Sluice Gate Presentation1

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    Cowlitz Fallsowlitz FallsHydroelectricydroelectricProjectroject

    The Continuing Saga of thehe Continuing Saga of theCowlitz Falls Sluice Gatesowlitz Falls Sluice Gates2003 Repairs003 Repairs

    By Steve Grega & J im ByrdBy Steve Grega & J im Byrd

    NW Hydro Conference J une 9, 2005NW Hydro Conference J une 9, 2005

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    Overview ofOverview of

    Cowlitz Falls ProjectCowlitz Falls Project

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    Where isWhere is

    Cowlitz Falls Dam?Cowlitz Falls Dam?

    Cowlitz Falls Dam

    I-5SR-12

    Chehalis

    Randle

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    Cowlitz Falls Project HistoryCowlitz Falls Project History

    Started Studies in

    1977 License

    Application in April

    1981 NEPA EIS April

    1983

    Licensed in J une1986

    Permitting until1991

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    Construction Started J une 1991Construction Started J une 1991

    Blasting

    Digging

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    Construction Continued ThrougConstruction Continued Throug

    19931993

    Concrete

    Equipment

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    Commercial Operation J uneCommercial Operation J une

    19941994

    Dam

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    Cowlitz Falls StatisticsCowlitz Falls Statistics

    145 feet off ofBedrock

    700 feet Long

    2 Kaplan-TypeTurbines

    2 35MWGenerators

    265,000MWHr

    Annually

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    Dam Unique FeaturesDam Unique Features

    Floating Debris

    Barrier (Queen Mary)

    Powerhouse SpillwayPowerhouse SpillwayOverflow DesignOverflow Design

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    Operation of Cowlitz FallsOperation of Cowlitz Falls

    ProjectProject Run of River Operation

    SCADA holds Lake at nearly Constant Level Up to Two Foot Daily Reservoir Variation

    If Flows are between 1000cfs and 1800cfs,Generate only Part of Day

    Inflow below 1000cfs and Riffe Lake below

    Elevation 750, Pass Inflow Drawdown if flows are great than 15,000 cfs

    in Randle. 10 to 20 dependant on Inflow

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    Staffing OperationStaffing Operation

    Staff of 7 Full-TimeEmployees

    Man the Plant 7days / week, 365days/ year

    8 Hours / day

    On-Call 16 hours /

    day Manned Full Time

    when Conditions

    warrant

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    Flood OperationsFlood Operations

    December 1995 FloodDecember 1995 Flood --70.000 cfs70.000 cfs

    February 1996 Flood ofFebruary 1996 Flood ofRecord 100,000 cfsRecord 100,000 cfs

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    Flood OperationsFlood Operations

    Gates 2 & 3 Full OpenGates 2 & 3 Full Open

    Gates 1 & 4 Full OpenGates 1 & 4 Full Open

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    The Sluice GatesThe Sluice Gates

    Two gated low-

    level outlet tunnelsunder Spillway #4

    Tunnel is equippedwith 12 wide by16 high wheeled

    gatesThird diversion

    tunnel blocked off

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    Purpose of Sluice GatesPurpose of Sluice Gates

    Assist in passing siltin front of dam

    Assist in passing flowsin access of turbineflow >10,500cfs

    Passing low flowsduring time inflowsbelow turbineminimums

    Dewatering Reservoir

    below spillway ogee

    l i

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    Sluice GateSluice Gate

    DesignDesign Regulating Wheel Gate

    74,000 poundsw/ballast

    Design Head 92 feet

    12 Stainless steelwheels 19.7diameter

    Hydraulic Raised,Gravity Closed

    3.5diameter rod @

    1000psi raises gate

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    Sluiceway DewateringSluiceway Dewatering

    MaintenanceBulkhead Gate

    Closes only underbalanced headconditions

    Guides do notcome to surface

    Requires diversand 50-ton craneto install andretrieve

    O i i l GO i i l G t

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    Original GateOriginal Gate

    DesignDesignTop & Bottom flanged

    wheels to restrainlateral movement

    Top & Bottom springTop & Bottom spring

    rollers to restrainrollers to restrainupstream movementupstream movement

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    First ProblemsFirst Problems May 1994May 1994

    Start-up testing ofSluice Gates

    Both Gates Noisy

    Both Gates

    jammed Would not move

    up or down

    Drained Reservoir Found gates off

    track

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    Modifications #1Modifications #1 Dec 1994Dec 1994

    Experts UnsteadyPressures exist that

    cause gate to jump Add Heavier spring

    assemblies

    Add side rails &bumpers

    Modify top Lintel

    Chamber ceiling

    Repair Wheels, etc.

