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KOTHARI PETROCHEMICALS LTD MANALI- CHENNAI CII- 22 nd NATIONAL AWARD EXCELLENCE IN ENERGY MANAGEMENT 2021 TEAM MEMBERS: Mr. Anand B R – Sr. Manager- TLS Mr. Saravanan J- Energy manager Mr. Karunamoorthy R- Asst. Manager- TLS

CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

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Page 1: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

KOTHARI PETROCHEMICALS LTD

MANALI- CHENNAI

CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY MANAGEMENT 2021

TEAM MEMBERS:Mr. Anand B R – Sr. Manager- TLSMr. Saravanan J- Energy managerMr. Karunamoorthy R- Asst. Manager- TLS

Page 2: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

1. KPL Business overview

Sugar Petro Chemical

DepositLocker

Bio Tech

Power Distillery

19901936 19611961 19611961

KPL is a part of the renowned “HC Kothari Group”, we are the largest producer of premium quality Polybutene in India. Since our founding in 1990

Page 3: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

KPL OUTLINE

PlantCommissioned

March 1990

Technology of the

ProcessCOSDEN

Earlier Plant Design

Capacity5000 MTA

In the Year Of 2002Capacity

Increased to 8400 MTA

In the Year Of 2007

PIB Train-2 was commissioned

Capacity Enhanced to

24KTAYear of

2007 - 2008

State of Art 2MW CPP PlantCommissioned

Year of 2018

Safety & Engineering Park

Created Year of 2020 Highest

Production of 25KTA was

achieved in the year of FY20-21

Capacity Enhanced to

36KTAYear of

2020 - 2021

Page 4: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

C4 Raffinate Storage

Reactor section

Neutralization section

De Butanizersection

Flashsection

Polymer storagesection

LP Storagesection

Blendingsection

FFU /Feed Treatsection

FS-2CPCL

FS-1CPCL

FS-3OTHER

RETURNCPCL

RETURNCPCL

C4 RAFFINATE TO SPHERE

C4 RAFFINATE TO REACTOR

FEEDSTOCK-2iB CONC- 8-12%

FEEDSTOCK-1iB CONC- 18-22%

FEEDSTOCK-3iB CONC- 99.9%

ENRICHEDiB CONC- 18-22%

CATALYSTSLURRY

10-15% NaOH

SPENTNaOH

OTHER BUTANES/ UNREACT

WEAK CAUSTIC

SOLN

CAT+POLYMER

4-6%

SPENTCAUSTIC

SOLN

OTHER BUTANES/ UNREACT

POLYMER+LP+

UNREACT +CATALYST

POLYMER+LP+

UNREACT

POLYMER+LPPOLYMER

*iB- isobutylene; LP-Light Polymer; CPCL-Chennai petroleum corporation limited

LP

2. Manufacturing Process Flow

Page 5: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

3. Impact of COVID-19

❖This pandemic has really tipped the balance of Global economy.

❖COVID 19 really taught us more. During the pandemic, we were at the stage we have to run the

plant at lower capacity. In this situation we are very keen on energy consumption.

❖We have a restricted our manpower as per government guidelines.

❖ Our team gave a greater support to run the plant at very efficiently and very productively.

❖We have Increased our productivity by 5%

❖We have Reduced our energy consumption by 5%.

❖We were at the stage, we have to export more than domestic demand. Which has a greater impact

in freight and transportation.

