/Day)
24.36 - 22.2
18Installation of Active Harmonic Filter (AHF) for
Power Factor improvement 4.14 - 4
19Installation of New Louver Ring in RM-3
(150 KW)8.46 - 0.5
Major Energy Saving Projects With Investment (2017-18)
at JK Lakshmi Cement
Reduction in Raw mill fan power consumption by installation of aerofoil design louver ring in VRM-III
Innovative Project-I
Background: Pressure drop across Mill
(892 mmwg)
Probable reason : Non uniform distribution
of air across louver ring
Action taken : Thorough study and replacement of louver ring
aerofoil louvers
Reduction in Raw mill fan power consumption by installation of
aerofoil design louver ring in VRM-III
Innovative Project-I
•This modification helped us to reduce
pressure drop by 62 mmwg.
• Production Increased by 3 Tph.
• Total units saved : 1089000 KWH/Year
• Total Savings : 5.98 Million/Annum (@5. 5Rs/Unit)
• Total Investment : 0.35 Million
• Payback Period : 1 Month
Savings in terms Power Consumption
•There is saving of 150 units/hour
in Raw mill fan Power
Installation of Hot Air Recirculation in Kiln-II to generate
more green power
Innovative Project-II
➢ Hot Air Recirculation in Fan Nos.6 , 7 & 8.
➢ Gross Power Generation Increased by 9500 Units/Day.
➢ Commissioned in January,2018.
➢ Reduction in Green House gases 12085 Kg CO2/Day.
Duct From CV Stack Entry At Fans
Innovative Project-II
Cost Benefit Analysis
• Total units generated : 3135000 KWH/Year
• Total Savings : 17.24 Million/Annum (@5.5 Rs/Unit)
• Total Investment : 22.2 Million
• Payback Period : 15 Months
Benefit & Savings
Particulars Units/Day
Increase in Power Generation from WHR
System
KW 9500
Reduction in Green House Gases Kg of CO2 12085
Reduction In Numbers of Hammers in Pre Crusher
Innovative Project-III
Background :Heavy Wear pattern of Hammers &(40%) of Hammers running Idle.
:Total No. Of Hammers : 102
: To reduce Maintenance time
Idea Generation: Study of the wear pattern
Action Taken : Decision to eliminate alternate row of Hammers
: Keeping 54 Hammers in line in 9-9-9 combination first
: Later on 51 Hammers in line with 9-8-9 combination
Reduction In Numbers of Hammers in Pre Crusher
Innovative Project-III
Results :
• Vibration of Rotor Bearing reduced by 1 mm/sec.
• Power saving by 40 Kw at same output
• Maintenance period reduced from 3 days to 1 day
Power saving : 40 KW
Annual Power Savings : 0.95 Million Rs
Annual Mechanical maintenance saving : 3.45 Million Rs
Total Savings : 4.4 Million Rs
Savings
Renewable Energy
Use of Bio Mass Such as Mustard, Moong, Mahendi,
Soyabean husk, Sarason to replace some quantity of Coal
used in PC firing of the kiln section.
Conservation of natural Resources.
Reduction in net CO2 emission in the atmosphere.
Low Cost.
Year 2015-16 2016-17 2017-18
Used Quantity
(MT)704** 2223** 11009.79
** Less due to Unavailability
Bio-Mass As A Renewable Energy
Benefits
Utilization Of Waste Material as Fuel
S No Fuel Used 2015-16 ( MT) 2016-17( MT) 2017-18 (MT)
1 Waste Mix Solid 0 0 714
2 TDI Tar 0 0 469
3 TPP Fly Ash 22836 23180 32795
4 De Oil Cake 0 287 3705
5 Pulp Waste 101 33 0
6 RDF Fluff 4323 2590 842
Total 23370 26090 38525
5.5 % TSR
Bio Mass Handling System
Renewable Energy From WHRS and GHG Reduction
0.00
50.00
100.00
2015-16 2016-17 2017-18
78.3790.08 92.46
21.63 23.55 24.63
WH
R G
en
era
tio
n (
Mil
lio
n K
WH
/An
nu
m
Co
2 R
ed
ucti
on
(K
g C
o2
/T
Clk
)
YEARS
JK LAKSHMI CEMENT, JAYKAYPURAM
Co2 Reduction (Kg Co2/T Clk)
WHR Generation Kg CO 2 / T Clk Reduction
660
665
670
675
680
214-15 2015-16 2016-17 2017-18
675 674 676 677
Kg Co2 / T Major Product
Co
2 R
edu
ctio
n (
Kg
Co
2/T
Cem
ent
GHG Inventorisation
BENEFITS
Saving of 25000 units/ year
CO2 emission reduction 40 Tonne/ Year
Solar Water Heater At Transit House
Solar Power Plant At Village Lumbaniya, District Jodhpur
(RAJ.)
