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Cowlitz Fallsowlitz FallsHydroelectricydroelectricProjectroject
The Continuing Saga of thehe Continuing Saga of theCowlitz Falls Sluice Gatesowlitz Falls Sluice Gates2003 Repairs003 Repairs
By Steve Grega & J im ByrdBy Steve Grega & J im Byrd
NW Hydro Conference J une 9, 2005NW Hydro Conference J une 9, 2005
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Overview ofOverview of
Cowlitz Falls ProjectCowlitz Falls Project
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Where isWhere is
Cowlitz Falls Dam?Cowlitz Falls Dam?
Cowlitz Falls Dam
I-5SR-12
Chehalis
Randle
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Cowlitz Falls Project HistoryCowlitz Falls Project History
Started Studies in
1977 License
Application in April
1981 NEPA EIS April
1983
Licensed in J une1986
Permitting until1991
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Construction Started J une 1991Construction Started J une 1991
Blasting
Digging
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Construction Continued ThrougConstruction Continued Throug
19931993
Concrete
Equipment
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Commercial Operation J uneCommercial Operation J une
19941994
Dam
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Cowlitz Falls StatisticsCowlitz Falls Statistics
145 feet off ofBedrock
700 feet Long
2 Kaplan-TypeTurbines
2 35MWGenerators
265,000MWHr
Annually
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Dam Unique FeaturesDam Unique Features
Floating Debris
Barrier (Queen Mary)
Powerhouse SpillwayPowerhouse SpillwayOverflow DesignOverflow Design
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Operation of Cowlitz FallsOperation of Cowlitz Falls
ProjectProject Run of River Operation
SCADA holds Lake at nearly Constant Level Up to Two Foot Daily Reservoir Variation
If Flows are between 1000cfs and 1800cfs,Generate only Part of Day
Inflow below 1000cfs and Riffe Lake below
Elevation 750, Pass Inflow Drawdown if flows are great than 15,000 cfs
in Randle. 10 to 20 dependant on Inflow
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Staffing OperationStaffing Operation
Staff of 7 Full-TimeEmployees
Man the Plant 7days / week, 365days/ year
8 Hours / day
On-Call 16 hours /
day Manned Full Time
when Conditions
warrant
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Flood OperationsFlood Operations
December 1995 FloodDecember 1995 Flood --70.000 cfs70.000 cfs
February 1996 Flood ofFebruary 1996 Flood ofRecord 100,000 cfsRecord 100,000 cfs
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Flood OperationsFlood Operations
Gates 2 & 3 Full OpenGates 2 & 3 Full Open
Gates 1 & 4 Full OpenGates 1 & 4 Full Open
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The Sluice GatesThe Sluice Gates
Two gated low-
level outlet tunnelsunder Spillway #4
Tunnel is equippedwith 12 wide by16 high wheeled
gatesThird diversion
tunnel blocked off
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Purpose of Sluice GatesPurpose of Sluice Gates
Assist in passing siltin front of dam
Assist in passing flowsin access of turbineflow >10,500cfs
Passing low flowsduring time inflowsbelow turbineminimums
Dewatering Reservoir
below spillway ogee
l i
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Sluice GateSluice Gate
DesignDesign Regulating Wheel Gate
74,000 poundsw/ballast
Design Head 92 feet
12 Stainless steelwheels 19.7diameter
Hydraulic Raised,Gravity Closed
3.5diameter rod @
1000psi raises gate
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Sluiceway DewateringSluiceway Dewatering
MaintenanceBulkhead Gate
Closes only underbalanced headconditions
Guides do notcome to surface
Requires diversand 50-ton craneto install andretrieve
O i i l GO i i l G t
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Original GateOriginal Gate
DesignDesignTop & Bottom flanged
wheels to restrainlateral movement
Top & Bottom springTop & Bottom spring
rollers to restrainrollers to restrainupstream movementupstream movement
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First ProblemsFirst Problems May 1994May 1994
Start-up testing ofSluice Gates
Both Gates Noisy
Both Gates
jammed Would not move
up or down
Drained Reservoir Found gates off
track
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Modifications #1Modifications #1 Dec 1994Dec 1994
Experts UnsteadyPressures exist that
cause gate to jump Add Heavier spring
assemblies
Add side rails &bumpers
Modify top Lintel
Chamber ceiling
Repair Wheels, etc.
Some improvement but still loud banging
M difi ti #2M difi ti #2 AA
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Modification #2Modification #2 AugAug
19961996 Installed pressing
system To holdgate downstream
Control software
modifications opengate to 112% toremove from
waterway
Still too
much gatemovement
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Modification #3Modification #3 Nov 1997Nov 1997
Installed 4 zeroInstalled 4 zero--clearanceclearance
side guide shoesside guide shoes
Installed stainless
steel side guide rails
Testing & Acceptance of theTesting & Acceptance of the
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Testing & Acceptance of theTesting & Acceptance of the
GatesGates Full operation testing
conducted in Mar 98
Gates smooth to 80%
90% to 112% roughoperation
112% open andspillway gate 4 open
3, sounds reduced SG#4 to 10open,sound reduced
Manufacture &Engineer left us
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Gate operation ProblemsGate operation Problems
19991999 20032003 Apr 99 Notice a bottom
Bumper was missing
Sep 99 Inspection found 3of the 4 bottom bumpergone
Bolts failed in tension Lower section of side rail
missing
Reduced max opening to63% or 10
Continued to Operate Gates
Top Side Bumper
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Failed ComponentsFailed Components
Box holdingbumper pads
Bolts securing bottom
bracket failed in tension
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Feb 2003 Operational FailureFeb 2003 Operational Failure
Plant mannedduring moderate
flood heavysediment load,drawn downreservoir 14 feet(elev. 848)
Spilling fromSpillways 1 & 4
SCADA system
opened sluice gates1 & 2 to 5
2003 Operation Failure2003 Operation Failure
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2003 Operation Failure2003 Operation Failure
Corrective ActionsCorrective Actions Operator closed Spill
Gate 4 followed by theclosing of sluice gates
Sluices closed to foot
Re-opened spill gate 4to pass flood
Other attempts were
made to close sluices Both gates stuck at 9
open
Stuck sluice gate fromD/S side
Drain the Reservoir?Drain the Reservoir?
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Drain the Reservoir?Drain the Reservoir?
Yep!Yep! After analyzing situation
balance closure withsluice bulkhead required
Must obtain permits
Clean out moorage site Move Debris Barrier
Construct a 2nd bulkhead
Drain Reservoir Install bulkhead gates
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Drawn Down ReservoirDrawn Down Reservoir
Silt?
lkh d l
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Bulkhead ClosureBulkhead Closure
After some coaxingbulkheads finally
seated & stoppedthe flow
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Removal of Sluice Gate #1Removal of Sluice Gate #1 Difficult &
expensive tofind crane tohandle load
1st remove
hatch cover Removecylinder & rod
Remove topplatform
Remove top
bumpers
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Removal of Sluice Gate #1Removal of Sluice Gate #1
Requires a 300-ton crane
Experienced Ironworkers
InspectionInspection
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InspectionInspection
& Findings& Findings Wheel Friction, 6 of
12 wheels could notbe turned by hand
IIWheel thrust washersWheel thrust washers
in poor conditionin poor condition
InspectionInspection
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InspectionInspection Wheel & Rails indicated
scoring on surfaces(from wheels not turning)
IISide spring rollersSide spring rollersindicated heavy impactindicated heavy impact
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InspectionInspection
ConcreteConcrete slotsloterosionerosion
Indications of
Lateralmovement(rail scoring)
C l i
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ConclusionsConclusions Gates Stuck do to
increased wheel bushingfriction
Wheel Damage causedby large impact forces
Bushing Damage caused
by dirt and possiblebushing material swelling no clearance
Gravity closure safetymargin too small
Lower bumpers subject
to high velocity flows &debris impact
G i & difi iG t R i & M difi ti
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Gate Repairs & ModificationsGate Repairs & Modifications Replaced wheel
bushings - Lubritemang-brnz with G-10lubricant
Add seals to reduce
contamination
IIReplaced thrust washersReplaced thrust washers
(Manganese(Manganese--Bronze)Bronze)
IIFace cut wheelsFace cut wheels
Gate Repairs & ModificationsGate Repairs & Modifications
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Gate Repairs & ModificationsGate Repairs & Modifications
Rebuilt side rollerspring assemblies
Combined lower
roller spring & zero-clearance guides
OrkotSliding Pad withRubber Pad behind
Gate Repairs & ModificationsGate Repairs & Modifications
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Gate Repairs & ModificationsGate Repairs & Modifications
Repaired Guides andConcrete
Used Emaco S88, fiber-reinforcedstructural repair mortar
Gate Repairs & ModificationsGate Repairs & Modifications
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Gate Repairs & ModificationsGate Repairs & Modifications
Rebuilt hydrauliccylinder
Rebuilt electronicposition device(temposonic)
Gate Repairs & ModificationsGate Repairs & Modifications
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Gate Repairs & ModificationsGate Repairs & Modifications
Repaired pressingsystem roller rails
Repaired Gate Seals
Final CheckFinal Check
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Final CheckFinal Check
and Installationand Installation Rehabilitation
Complete
Where do we go from here?Where do we go from here?
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Where do we go from here?Where do we go from here?
Tested gates to 10
Evaluate adding
additional ballastto gates
Evaluated addingupper snubbersystem to reducemovement in fullopen position
Extend gantrycrane rail acrossbay 4
Cowlitz Falls HydroelectricCowlitz Falls Hydroelectric
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yy
ProjectProject
Questions?