Page 6: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

4. Energy Consumption Overview

Plant absolute energy consumption FY-2020-2021

-

500.0

1,000.0

1,500.0

2,000.0

2,500.0

3,000.0

3,500.0

4,000.0

Power, toe Thermal, toe Total Plant, toe

831.6

3,132.2

3,964

FY-21

Power, toe21%

Thermal, toe79%

PLANT TOTAL ENERGY CONSUMPTION

Page 7: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

4. Energy Consumption Overview (Last three years)

❖Total power consumption dropped by 4%

❖ Total Thermal energy consumption increased by

13%

❖ Energy consumption increase 9%

❖ Productivity increase 5%

94,00,000

95,00,000

96,00,000

97,00,000

98,00,000

99,00,000

1,00,00,000

1,01,00,000

FY-19 FY-20 FY-21

96,75,421

1,00,73,994

96,72,070

Power consumption, kWh

2,500.0

2,600.0

2,700.0

2,800.0

2,900.0

3,000.0

3,100.0

3,200.0

FY-19 FY-20 FY-21

2,727.5 2,743.3

3,132.2

Thermal energy consumption, toe

3,300

3,400

3,500

3,600

3,700

3,800

3,900

4,000

FY-19 FY-20 FY-21

3,560 3,610

3,964

Total energy consumption, toe (Power+Thermal)

Page 8: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

5. Specific Energy Consumption (Last three years)

0.0

100.0

200.0

300.0

400.0

500.0

FY-19 FY-20 FY-21

488.3

421.4386.9

Power Sp. Consumption MT/MT

1000000.0

1050000.0

1100000.0

1150000.0

1200000.0

1250000.0

1300000.0

1350000.0

1400000.0

FY-19 FY-20 FY-21

1377262.1

1148194.9

1253547.7

Thermal energy consumption Kcal/MT

0%

20%

40%

60%

80%

100%

FY-19 FY-20 FY-21

1377262.1 1148194.9 1253547.7

419927 362404 332706

Total Energy Sp. Consumption Kcal/MT (Thermal + Power)

Reduced By 8%

Increased By 9%

Increased By 5%

Page 9: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

5. Production Details (Last three years)

0

5000

10000

15000

20000

25000

30000

FY-19 FY-20 FY-21

19815

2390625001

Production, MTAIncreased

By 5%

Page 10: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

5. Energy Consumption Plan- FY22&23

Plan to Reduce Energy Consumption:

❖ Increasing Feed throughput & concentration to reactor, increase in productivity with in house trials

❖ Identifying Bottlenecks and implementing process change.

❖ Utilization of plant at maximum capacity, Running the plant without interruption.

❖VFD Provision for Butane compressor to optimize the load and energy consumption.

❖ Implementing waste heat recovery system- Pinch Analysis

❖ Best Engineering practices of- Thermal survey across the plant; Ultrasound leak detection program.

0.0

200000.0

400000.0

600000.0

800000.0

1000000.0

1200000.0

1400000.0

FY-19 FY-20 FY-21 FY-22 FY-23

1377262.1

1148194.91253547.7

1029893.0 1009093.0

Thermal energy consumption Kcal/MT

0

50

100

150

200

250

300

350

400

450

500

FY-19 FY-20 FY-21 FY-22 FY-23

488.3

421.4386.9

362 353

Power Sp. Consumption, kWh/MT

Page 11: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

5. Specific Energy Consumption

Factors Influencing SEC variation.

Internal Factors External Factors

Grade change over

Shutdown & Start-up

Employee Participation

De Bottlenecking trials

Effective energy management system

Capacity utilization due to market demand

Climatic condition

Fuel Price/ Availability in Market

OEM/ Customer requirement

Raw material availability & Quality

Preventive maintenance

Page 12: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6. Energy Project Implemented (Last three year’s)

2018-2019

2019-2020

DESCRIPTION ZERO INVESTMENT WITH INVESTMENT TOTAL

Project in No's 1 6 7

Total Investment in Million 1.946

Total savings in Million 7.71

Total Energy saving- Thermal MKcal/Year 4132.2

Total Energy saving- Power MkWh/Year 0.15

Total Water saving- KL/Year 28800

Pay Back in Months 3

DESCRIPTION ZERO INVESTMENT WITH INVESTMENT TOTAL

Project in No's 5 5 10

Total Investment in Million 0.33

Total savings in Million 21.1

Total Energy saving- Thermal MKcal/Year 9711.3

Total Energy saving- Power MkWh/Year 1.34

Total Water saving- KL/Year 6840

Pay Back in Day's 0.2

2020-2021

DESCRIPTION ZERO INVESTMENT WITH INVESTMENT TOTAL

Project in No's 7 9 16

Total Investment in Million 6.22

Total savings in Million 7.53

Total Energy saving- Thermal MKcal/Year 1301

Total Energy saving- Power MkWh/Year 0.66

Total Water saving- KL/Year 25430

Pay Back in Month's 9.9

Page 13: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6. Energy Project Implemented (2020-2021)

