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19th National Award for Excellence in
Energy Management-2018
Fortis Hospital Vasant Kunj
FHVK- BRIEF INTRODUCTION Fortis Hospital FHVK was established
in 2006, and has built up recognition as foremost super specialty Hospital
FHVK is a 150 bedded, NABH, NABL,GREEN OT certified Super specialty tertiary care hospital,
Fortis is accredited with NABH, has platinum grade Green OT certification and awarded best nursing excellence award
Services Location
• OPD Block (Basement)/ Ground floor
• IPD Block (1st & 2nd Floor
• OT & ICU (3rd Floor)
• Pathology (4th & 5th Floor)
Energy Management Structure
National Head EnergyMr. Ravi Adlakha
Head Engg. Unit Vasant Kunj
Mr. Subhash Jha
Head Engg.Unit Mohali
Mr. Neeraj Tandon
Head Engg. Other Units
Various Units Teams
2014-15 2015-16 2016-17 2017-18
4348178 4068661 3777413.5 3640770.8
Power consumption trend 2014-18
Energy Usage
EquipmentAve.
Consumption
HVAC (heating, ventilation, & air conditioning)
55-65%
Lighting 7-10%
Medical Equipment 10-15%
Boilers 2-3%
Water Systems 3-5%
Medical Gases 01- 02%
STP (sewage treatment plant) 2-3%
ENERGY ANALYSIS
Parameter 2014-15 2015-16 2016-17 2017-18
Specific Energy Consumption in
kWh/M2/annum 252 236 219 211
Total kWh/Bed 28987 27124 25182 24271
No. Of Beds 150 150 150 150
Area of building 17232 17232 17232 17232
Chiller TR KW/TR
Trane 250 0.65
Clivet 175 1.1
Replacement of clivet chiller by VFD Trane chiller
Trane chiller
Adaptive Frequency
Drive
The largest energy user in most buildings
is the chilled water system. The RTHD Adaptive
Frequency Drive, from Trane Care Energy Services,
can make significant savings in the energy
consumed.
Trane Chiller VFD
Adaptive Frequency Drive Overview
A powerful upgrade that
delivers
1.Precision control
2.Energy efficiency
3.Lower utility costs
4.Noise reduction
5.Longer equipment life
Performance
Up to 35% better energy efficiency at all load points
Trane AFD reduces electricity bills by improving chiller
efficiency at reduced load, while at same time meeting
the building’s cooling requirements. The combination
of Trane chiller capacity control and Adaptive
Frequency Drive will improve chiller efficiency up to
35%.
Benefits
Benefits
• Low load capability
• Unloading capabilityRTHD : 20%
RTHD AFD: 12%
Reduces start-stop cycles by enabling the chiller to
operate at lower capacities.
For chiller operating at low loads (comfort application)
stop/start will be reduced by ~45%
Benefits
Benefits
• Lower inrush current
• Starting current reduced by 5
Helpful for application experiencing
disruption when starting many electric
devices at same time.
Starter type Inrush current (% Imax)
Direct in line 600 - 800%
Wye Delta 200 – 275%
Solid State 300 - 500%
AFD <100%
Maintenance in existing Air- conditioning system for better Efficiency
Air Handling Unit:• Cooling Coil efficiency – by cleaning with proper cleaning
agent at regular interval. Use of UV light to reduce bacteria growth in the coil.
• Fan efficiency
Cooling Tower (for water-cooled system)• Proper spray of water
• Clean of fills
• Proper adjustment of fan blades.
• Use of water bleed off for circulation water
• Only soft water to be used for make up to reduce fouling in the condenser .
National Bench mark 17762 KWh/Bed per annum (reference Bureau of Energy Efficiency, Govt. of India ECO-III project)
14
0
5000
10000
15000
20000
25000
30000
2014-15 2015-16 2016-17 2017-18 Bench Mark
28987
27124 25182
24271
17762
KWH/Bed
2014-15
2015-16
2016-17
2017-18
Bench Mark
National Bench mark 17762 kwh / Bed per annum Reference ECO III serve
KWH / SQM
2014-15 2015-16 2016-172017-
18
252 236 219 211
Specific power consumption
LIST OF ENCON PROJECTS IMPLEMENTED IN 2015-16
Sr. No. PROJECT
Annual Savings Achieved
INVESTMENT (in Lac)
ROI (Months)
KWHINR
(lacs)
2015-16
250 TR Trane chiller installed. 223613 22.80 38.00 20
Conventional CFL replaced with LED 55903 5.7 6.48 11.44
Total 279516 Units , Rs. 2851063
Energy saving activity 2016-17
Sr. No. PROJECT
Annual Savings Achieved
INVESTMENT (in Lac)
ROI (Months)
KWHINR
(lacs)
2016-17
Replacement of 4 Nos. split Ac with FCU. 37324 3.80 1.0 3.15
Conventional light replaced with LED 171247.5 17.46 17.28 11.87
Total 208571.5 Units , Rs. 2126724.5
LIST OF ENCON PROJECTS IMPLEMENTED IN 2017-18
Sr. No. PROJECT
Annual Savings Achieved
INVESTMENT (in Lac)
ROI (Months)
KWHINR
(lacs)
2017-18
Descaling of chiller plant to maintain the approach below 4 Deg. Fahrenheit
74000 7.54 0.22 0.34
Conventional CFL replaced with LED 62595.7 6.38 6.48 12.12
Total 13659.7Units , Rs. 1393276.14
Energy Consumption Trend
Remarks– New MRI machine installed increased 750 kw / month of load, our
energy conservation effectively neutralizes the upward consumption trend.
