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    Molded Coil Endcaps Coil Stage Design Completed Endcaps

    After the end caps were completed, they were positioned along

    the barrel and holes were drilled so the IR detector beams could

    shine across the barrel. Then the coils were wound carefully in

    between the end caps with the aid of my vice grip. Each inner coil

    layer is secured with a single layer of packing tape.

    Placement of Coil

    Endcaps

    Coil Winding Completed Coils

    Construction

    End Caps

    The first components to be constructed were the magnetic coil end caps. Mixing and molding the iron-epoxy compound was challenging to

    say the least. The mixture ratio has to be just right. If theres too much epoxy, the end cap wont be ferrous enough and might as well be a

    chunk of plastic. If theres too much iron, the piece will conduct eddy currents and possibly crack when coming out of the mold. Also, the

    right amount of compression has to be applied to the mold- too much compression will cause the epoxy to ooze out, leaving an overly

    iron-rich piece inside. I had to make 16 end caps to get 9 that were good- meaning I had a 56% success rate with this process. Each

    piece took 48 hours to dry, making the effort long and frustrating. Lastly, the end caps were fitted with brackets to mount the infrared

    projectile sensors and coil magnet wire.

    Coils

    Projectiles

    An advantage to using steel nails as projectiles is the ease of fabrication, which is a huge plus when you need to make twenty of them.

    Each projectile was simply measured, cut, and filed into shape. Maintaining a precise length was important to insure that each projectile

    extends far enough to trip the first stage IR trigger when pushed out o f the magazine.

    Finished Projectiles

    Initial Testing

    struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr

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    components used to switch the coils on and off. Two thick copper

    bus bars connected to the battery terminals run the length of the

    housing down either side. Between the copper rails are the eight

    IGBTs, one to switch each coil. Between each IGBT is a small

    circuit board containing the voltage suppression electronics.

    Initially, each voltage suppression circuit board contained four

    series diodes, which I mistakenly thought was the fastest way to

    quench the coil current. Later, I learned that the single

    diode/resistor method was much faster, so each circuit board was

    removed and upgraded. Lastly, each stage has a red LED that

    lights when the IGBT is conducting. This provides a fault indicator

    if a coil is erroneously switched on as well as a cool racing LED

    effect during each shot.

    IGBTs Installed Copper Busbar Fabricated Busbars Installed

    Switch Indicator LED

    Early Voltage Suppression

    Circuit Boards

    Circuit Boards Installed

    Frame

    The gun frame had to be built twice. The first attempt was based on a design that just

    couldnt be built with hand tools, so I redesigned it to use pre-existing aluminum cross-

    sections to minimize parts, cuts and joints. The second design was stronger and easier

    to build, but several parts still had to be redone once, twice, and even three times until I

    had something that was solid and respectable. By the time the aluminum frame was

    complete and ready to accept the gun components, I had probably ingested more

    aluminum sawdust than a healthy human being ever should, but it was worth it. The

    final product is extremely rigid and sturdy, with no rattles or creaking even when tested

    under heavy loads (such as when I accidentally ran into it head-first while vacuuming the

    floor one day).

    Lots of additional components were built into the frame. The pistol-grip and trigger are hugely improved from the CG-33. The ergonomic

    grip is solidly bolted into the frame, and the trigger pulls smoothly and comes to a confident stop just as the shot is triggered. The select

    fire switch, power switches, battery monitor LEDs, circuit board mounting brackets, safety fuses and a targeting laser were all designed,

    built, redesigned and rebuilt and mounted into the frame during this phase as well.

    struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr

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    Foregrip Cut Vicegrip Used as Brake Completed Foregrip

    Led Panel Battery LEDs Installed Modified Laser Pen

    Laser, Switches & Fuses Grip & Trigger Completed Gun Frame

    Circuit Boards

    A circuit that makes perfect sense on paper wont work when you simulate it, and a

    circuit that works perfectly in a simulator wont work when you test it on a breadboard,

    and a circuit that works perfectly on a breadboard wont work once you solder it

    together. Then you spend three weeks troubleshooting it, only to find that it starts

    working again for no reason at all. Thus went the process for the CG-42s circuit boards.

    In the end, everything worked out. The layouts of all the circuit boards were sketched on

    paper before-hand to fit into their small spaces while remaining neat and organized.

    Cramped, messy circuit boards make it easy for shorts and loose connections to occur.

