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IMPROVEMENT PROJECT FOR THE
AUTOMOTIVE A/C MUFFLE ASSEMBLY
Project Leader Denis Sexton
Page 2
D CIAM
In late 2000, after a Pareto Analysis at a automotive A/C
manufacturing plant, the first time quality reject rate (FTQ)
was the highest and most costly in the brazing furnace cell.
A cross functional team was initiated to investigate the
problem.
Team members & roles
CM : Production Team Leader
SR : Manufacturing Engineer
RT : Production Manager
DN : Quality Manager
DS : Engineering Black Belt / Mentor
Introduction
Page 3
Pareto of FTQ Problems in Manufacturing Plant -
2000
05
10152025303540
Muf
fler B
raze
Are
a
Crim
p Diam
eter A
C 1
Crim
p Diam
eter A
C 2
Valve
Inse
rtion
Crim
p Diam
eter P
S 1
Crim
p Diam
eter P
S 2
Oth
er
Source
% D
efe
cti
ve o
f P
lan
t
To
tal
0
20
40
60
80
100
120
Cu
m.F
req
%.
FREQUEN.
CUM.FREQ.
D CIAMStep A: Identify Project CTQs
CTQ = FTQ = Cost Reduction
Page 4
Step A: Identify Project CTQs D CIAM
Pareto of FTQ Problems in Muffler Brasing Process -
2000
05
1015202530354045
Muf
fler j
oint lea
ks
Exc
ess
braz
e us
ed
Hand
ling
Dam
age
Maint
enanc
e Issu
es
Sup
pler I
ssue
A
Sup
pler I
ssue
B
Oth
er
Source
% D
efe
cti
ve o
f P
rocess
To
tal
0
20
40
60
80
100
120
Cu
m.F
req
%.
FREQUEN.
CUM.FREQ.
CTQ = FTQ = Cost Reduction
Page 5
D CIAMStep A: Identify Project CTQs
Muffle
Assembly
unit in situ
on vehicle.
A good muffle unit was defined as one which passed leak test after the first pass in the oven. A bad part was defined as one which failed leak test after the first pass and had to be passed through the oven twice or more. This higher the FTQ, the higher the costs in rework, (meaning more overtime, more brazing paste consumption, more electricity used, and greater maintenance costs due to additional wear and tear on furnace) . The high FTQ also resulted in pressure to keep up with the next operations demand. FTQ became the project “critical to quality” (or CTQ) characteristic.
D CIAMStep A: Identify Project CTQs
Page 7
Step B: Team Charter
Business Case: (BIG Y – Net Sales, Customer Satisfaction, Compliance/Legal, Employee Satisfaction).
All muffle assemblies require 100% in line leak test. This testing can create high costs in the
process if the FTQ is excessive. In addition, the added handling increases the opportunities for
defects and damage.
Problem Statement: With higher FTQ’s it requires greater operator time to rework muffler in
furnace and re leak test. The burden of this rework and inspections is estimated at, USD $35000
or the cost of one permanent head count resource. This does not include hidden additional costs
(see slide 9).
Goal statement: To reduce the FTQ from brazing furnace to half the current level. This will
provide the opportunity to eliminate a permanent rework head count resource and save USD
$35000. In addition, indirect labour savings can be made as well as savings in gas and additional
unnecessary wear and tear on furnace which will result in reduction in downtime and spare parts
cost from the additional maintenance.
Timeline: Define (Oct 00), Measure (Jan 01), Analyse (Feb 01), Improve (March 01), Control (April
01)
D CIAM
Page 8
Step C: Process Map SIPOC D CIAMSuppliers Inputs Outputs
(Providers of the
required resources)
(Resources
required by the
process)
(Deliverables from
the process)
Requirements Requirements
Internal supplied Operators Training
parts from press shop Experience
Units per hour Zero defect from
next operation Internal Customer
(next operation)
Braze Paste Type Complete volume
Quantity in prescribed time. Final Customer
Location
Cycle Time
Furnace Running conditions
Maintenance
FTQ Data and
Work instructions Correct Recordkeeping
Current
Understood
Process Customers
(Top level description of the activity) (Stakeholders who place the
requirements on the outputs)
Prepare
Part for
Brazing
Furnace
(add
braze).
Pass parts
through Furnace
Muffler is
leak tested
and
passed to
plating
area.
Customer View
Page 9
Step 1: Select CTQ Characteristics
Project CTQ (Y) = Cost Reduction
Project y = FTQCost Reduction
Product Labour Machine
Rework Scrap Direct Indirect Uptime Productivity
Cycle
Times
Efficiency
StoppagesReliability
Quality Maintenance
INCREASED COST $$$$$$
D CIAM
Page 10
Step 2: Determine Performance Standard.
Defect Definition CTQ Elements: D CIAM
Output Unit COST
REDUCTION (BIG Y)
Output Characteristic. DELIVERY
OF PARTS WITHOUT LEAK.
Operational Definition MUFFLE ASSEMBLY
Project Y measure FTQ
TARGET 20,500 PPM LEAKS
Defect Definition LEAK FROM MUFFLE AT FIRST TEST
Number of Defect Opportunities ONE PER UNIT
NB. Muffle leak is measured after furnace
by two small Leak decay units.
At this stage, an internal specification
was determined as a pass/fail based on the
requirements of the final assembly.
At final assembly, the leak rate becomes
a significant customer characteristic so the
“after furnace” muffle leak test was initiated
to stop rejection at final assembly.
Page 11
Step 3: Validate Measurement System On Y Kappa
(Cross tabulation) Study for Attribute Leak data. D CIAM
Number of
Part/Samples/Questions n = 50
Number of Judges/Raters m = 2
ENTER CATEGORY INFORMTION
Categories 1 Leak 4 7 10 13
2 No Leak 5 8 11 14
3 6 9 12 15
More than two judges? No
Two judges only? Yes RAW DATA FOR 2 JUDGES
Multiple Judges (> 2) Two Judges
sum x2ij = Pobserved = 1.0
sum p*q = Pchance = 0.500
Koverall = Koverall or Individual = 0.96
Kappacategory for 2 judges
Category Kappa
#REF! #DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
#DIV/0!
ENTER INFORMATION IN COLUNMS BELOW
CALCULATIONS WILL APPEAR BELOW ONCE DATA IS ENTERED IN THE APPROPRIATE WORKSHEET
Step 1: Clear any categories values previously entered
Step 2: Enter Information
Step 3 Enter Data into this Worksheet:
Advanced Integrated
Technologies Group, Inc.
Copyright 1999, AIT Group Inc. All rights reserved.
Kappa Value of 0.96. This means that on a sample of
50 parts tested twice by two different operators, on two
readings the operators disagree on “good” and “bad” assemblies.
This was later Found to be a seal issue which was fixed. In general
Kappa values Greater than 0.75 are considered acceptable for inter-rater
agreement.
It should be remembered though that in the case of attribute studies applied,
any disagreement between raters is investigated to ensure no nonconforming
Parts are passed. In this case the next operations will assemble the muffler
into an AC system, which is leak tested automatically prior to final customer.
The purpose of this process is to reduce occurrence of high FTQ at Final
Assembly. Assemblies which pass muffle leak test nearly always pass at
Final assembly unless the leak is elsewhere in the A/C system.
Page 12
D CIAM
As data from muffler leak test is attribute (leak/not leak), the data is collected on
P charts. The current capability of the process is measured by “P Bar” which is
in percent defective. This in turn can then be translated into FTQ PPM for the
leak test operation.
The current year to date Capability (or DPMO) for the braze furnace (which is a
single in-process operation), is 42,000 PPM and needs to be Improved
drastically. The Raw data taken for the 60 days prior to the trials was compiled
onto a P Chart and showed 41,361 DPMO (as shown on next slide).
Although ideally a target of zero would be a long term goal, it is not a realistic
target. For the purpose of the project, a target of 20,500 DPMO has been set as
the benchmark.
Step 4: Define Performance Objectives
Page 13
D CIAMStep 5: Establish Process Capability
Mean FTQ is just over 41,000 PPM for the 60 days prior to the start of Improvement trials
P Chart for production Data prior to Experimental trials
0
0.02
0.04
0.06
0.08
0 10 20 30 40 50 60 70
Production Day Number
Fra
cti
on
De
fec
tiv
e
Page 14
Step 5: Establish Process Capability.
Comparison of FTQ with Process Capability
(Ppk or Cpk)D CIAM
Cpk Ppk Sigma DPMO Cpk Ppk Sigma DPMO Cpk Ppk Sigma DPMO
1 3 66810 1.34 4 6210 1.68 5 233
1.034 3.1 54800 1.374 4.1 4661 1.714 5.1 159
1.068 3.2 44570 1.408 4.2 3467 1.748 5.2 108
1.102 3.3 35930 1.442 4.3 2555 1.782 5.3 72
1.136 3.4 28720 1.476 4.4 1866 1.816 5.4 48
1.17 3.5 22750 1.51 4.5 1350 1.85 5.5 32
1.204 3.6 17860 1.544 4.6 968 1.884 5.6 21
1.238 3.7 13900 1.578 4.7 687 1.918 5.7 13.4
1.272 3.8 10720 1.612 4.8 484 1.952 5.8 8.6
1.306 3.9 8198 1.646 4.9 337 1.986 5.9 5.4
2.02 6 3.4
Page 15
D CIAMStep 5: Establish Process Capability
• From the P chart data:
• P bar = 0.0413
• Process Capability currently is 41,300 DPMO failures of the functional check.
• Customer is protected from receiving nonconforming product by 100% test on final A/C assembly but the failure rate is wasteful. Develop an action plan to reduce failure rate at furnace.
Page 16
Step 6: Identify Variation Sources Potential X’s D CIAM
Press 3
components
together to
make muffle
assembly .
Paste to
outside of
joint.
Pass
Assembl
y through
furnace.
Leak test
muffle and
pass to Store.
Plate
Muffle
Assembly.
Crimp
Hydraulic A/C
Lines to
Muffle.
Final
Assembl
y and
Leak Test
S/C.
Page 17
Step 7: Screen Potential Causes D CIAM
FTQ
Environment
Measurements
Methods
Material
Machines
Personnel
Team Leader
Maintenance
O perator
Leak Test Unit
Paste Dispenser
Furnace
Paste Ty pe
Muffle A ssembly
Paste A pplication
Belt Speed
Leak / No Leak
O v en Temp
Time in O v en
Time to O v en
Feet per Min
Wind gusts
Temperature
A fternoon Shift
Day Shift
Cause and Effect of Factors related to Muffle Leak FTQ
Page 18
Step 7: Screen Potential Causes D CIAM
• An screening trial was carried out on the muffle assembly with
the aim of reducing the occurrence of leakage between the centre
and end sections.
• The trial plan was developed to try different combinations of
paste, copper rings, and different methods of applying the paste,
with the aim of finding the best method that would provide the
highest first time “no leak” condition.
• The set up of samples is shown. There were 36 samples per
group. The other parameters such as belt speed and zone
temperatures were considered less important but were kept
constant throughout the trials.
Page 19
Step 7: DOE Screening Trial Initial results D CIAM
Group No Method Description Total Leaks
1 New Paste inner top cap 36 3
2 Old Wire on Centre 36 9
3 New Double paste on top 36 3
4 Old Old Caps 36 4
5 Old Wire on Cap 36 9
6 Old Different Paste Copper/Tin 20% 36 9
7 Old Different Paste Copper/Tin10% 36 21
8 Old Different Paste B Bronze 36 9
9 Old Different Paste Copper/Tin(other) 36 6
10 Old Double Line on Centre Can 36 9
11 New Paste on Centre Can - Top 36 3
Page 20
D CIAM
• There must be an adequate sample- the expected (not
obtained) frequency in each category must be at least 5.
Three assumptions must be met to use the Chi Square test:
• All observations must be independent, that is counted only once.
• Each observation must fit in only one category.