    Some improvement but still loud banging

    M difi ti #2M difi ti #2 AA

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    Modification #2Modification #2 AugAug

    19961996 Installed pressing

    system To holdgate downstream

    Control software

    modifications opengate to 112% toremove from

    waterway

    Still too

    much gatemovement

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    Modification #3Modification #3 Nov 1997Nov 1997

    Installed 4 zeroInstalled 4 zero--clearanceclearance

    side guide shoesside guide shoes

    Installed stainless

    steel side guide rails

    Testing & Acceptance of theTesting & Acceptance of the

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    Testing & Acceptance of theTesting & Acceptance of the

    GatesGates Full operation testing

    conducted in Mar 98

    Gates smooth to 80%

    90% to 112% roughoperation

    112% open andspillway gate 4 open

    3, sounds reduced SG#4 to 10open,sound reduced

    Manufacture &Engineer left us

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    Gate operation ProblemsGate operation Problems

    19991999 20032003 Apr 99 Notice a bottom

    Bumper was missing

    Sep 99 Inspection found 3of the 4 bottom bumpergone

    Bolts failed in tension Lower section of side rail

    missing

    Reduced max opening to63% or 10

    Continued to Operate Gates

    Top Side Bumper

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    Failed ComponentsFailed Components

    Box holdingbumper pads

    Bolts securing bottom

    bracket failed in tension

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    Feb 2003 Operational FailureFeb 2003 Operational Failure

    Plant mannedduring moderate

    flood heavysediment load,drawn downreservoir 14 feet(elev. 848)

    Spilling fromSpillways 1 & 4

    SCADA system

    opened sluice gates1 & 2 to 5

    2003 Operation Failure2003 Operation Failure

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    2003 Operation Failure2003 Operation Failure

    Corrective ActionsCorrective Actions Operator closed Spill

    Gate 4 followed by theclosing of sluice gates

    Sluices closed to foot

    Re-opened spill gate 4to pass flood

    Other attempts were

    made to close sluices Both gates stuck at 9

    open

    Stuck sluice gate fromD/S side

    Drain the Reservoir?Drain the Reservoir?

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    Drain the Reservoir?Drain the Reservoir?

    Yep!Yep! After analyzing situation

    balance closure withsluice bulkhead required

    Must obtain permits

    Clean out moorage site Move Debris Barrier

    Construct a 2nd bulkhead

    Drain Reservoir Install bulkhead gates

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    Drawn Down ReservoirDrawn Down Reservoir

    Silt?

    lkh d l

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    Bulkhead ClosureBulkhead Closure

    After some coaxingbulkheads finally

    seated & stoppedthe flow

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    Removal of Sluice Gate #1Removal of Sluice Gate #1 Difficult &

    expensive tofind crane tohandle load

    1st remove

    hatch cover Removecylinder & rod

    Remove topplatform

    Remove top

    bumpers

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    Removal of Sluice Gate #1Removal of Sluice Gate #1

    Requires a 300-ton crane

    Experienced Ironworkers

    InspectionInspection

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    InspectionInspection

    & Findings& Findings Wheel Friction, 6 of

    12 wheels could notbe turned by hand

    IIWheel thrust washersWheel thrust washers

    in poor conditionin poor condition

    InspectionInspection

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    InspectionInspection Wheel & Rails indicated

    scoring on surfaces(from wheels not turning)

    IISide spring rollersSide spring rollersindicated heavy impactindicated heavy impact

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    InspectionInspection

    ConcreteConcrete slotsloterosionerosion

    Indications of

    Lateralmovement(rail scoring)

    C l i

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    ConclusionsConclusions Gates Stuck do to

    increased wheel bushingfriction

    Wheel Damage causedby large impact forces

    Bushing Damage caused

    by dirt and possiblebushing material swelling no clearance

    Gravity closure safetymargin too small

    Lower bumpers subject

    to high velocity flows &debris impact

    G i & difi iG t R i & M difi ti

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    Gate Repairs & ModificationsGate Repairs & Modifications Replaced wheel

    bushings - Lubritemang-brnz with G-10lubricant

    Add seals to reduce

    contamination

    IIReplaced thrust washersReplaced thrust washers

    (Manganese(Manganese--Bronze)Bronze)

    IIFace cut wheelsFace cut wheels

    Gate Repairs & ModificationsGate Repairs & Modifications

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    Gate Repairs & ModificationsGate Repairs & Modifications

    Rebuilt side rollerspring assemblies

    Combined lower

    roller spring & zero-clearance guides

    OrkotSliding Pad withRubber Pad behind

    Gate Repairs & ModificationsGate Repairs & Modifications

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    Gate Repairs & ModificationsGate Repairs & Modifications

    Repaired Guides andConcrete

    Used Emaco S88, fiber-reinforcedstructural repair mortar

    Gate Repairs & ModificationsGate Repairs & Modifications

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    Gate Repairs & ModificationsGate Repairs & Modifications

    Rebuilt hydrauliccylinder

    Rebuilt electronicposition device(temposonic)

    Gate Repairs & ModificationsGate Repairs & Modifications

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    Gate Repairs & ModificationsGate Repairs & Modifications

    Repaired pressingsystem roller rails

    Repaired Gate Seals

    Final CheckFinal Check

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    Final CheckFinal Check

    and Installationand Installation Rehabilitation

    Complete

    Where do we go from here?Where do we go from here?

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    Where do we go from here?Where do we go from here?

    Tested gates to 10

    Evaluate adding

    additional ballastto gates

    Evaluated addingupper snubbersystem to reducemovement in fullopen position

    Extend gantrycrane rail acrossbay 4

    Cowlitz Falls HydroelectricCowlitz Falls Hydroelectric

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    yy

    ProjectProject

    Questions?