Capacity-: 6.12 MW
Solar Power Plant At Jaykaypuram Colony
Capacity- 232 KW
Green Supply Chain
http://jklakshmicementsrm.com/srm/
Energy Management Policy
(Integrated Management System)
Employee Association In Encon Activities
CFT
KAIZEN
QUALITY CIRCLE
TECH CELL
SHOP FLOOR ENCON TEAM
Feasibility Test
Suggestion at
Concerned Section
reviewCommittee review
Suggestion
Approval
Trail
Successful
Documentation
&
Implementation
of Suggestion
Review Of
Implemented Idea for
benefits &
Sustainability
Audit Team
Confirmation
Rewards,
Recognition &
Appreciation
Employee Association In ENCON Activities Suggestion Scheme
Methodology
❖Daily, weekly& monthly monitoring & analysis of SEC.
❖Online display of SEC in DCS
❖Inter-firm comparison for SEC.
❖Adoption of best practices.
❖ Attending task force meeting with BEE
❖Internal & external audits .
❖Regular training programmes.
❖CFT , SGA, Kaizen, Quality circle
Sustainability
Monitoring
And
Analysis
Decision Making
Management Level
Decision Making
Operations Level
Decision Making
Real Time
Action
Feedback
Feedback
Off Line
On Line
Data
Action
ActionOperator
Real Time
Information System
Plant
Data
Energy Management Tool
Plant Head
Departmental
Heads
Energy Manager
(Process)Energy Manager
(Electrical)
Section In charge / CFT
Plant Operator
WTD
JKLC HAS DEDICATED ENERGY
CELL WITHIN
TECHNICAL SERVICES
Energy Management Team
❖Energy management cell with clear cut responsibilities.
❖Daily monitoring of Energy Deviation report.
❖ Benchmarking National/International/group wise/Cluster units.
❖ Regular study of equipments on deviation and their analysis.
❖ Process evaluation & identification of energy conservation scope.
❖ Feasibility study of suggestions and designing proposals for sanctions.
❖ Taking corrective and preventive measures and ensuring
implementation.
❖ Organizing internal and external Energy Audit survey.
Energy Monitoring Methodology
Certificate Observations Actions Taken
OHSAS 18001:2007
1. White wash of Canteen may be considered.
2. Better housekeeping near Electrical Panels by removing unwanted items
Implemented.
ISO 9001:2015
Monitoring of inter locking system may be recorded
The new record sheet made & system implemented.
Doc No: DSP/07/F/16 Rev: 00 25th Oct 2017
ISO 14001:2015
Energy Efficiency criteria in
the procurement process is
already implemented to be
recorded properly.
Implemented
Implementation of Integrated QEnHSE
Management System External Audit Report: Stage2
Note- There was no any non-conformity but observations for
opportunity to improvement
Environment
Greenery in Plant, Colony and nearby area
Environment
Cap
. 16500
m3
Cap
. 12500
m3
Rain Water Harvesting in Pond
Surface and Roof Top Water Harvesting
Watershed Management in Mines Hills
Environment
KFP Patented Rain Water Harvesting Systems to augment ground water recharge.
Environment
4NH3+4NO+O2→4N2+6H2O
NOX (mg/Nm³)@ 10 % O2 < 800
SNCR System In All Three Kilns.
NOX (mg/Nm³)@ 10 % O2 < 1000
Inauguration on 29Th November 2017
Safety Innovation
65
National Safety MonthRoad Safety Week
Fire Service Week
Safety Celebration
Corporate Social Responsibility (CSR)
Adopted Primary Health Centre
Swatch Bharat Mission – Ek Abhiyaan
Corporate Social Responsibility (CSR)
Literacy Projects Reward and recognition to academically
bright children and talented sportspersons
Free Medical Services to Nearby
Villages
Family Welfare Programs in
Nearby Villages
Corporate Social Responsibility (CSR)
Blood Donation Camp At Jaykaypuram
One of Top 25 Most Innovative Companies
Rewards and Recognition
CII “Excellent Energy Efficient Unit Award -2016 & 2015”
CII “Excellent Energy Efficient Unit Award -2014 & Most Innovative Project Award”
Rewards and Recognition
CII “Energy Efficient Unit
Award -2013
CII “ExcellenceEnergy
Efficient Unit Award -2012
National award for energy efficiency in cement industry (2013-14)
Rewards and Recognition
Energy Concervation
Award -2011 By StateEnergy Consevation
Award by BEE -2011
National award for excellence in
energy management 2010-energy
efficient unit ”
Best Energy Efficient Practice
Exhibitioner- 1st Prize
Rewards and Recognition
International Safety
Award -2016 from British
Safety Council London
FAME-Excellence Award 2016
“Best Innovative CSR Project
GOLD AWARD"
Rewards and Recognition