Upload
scribdtaker12345
View
214
Download
0
Embed Size (px)
Citation preview
8/12/2019 gausmg2
1/6
Molded Coil Endcaps Coil Stage Design Completed Endcaps
After the end caps were completed, they were positioned along
the barrel and holes were drilled so the IR detector beams could
shine across the barrel. Then the coils were wound carefully in
between the end caps with the aid of my vice grip. Each inner coil
layer is secured with a single layer of packing tape.
Placement of Coil
Endcaps
Coil Winding Completed Coils
Construction
End Caps
The first components to be constructed were the magnetic coil end caps. Mixing and molding the iron-epoxy compound was challenging to
say the least. The mixture ratio has to be just right. If theres too much epoxy, the end cap wont be ferrous enough and might as well be a
chunk of plastic. If theres too much iron, the piece will conduct eddy currents and possibly crack when coming out of the mold. Also, the
right amount of compression has to be applied to the mold- too much compression will cause the epoxy to ooze out, leaving an overly
iron-rich piece inside. I had to make 16 end caps to get 9 that were good- meaning I had a 56% success rate with this process. Each
piece took 48 hours to dry, making the effort long and frustrating. Lastly, the end caps were fitted with brackets to mount the infrared
projectile sensors and coil magnet wire.
Coils
Projectiles
An advantage to using steel nails as projectiles is the ease of fabrication, which is a huge plus when you need to make twenty of them.
Each projectile was simply measured, cut, and filed into shape. Maintaining a precise length was important to insure that each projectile
extends far enough to trip the first stage IR trigger when pushed out o f the magazine.
Finished Projectiles
Initial Testing
struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr
6 08/19/2013 03
8/12/2019 gausmg2
2/6
8/12/2019 gausmg2
3/6
components used to switch the coils on and off. Two thick copper
bus bars connected to the battery terminals run the length of the
housing down either side. Between the copper rails are the eight
IGBTs, one to switch each coil. Between each IGBT is a small
circuit board containing the voltage suppression electronics.
Initially, each voltage suppression circuit board contained four
series diodes, which I mistakenly thought was the fastest way to
quench the coil current. Later, I learned that the single
diode/resistor method was much faster, so each circuit board was
removed and upgraded. Lastly, each stage has a red LED that
lights when the IGBT is conducting. This provides a fault indicator
if a coil is erroneously switched on as well as a cool racing LED
effect during each shot.
IGBTs Installed Copper Busbar Fabricated Busbars Installed
Switch Indicator LED
Early Voltage Suppression
Circuit Boards
Circuit Boards Installed
Frame
The gun frame had to be built twice. The first attempt was based on a design that just
couldnt be built with hand tools, so I redesigned it to use pre-existing aluminum cross-
sections to minimize parts, cuts and joints. The second design was stronger and easier
to build, but several parts still had to be redone once, twice, and even three times until I
had something that was solid and respectable. By the time the aluminum frame was
complete and ready to accept the gun components, I had probably ingested more
aluminum sawdust than a healthy human being ever should, but it was worth it. The
final product is extremely rigid and sturdy, with no rattles or creaking even when tested
under heavy loads (such as when I accidentally ran into it head-first while vacuuming the
floor one day).
Lots of additional components were built into the frame. The pistol-grip and trigger are hugely improved from the CG-33. The ergonomic
grip is solidly bolted into the frame, and the trigger pulls smoothly and comes to a confident stop just as the shot is triggered. The select
fire switch, power switches, battery monitor LEDs, circuit board mounting brackets, safety fuses and a targeting laser were all designed,
built, redesigned and rebuilt and mounted into the frame during this phase as well.
struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr
6 08/19/2013 03
8/12/2019 gausmg2
4/6
Foregrip Cut Vicegrip Used as Brake Completed Foregrip
Led Panel Battery LEDs Installed Modified Laser Pen
Laser, Switches & Fuses Grip & Trigger Completed Gun Frame
Circuit Boards
A circuit that makes perfect sense on paper wont work when you simulate it, and a
circuit that works perfectly in a simulator wont work when you test it on a breadboard,
and a circuit that works perfectly on a breadboard wont work once you solder it
together. Then you spend three weeks troubleshooting it, only to find that it starts
working again for no reason at all. Thus went the process for the CG-42s circuit boards.
In the end, everything worked out. The layouts of all the circuit boards were sketched on
paper before-hand to fit into their small spaces while remaining neat and organized.
Cramped, messy circuit boards make it easy for shorts and loose connections to occur.