Project Implemented : Waste heat recovery from LP condensate drum vent using PHE

Description:❖ LP steam is used in Feed fractionation unit, condensate from FFU is being stored in separate

collection drum and send back to boiler. ❖ Flash steam from the drum kept in local. ❖ New PHE provided to recover the heat from flash steam vent.

Investment made : 0.8 Lakhs

Benefit achieved :❖ Total clean condensate collection- 600KL/Annum❖Total thermal energy saving – 441MKcal/ Annum❖ Total cost savings – 5.7 Lakhs/Annum

Pay Back Period: 1.7 Month

Page 14: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6. Energy Project Implemented (2020-2021)

Project Implemented : Waste Heat recovery from HP condensate drum vent using PHE

Description:❖ HP Condensate drum vent is been connected with condenser lined-up with CT water.❖ New PHE provided and connected with Boiler feed water to pre heat and send to Boiler. ❖ The heat load is been going to cooling tower is been diverted to Boiler feed water.

Investment made : 5.34 Lakhs

Benefit achieved :❖ Total clean condensate collection- 1348KL/Annum❖Total thermal energy saving – 718MKcal/ Annum❖ Total cost savings – 9.08 Lakhs/Annum

Pay Back Period: 27 Days

Page 15: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6. Energy Project Implemented (2020-2021)

Project Implemented : Capacitor provision for MCC-2

Description:❖ During continues monitoring of MCC panel, PF found to be low in MCC-2, ❖ Which has been identified and capacitor was provided to balance the load. Now it is running

normal; Before PF-0.77; After PF-0.95

Investment made : 1.59Lakhs

Benefit achieved :❖ Total thermal energy saving – 0.1MkWh/ Annum❖ Total cost savings – 5.01 Lakhs/Annum

Pay Back Period: 3.8 Months

Page 16: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6. Energy Project Implemented (2020-2021)

Project Implemented : Condensate collection from FG Storage area

Description:❖ FG Tank heating condensate drain into gutter, the clean condensate can be re use to boiler

feed tank.

Investment made : 16.57Lakhs

Benefit achieved :❖ Total water saving – 7200KL/Annum❖Total cost savings – 9.36 Lakhs/Annum

Pay Back Period: 21 Months

Page 17: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6.Energy Project Implemented (2020-2021)

Project Implemented : Pump swaping in Process (High capacity pump to low capacity pump)

Description:❖ Process water injection pump have a high head and high capacity❖ Since we required low capacity (50% of the pump capacity is been utilized). ❖ Pump is been replaced with adequate pump (redundant pump).

Investment made : Zero Investment

Benefit achieved :❖ Total Power saving – 6048/Annum❖Total cost savings – 0.35 Lakhs/Annum

Pay Back Period: -

Page 18: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

6. Energy Project Implemented (2020-2021)

Project Implemented : UP-9000 Leak detector usage.

Description:❖ Since we are handling LPG as a raw material we are unable to detect the untraceable (Lower

than detection level) quantity of LPG leak. ❖ Now we have procured ultra sound leak detector to identify the Fugitive emission from

process.

Investment made : 5.0 Lakh

Benefit achieved :❖Total cost savings – 1.16 Lakhs/Annum

Pay Back Period: 4 Months

Page 19: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

7. Innovative Project Implemented

Project Implemented : RO Reject water using for cooling tower

Description:❖ RO Reject water is been used for cooling tower makeup. ❖ Earlier we use metro water to produce DM water. ❖ Since the conductivity of metro water is high it is necessary to treat RO reject water in our

Effluent treatment plant. ❖ Now we signed MOU with CMWB to use TTRO water from their STP unit. ❖ This water quality is better than metro water, conductivity and other parameters are match

the CT makeup water.

Investment made : 29.8Lakhs

Benefit achieved :❖ Total water saving – 7279KL/Annum❖ Total thermal energy saving – 0.21MkWh/ Annum❖ Total cost savings – 17.98 Lakhs/Annum

Pay Back Period: 20 Months

Page 20: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

7. Innovative Project Implemented

Project Implemented : Hot condensate using for wash vessel makeup instead of cooled condensate

Description:❖ Earlier cold condensate from Ejector is being used for wash vessel.❖ Hot condensate from common condensate collection drum is being cooled and used for column

injection. ❖ Injecting the cool condensate to wash vessel incur heat loss and also lead to washing inefficiency, hot

condensate from common condensate collection drum can be directly use into wash vessel, at the same cool condensate from ejector directly use for column injection without additional cooling.

❖ By doing this heat load to cooling tower is reduced, the equivalent amount of heat load is being used for washing section pre heater has been reduced, and also cooled condensate injection pump to column has be isolated.

Investment made : Zero Investment

Benefit achieved :❖Annual water saving – 242 KL❖ Annual thermal energy savings – 142.3 Mkcal❖ Total cost savings – 2.02 Lakh

Pay back Period: -

Page 21: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

8. Utilization of renewable energy source

Onsite Solar farm-2

93.6kWh

OnsiteSolar Farm- 1

156kWh

We have Bio- Mass Operated Captive

Power Plant2MW

Installed in KPL Site

Page 22: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

8. Utilization of renewable energy source (Last three years)

7.5%

90.1%

2.5%

Power source FY19

EB/DG

Biomass

Solar

2.3%

95.4%

2.3%

Power source FY20

EB/DG

Biomass

Solar

❖We produce and consume around 92% of our

own power requirement through renewable energy

resource (Solar + Bio mass)

7%

90%

2% 1%

Power source FY-21

EB/DG

Biomass

Solar

Coal

Page 23: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

9. Utilization of waste material as fuel

Waste Utilization:❖ OFF Gas recovery system was implemented, recovered and reused for TFH System.❖ Earlier TFH system was run by FO.❖ OFF Gas recovery and utilization was gradually increased in 56% Plan FY22:❖ Implementation of complete OFF gas recovery system inclusive of pump drain, coalescer drain..etc.

0

100

200

300

400

500

600

700

800

900

FY-19 FY-20 FY-21

388.8

624.6

890.5

OFF Gas recovery MTA

0.0

100.0

200.0

300.0

400.0

500.0

600.0

700.0

800.0

900.0

1000.0

FY-19 FY-20 FY-21

413.8

664.8

947.7

Energy Recovery toe/Annum Increased By 56%

Page 24: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

Green Go Project

Project Implemented : HPIB Purchase

Description:

❖ Earlier procurement concentration of C4 raffinate is 33%

❖ Now the procurement concentration of C4 raffinate is 99%

❖ Number of round trip got reduced- 1700 No’s

Investment made : Zero Investment

Benefit achieved :

❖ CO2 emission reduction- 6551.5 MT/Year

Page 25: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

10. GHG Emission Intensity and Verification (Last Three Years)

❖ Total GHG intensity reduction is 2.5%

0.000

0.100

0.200

0.300

0.400

0.500

0.600

0.700

FY-19 FY-20 FY-21

0.645

0.568

0.415

Power- CO2 Emission MT/MT

0.000

0.050

0.100

0.150

0.200

0.250

0.300

0.350

0.400

0.450

FY-19 FY-20 FY-21

0.379

0.319

0.450

Thermal CO2 Emission MT/MT

0.750

0.800

0.850

0.900

0.950

1.000

1.050

FY-19 FY-20 FY-21

1.024

0.8870.865

Total CO2 Emission (Thermal + Power) MT/MT

Reduced By 26%

Increased By 29%

Reduced By 2.5%

Page 26: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

10. GHG Emission Intensity Reduction Plan

CO2 Emission Reduction MT/MT

Short term goals:❖ Implementing complete OFF Gas recovery system❖ Conducting Insulation efficiency survey❖ Increasing the Productivity with in House trials.❖ Increasing waste heat recovery across the plant.

Long term goals:❖ Converting Fuel Bio Mass to Clean Fuel (LNG)❖Conducting comprehensive energy audit (3rd Party)❖ Increasing the productivity with the help of De Bottleneck.

0.000

0.200

0.400

0.600

0.800

1.000

1.200

FY-19 FY-20 FY-21 FY-22 FY-23

0.645 0.5680.415 0.380 0.350

0.379

0.3190.450

0.3950.365

CO2 Emission reduction MT/MT

CO2-Power Sp.Consumption CO2 Emission- Thermal

Reduction By 18%

Page 27: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

10. Fly Ash Utilisation

❖ Bio Mass Operated boiler Fly Ash Disposed to Fly ash Brick Manufacturers

Disposal : 100% Daily generation of Fly ash disposed to Fly ash Manufacturer.

❖ Mode of Disposal: Closed Container.

❖ Environmental Benefit: 100% recycle to eco friendly Brick making

Page 28: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

12. KPL Energy Cell

Top Management

Energy Manager

Administrative Department

Technical Service Department

Finance Department

Energy management committee

Production In-charge

Plant Maintenance

Page 29: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

12. Energy Team Work- National Energy Conservation Day Celebration

ENERGY BEST SUGGESTION: Mr. PANDIYANCOALESCER INSULATION PROVISION TO AVOID HEAT RADIATION

ENERGY BEST SUGGESTION: Mr. ARUL MURUGANPUSH TYPE TAP FOR DRINKING WATER TO AVOID WATER LOSS

Page 30: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

“7QC Tools”3 Day’s External workshop conducted Cost Impact of Leak

Energy Training- Importance of energy conservation in industriesBest Engineering Practices- “Using Ultra Sound”

Description Value

Total Number of training provided- In House Training

05

Total Number of training provided- By ExternalTraining

02

Total number of training participants 52

Total number of man hour training completed 98

12. Energy Team Work

Energy Cell Activity

Energy Training and Development

Leak Identification program

Description Value

Total steam leak identified across ISBL 17

Total steam leak arrested - Completed 16

Number of steam leak required Shutdown 01

Cost saving in Steam leak arresting (Rs/Day) 3314

Page 31: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

12. Energy Team Work- “GREEN GO” Cycling event Organized

Page 32: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

13. Implementation of ISO 50001

❖KPL Have Combination of ISO 9001, 14001,

45001 as IMS in Place.

❖We are way forward to implement ISO 50001:

2018 By End of FY-23; Measures are in place to

convince management.

0.00%

0.05%

0.10%

0.15%

0.20%

0.25%

0.30%

FY-19 FY-20 FY-21

0.06%

0.01%

0.27%

Inve

stm

en

t %

Turnover vs. Enery Project Investment %

Increased By 17%

Page 33: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

13. Learning From CII Energy Award 2020

❖ Through CII- Energy award-2020 we have learned some of best engineering practices, are implemented in our site

and got positive result of energy saving; Some of

Ultrasound leak detection survey :❖ Instrument air leak reduction❖Nitrogen leak reduction.❖Fugitive emission reduction (Hydrocarbon leak from process)❖Steam trap testing.

Thermal and Insulation survey :❖ Thermal and Insulation survey instrument procured and schedule has been followed.

Page 34: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …

Thank you

CONTACT DETAILS:Mr. Anand B R – Sr. Manager- TLSMain ID: [email protected]. No: +91 7299044611

CONTACT DETAILS:Mr. Srinivasan K S – AGM Maintenance / Energy CellMain ID: [email protected]. No: +91 7299044605

Page 35: CII- 22nd NATIONAL AWARD EXCELLENCE IN ENERGY …