ENERGY MEASUREMENT,MONITORING & REPORTING
•Dedicated energy Meters for all the panels
•Separate energy meters for lighting, HVAC
•Record of daily energy meter recording
•Annual calibration of all energy meters.
•Monthly review of energy balancing by energy
Management Cell
Waste Reduction
• Mixture Tap nozzle fixed in OPD area washroom to reduce the waterconsumption approx 500 KL monthly
• Hand Dryier fixed in OPD wash room to reduce the paper consumption upto 15 %
• Paper saving by Using both sides of paper while printing also reuse old papers for inter office work.
• X-Ray films eliminated using PACS systems through IT.
• On line soft wares are used for office work like oracle, my Fortis,out look, Patient Portal ,QMS etc. Resulting saving of papers
Implementation on Energy, Water & Environment
BY maintaining of Power factor above 0.99Regular de-dusting of lighting fixture.Cleaning of filters in air conditioning system.Maintaining the optimum voltage of lighting systemSwitching off lights/monitors/AC when not in use.Use of high –efficiency fixtures (water closet & urinal) to reduce the potable water demand.Raw and treated sewage quality monitoring on daily basis and Quaterly report to be submit to DPCC. water meter to be measured on daily basis for the water consumption control. Conducting Daily inspection walkthroughs for identification of any water losses.Use of separate storm , sewage and oil water separators drainages to avoid ground water contamination.Celebration of Environmental day, Engineers day etc.
corrective/preventive action for better efficiency
• Routine preventive maintenance and Calibrations and testing of equipment,
on yearly basis
• Realignment of lighting with respect to the lumen , corridors, staircases & IPD OPD rooms
• Running only one Transformer during non peak season when the load goes down .
• Installation of VFDs
• Monthly CFM measurement to check the Hepa filter efficiency and replacement when the efficiency comes down
Initiatives
Solar water heatingOutcome: • Fuel oil consumption reduced by Hot water
generator after installation solar water heating
system
Rain water harvesting pitsOutcome:
• 2Nos of rain water harvesting pits improves
the ground water
Utilization of Waste Materials
• STP Water is reused in gardening, Irrigation and in cooling towers, .
• Newspaper & waste papers are sent to authorized person , for recycling.
• Plastic, Polythene is sent for recycling.
• Kitchen waste is being given for making fuel .
• Used Engine oil & lubricant materials are sent to Authorized
recyclers.
Operation and maintenance practices Categories Remark
Authorized O& M vendor for all equipment Available
Daily monitoring of energy consumption as compared to the last year same day
Available
Training to motivate the staff for energy saving Available
Half yearly performance check of all equipment's Like DGs, chillers , UPS etc
Available
Preventive maintenance of all the equipment for maintaining the efficiency
Available
Reduction of diesel consumption by the reduction of DG testing time on daily basis
Available
Monthly energy saving meeting with the dept. Available
Use of renewable energy for day to day operations In progress
WHERE WE ARE TODAY
Benchmarks :- 200 KWh/m2
(By Bureau of Energy Efficiency,
Govt of India ECO-III project)
EMPLOYEE INVOLVEMENT /TEAM WORK • Suggestion from all levels of employees on
energy conservation
• Training/Awareness for contract labour/office staff on energy conservation.
• Sharing best practices among the industries
• Objective are set for employees on reduction in energy and water .
• To adopt safe and hygienic hospital
procedures and practices
• Environmental safety and fire fighting training sessions
• Hand Hygiene campaign launched and Emphasis on 5S initiative
• Trainings imparted and monitoring done on Energy Conservation measures.
• Energy savings Efficiencies of Boiler, DG sets and HVAC are regularly monitored for timely maintenance and energy savings.
GREEN INITIATIVE
• We have solar water heating system to used the non-conventional energy resources for hot water of the hospital.