When your circuits are connected to two giant flammable batteries that you hold right
next to your face when you shoot the gun, thats some pretty serious business.Power Supply Circuit Board
Projectile Feed System
This was a challenge to build, as moving parts usually are. For
the coilgun to operate reliably, the projectile feed system will have
to operate smoothly and consistently even when actuated 10
times per second. The difficulty began with the magazine. Two
magazines, three followers and four magazine springs were
designed, built, and failed before I came to a good design thatcould feed the projectiles without jamming. The first magazine was proven wrong with my hammer.
The final magazine is built from bended aluminum sheets joined
with epoxy, and the spring was manually bent from steel wire.
Instead of using a mechanical latch, the magazine is held in place
by a Neodymium magnet.
The injector solenoid required some modification to get it to
function properly. The stock return spring didnt provide enough
force to retract the solenoid to its starting position when subjected
to friction against the spring-loaded projectiles. Using two stock
Final Magazine Stenciled
on Aluminum
Magazine Plate Cut Out Magazine, Follower, and
Base Plate
struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr
6 08/19/2013 03
8/12/2019 gausmg2
5/6
springs provided enough force, but the action was mushy and
inconsistent. Using a trick from freshman physics lab, I measured
the springs force constant and purchased a new single spring that
provided double the force. This fed the projectiles much more
reliably. After some time spent adjusting the positioning and
stroke-length of the solenoid, I finally had a mechanism capable of
sustaining full-auto projectile feed.
Spring Bending
Assembled Injector
Mechanism
Injector in Aluminum
Housing
Final Testing
After many months spent connecting all of the components together and troubleshooting all sorts of problems, the whole coilgun was
assembled and ready to go. The first full-power test shots were fired on July 1st, 2013. The first shot was a success. Immediately after
the second shot, the IGBT controlling the first stage failed dead-short and exploded. The battery fuse failed to trip, allowing the first stage
coil to melt and burn quite thoroughly. The entire incident can be observed below:
After making th is video I was so amped up on science I couldnt sleep until two in the morning
Fortunately, the circuit board fuses worked properly and protected the rest of the components. The cause of IGBT failure was later
determined to be excessive voltage allowed by a blown resistor in the voltage suppression circuit. The first stage coil had to be replaced,
and all eight voltage suppressors were refitted with higher wattage resistors to widen the safety margin. Thanks to requirement 4
(maintainability) the repairs were quick and the gun was back up and running in less than two weeks. The results of the full performance
characterization are shown below.
struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr
6 08/19/2013 03
8/12/2019 gausmg2
6/6
Final Testing Results
With a total efficiency of 7.0% the results are extremely pleasing (compared to a typical 2% coilgun). As expected, performance had
improved since initial testing. This is due to the resistors that I added to the voltage suppression circuits to quench the coil current more
quickly. This drastically reduces suck-back, especially in later stages where the projectile is moving very fast. The efficiency of the first and
last coils dropped (relative to the other stages), likely due to induction of eddy currents in the aluminum gun frame which the first and last
coils are now mounted into. As to what causes the performance drop on the 6th stage, I have no theories. Oddly, looking back at the initial
test with 7 stages, the 3rd-to-last stage performed low as well.
Completion
After an eternity of sawing, filing, drilling and soldering I suddenly realized that there was nothing left to be done and the gun was finished.
Somehow everything turned out better than I expected, from the appearance of the gun to the performance numbers. All of the goals were
met, except rate of fire which came in at 7.7 rounds/sec. This could be increased by changing a single resistor, but I chose to keep it this
way since the coils wont hea t up as quickly.
The battery powered coilgun equation was remarkably accurate in determining the power required. This is because the actual acceleration
of the projectile was very close to being constant, which was the key assumption of that equation. The efficiency guess (6-10%) was also
fairly close. However, the 40m series resistance prediction was way off- actual series resistance was closer to 100m due to
unexpectedly high internal resistance within the battery cells. The coils only get about 190A instead of the 300A I planned for, but since
the 300A was way over-designed, the coils still get enough current to meet the projectile power demands. This means I could have gotten
away with using the smaller 2500mAh batteries, but the bigger batteries provide the advantage of being able to power far more shots.
While testing and making the video, I put about 100 rounds through the gun and the batteries only dropped from 50.20 to 49.03V. I could
probably fire several hundred more rounds before the batteries drain to the minimum 36V and need a recharge.
In the end, Im very happy with how it turned out. Holding the gun makes you feel like a mad scientist, and firing full-auto bursts gives the
shooter a terrifying sense of excitement and destructive power. Project complete!
Return to Overview
Delta-V Engineering| Powered by Mantra& WordPress.
struction - Delta-V Engineering http://www.deltaveng.com/gauss-machine-gun/constr