Step 7: DOE Chi Square Assumptions
Page 21
D CIAM
Good Leaks All
1 33 3 36
28.273 7.727
2 27 9 36
28.273 7.727
3 33 3 36
28.273 7.727
4 32 4 36
28.273 7.727
5 27 9 36
28.273 7.727
6 27 9 36
28.273 7.727
Chi-Square DF P-Value
Pearson 44.191 10 0.000
7 15 21 36
28.273 7.727
8 27 9 36
28.273 7.727
9 30 6 36
28.273 7.727
10 27 9 36
28.273 7.727
11 33 3 36
28.273 7.727
All 311 85 396
Good Leaks All
Step 8: Analysis between Groups.
Group difference is significant (p=<0.05)
Page 22
1110987654321
20
15
10
5
Group
Leaks
Interval Plot of Leaks95% CI for the Mean
Individual standard deviations are used to calculate the intervals.
D CIAMStep 8: Analysis between Groups.
Page 23
D CIAM
• The Main Conclusions that was drawn from this trial was that with
existing parameters and existing paste, the application of the paste to
the inside of the joint prior to press assembly (new) shows an
significant improvement from the existing (old) method. This was
further confirmed when a full Day’s production was run with the
change in paste application.
Step 8: Discover Variable Relationships.
• Different paste combinations should be used with the “new” method.
• Cost v FTQ benefit of different paste to be investigated. Initial P
Chart comparison for before and after (slides 26 and 27) shows
production data with same paste type .
Page 24
D CIAMStep 9: Establish New Assembly Process
Paste to
INSIDE of
joint.
Press 3
components
together to
make muffle
assembly.
Pass
Assembl
y through
furnace.
Leak test
muffle and pass
to store.
Swap Order of
Operations
Page 25
• Paste to be applied to the inside of the end can joints prior to pressing
operation.
• Muffle assembly to be pressed together within 4 hours of applying
paste.
• Muffle assembly to be passed through furnace within 72 hours of
pressing.
• Different types of paste to be trialed under these conditions.
D CIAMStep 9: Establish Operating Tolerances
Page 26
Step 10: Comparison from 60 days BEFORE
to after from validated Measurement System. D CIAM
Mean FTQ is just over 41,000 PPM for the 60 days prior to the start of Improvement trials
P Chart for production Data prior to Experimental trials
0
0.02
0.04
0.06
0.08
0 10 20 30 40 50 60 70
Production Day Number
Fra
cti
on
De
fec
tiv
e
Page 27
Step 10: Comparison from 60 days before to
AFTER from validated Measurement System. D CIAM
Mean FTQ is just under 10,000 PPM for the 60 days after the start of Improvement trials
P Chart for Production Data after process changes implemented.
-0.01
-0.005
0
0.005
0.01
0.015
0.02
0.025
0.03
0 10 20 30 40 50 60 70
Production Day Number
Fra
cti
on
De
fec
tiv
e
Page 28
Step 11: Determine Process Capability Improved
Performance – BEFORE PROJECT D CIAM
Step 11: Determine Process capability Improved
Performance – AFTER PROJECT
P Bar WAS 0.0413 which equates to
41,300 PPM
P Bar IS 0.00985 which equates to
9850 PPM
• Introduce New Paste (from group 9) as running change into
production with new paste application method and monitor FTQ
Page 29
Step 12: Implement Process Controls
To Maintain Performance D CIAM
P Bar = 7612 ppm. Ongoing monitoring via P Chart will ensure improvements have been
maintained and any positive or negative fine tuning can be evaluated moving forward.
P Chart for ongoing production 2001
-0.01
-0.005
0
0.005
0.01
0.015
0.02
0.025
0 10 20 30 40 50 60 70
Shift or Day number
Fra
cti
on
De
fec
tiv
e
Page 30
• FTQ may be improved further by upgrades in hardware and/or
adjustments to other Process Parameters which may need to be
evaluated separately for a cost/ benefit analysis. Longer term design
analysis (DFSS) may be utilised.
• What has been achieved from this project is a reduction in FTQ (and
thus hours saved in overtime, maintenance and downtime) on the
furnace due to additional hours in service for rework, without
any additional capital investment.
• Dedicated rework person was removed from line and used
elsewhere on more value adding activities.
D CIAMStep 12: Implement Process Controls
To Maintain Performance