• Under discussion to have solar electricity system for the electricity power supply of the hospital.
Reduction of CO2 in MT
Replaced kone lift with hyundai
Type Amp KWH/YearSaving KWH
Saving Rs Investment ROI
Kone 30 83838 33534342046 2600000 91.2
Hyundai 18 50303
• Reduction of water consumption of 2016-17 to 2017-18 by 7499.5 KL yearly due to fixing of nozzle into taps of mixture in general wash room & nursing station area along with sensor operated taps.
• Total annual saving Rs. - 7 Lacs
water consumption trend
• Diesel consumption reduced by optimum utilization of solar water heater.
Diesel consumption of Hot Water Generators 2016-2018
FUTURE PLAN
20
17
-18
Total Existing CFL(KWH)
Total Existing LED(KWH)
Savings (kWh)
Savings (INR in Lacs)
Investment (In Lacs)
ROI (Years)
189864 92739 97125 9.90 14.38 1.74
LED light replacement with conventional CFL
FUTURE PLAN
Sr. No.Hot water generator conversion into PNG
Proposed consumption
Saving /YearINVESTMENT
(in Lac) ROILiters/
YearAmount
20
17
-18
HSD consumption/ Year
26455 1666667
3684921000000
32.56PNG consumption/ Year 27045 1298174
Conversion of hot water generator into PNG
Future Plan
• Replacement of old chiller plant with energy efficient chiller
• Replacement of conventional pump with energy efficient pump
• Re-insulation of chilled water line After testing the insulation by thermography equipment to reduce the losses
• Fixing of sun film towards the sun facing area of the hospital
• Installation of heat pump for the energy saving after completion of energy audit
• Replacement of Old kone lift with energy efficient lift
• Complete water and air balancing for the air conditioning system to reduce the losses.
• To start the solar energy.
Cost benefit analysis hot water generatorS no. HOT WATER GENERATOR Unit HSD PNG
1 Capacity in Kcal/hr Kcal/hr 200,000 200,000
2 Actual load Kcal/hr 200,000 200,000
3 Efficiency NCV % 90% 87%
4 Cal val. Of Fuel kcal/kg or NM3/hr 10500 8500
5 Fuel cost Rs/lit or Rs/kg 63.00 48.00
6 Fuel Consumption Kg/hr 21.16 27.05
7 Density of Fuel kg/lit 0.8 1
8 Fuel Consumption lit or kg/hr 26.46 27.05
9 Fuel Cost per Hour Rs/hr 1666.67 1298.17
10 No. of hrs operation in an year hrs 1000 1000
11 Total Fuel Cost Rs/year 1666667 1298174
12 Net saving/year 368492
Existing CFL Tube light fixtureConversion of CFL(conventional Light) with LED
S. NoType of fixture
QuantityTotal watts
Rate/unitR/Hours(
AVG)KW
Total unit/day in KWH
Amount/day
Amount/month
Annual
1 1x18WCFL 215 3870 10.2 15 3.87 58.05 592.11 17763.3 213159.6
2 2x18W CFL 174 6960 10.2 15 6.96 104.4 1064.88 31946.4 383356.8
3 2x36W CFL 67 5360 10.2 15 5.36 80.4 820.08 24602.4 295228.8
4 3x36WCFL 25 3000 10.2 15 3 45 459 13770 165240
536WTube
light325 13000 10.2 15 13 195 1989 59670 716040
618 W Tube
light135 2970 10.2 15 2.97 44.55 454.41 13632.3 163587.6
Total 527.4 5379.48 161384.4 1936613
Total Unit/year
189864
LED light replacement planLed light details
S.no
Type of fixtureQuantity
Total watts
Rate/unit
R/Hours(AVG)
KWTotal unit/day
in KWHAmount/
dayAmount/
monthAnnual
118 W CFL replaced with
12 W215 2580 10.2 15 2.58 38.7 394.74 11842.2 142106.4
218x2W CFL replaced with
12x2 W LED174 4176 10.2 15 4.176 62.64 638.928 19167.84 230014.1
32x36 WCFL replaced with
40 W LED67 2680 10.2 15 2.68 40.2 410.04 12301.2 147614.4
43x36WCFL replaced with
3x18W LED25 1350 10.2 15 1.35 20.25 206.55 6196.5 74358
536W tube light replaced
with 18 W LED325 5850 10.2 15 5.85 87.75 895.05 26851.5 322218
618W Tube light replaced
with 10W LED135 1350 10.2 15 1.35 20.25 206.55 6196.5 74358
Total Unit
269.79 2751.85 82555.74 990668.9
Total Unit/yea
r97124.4
Net Saving
Amount
1936613 -990668=945943.9
Thank You