    When your circuits are connected to two giant flammable batteries that you hold right

    next to your face when you shoot the gun, thats some pretty serious business.Power Supply Circuit Board

    Projectile Feed System

    This was a challenge to build, as moving parts usually are. For

    the coilgun to operate reliably, the projectile feed system will have

    to operate smoothly and consistently even when actuated 10

    times per second. The difficulty began with the magazine. Two

    magazines, three followers and four magazine springs were

    designed, built, and failed before I came to a good design thatcould feed the projectiles without jamming. The first magazine was proven wrong with my hammer.

    The final magazine is built from bended aluminum sheets joined

    with epoxy, and the spring was manually bent from steel wire.

    Instead of using a mechanical latch, the magazine is held in place

    by a Neodymium magnet.

    The injector solenoid required some modification to get it to

    function properly. The stock return spring didnt provide enough

    force to retract the solenoid to its starting position when subjected

    to friction against the spring-loaded projectiles. Using two stock

    Final Magazine Stenciled

    on Aluminum

    Magazine Plate Cut Out Magazine, Follower, and

    Base Plate

    struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr

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    springs provided enough force, but the action was mushy and

    inconsistent. Using a trick from freshman physics lab, I measured

    the springs force constant and purchased a new single spring that

    provided double the force. This fed the projectiles much more

    reliably. After some time spent adjusting the positioning and

    stroke-length of the solenoid, I finally had a mechanism capable of

    sustaining full-auto projectile feed.

    Spring Bending

    Assembled Injector

    Mechanism

    Injector in Aluminum

    Housing

    Final Testing

    After many months spent connecting all of the components together and troubleshooting all sorts of problems, the whole coilgun was

    assembled and ready to go. The first full-power test shots were fired on July 1st, 2013. The first shot was a success. Immediately after

    the second shot, the IGBT controlling the first stage failed dead-short and exploded. The battery fuse failed to trip, allowing the first stage

    coil to melt and burn quite thoroughly. The entire incident can be observed below:

    After making th is video I was so amped up on science I couldnt sleep until two in the morning

    Fortunately, the circuit board fuses worked properly and protected the rest of the components. The cause of IGBT failure was later

    determined to be excessive voltage allowed by a blown resistor in the voltage suppression circuit. The first stage coil had to be replaced,

    and all eight voltage suppressors were refitted with higher wattage resistors to widen the safety margin. Thanks to requirement 4

    (maintainability) the repairs were quick and the gun was back up and running in less than two weeks. The results of the full performance

    characterization are shown below.

    struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr

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    Final Testing Results

    With a total efficiency of 7.0% the results are extremely pleasing (compared to a typical 2% coilgun). As expected, performance had

    improved since initial testing. This is due to the resistors that I added to the voltage suppression circuits to quench the coil current more

    quickly. This drastically reduces suck-back, especially in later stages where the projectile is moving very fast. The efficiency of the first and

    last coils dropped (relative to the other stages), likely due to induction of eddy currents in the aluminum gun frame which the first and last

    coils are now mounted into. As to what causes the performance drop on the 6th stage, I have no theories. Oddly, looking back at the initial

    test with 7 stages, the 3rd-to-last stage performed low as well.

    Completion

    After an eternity of sawing, filing, drilling and soldering I suddenly realized that there was nothing left to be done and the gun was finished.

    Somehow everything turned out better than I expected, from the appearance of the gun to the performance numbers. All of the goals were

    met, except rate of fire which came in at 7.7 rounds/sec. This could be increased by changing a single resistor, but I chose to keep it this

    way since the coils wont hea t up as quickly.

    The battery powered coilgun equation was remarkably accurate in determining the power required. This is because the actual acceleration

    of the projectile was very close to being constant, which was the key assumption of that equation. The efficiency guess (6-10%) was also

    fairly close. However, the 40m series resistance prediction was way off- actual series resistance was closer to 100m due to

    unexpectedly high internal resistance within the battery cells. The coils only get about 190A instead of the 300A I planned for, but since

    the 300A was way over-designed, the coils still get enough current to meet the projectile power demands. This means I could have gotten

    away with using the smaller 2500mAh batteries, but the bigger batteries provide the advantage of being able to power far more shots.

    While testing and making the video, I put about 100 rounds through the gun and the batteries only dropped from 50.20 to 49.03V. I could

    probably fire several hundred more rounds before the batteries drain to the minimum 36V and need a recharge.

    In the end, Im very happy with how it turned out. Holding the gun makes you feel like a mad scientist, and firing full-auto bursts gives the

    shooter a terrifying sense of excitement and destructive power. Project complete!

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    struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr