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The Ramco Cements Limited, Alathiyur Profile

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Page 1: The Ramco Cements Limited, Alathiyur Profile

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Page 2: The Ramco Cements Limited, Alathiyur Profile

The Ramco Cements Limited, Alathiyur Profile

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A flagship company of RAMCO Group, having five Cement manufacturing units, four grinding units and one packing unit with the total capacity of 16.5 MTPA.

Alathiyur plant was setup in two phases 1997 & 2001 with Cement capacity of 3.05 Million Tons / Annum and 2 X 3700 TPD Kilns.

The manufacturing products are Ordinary Portland Cement, Portland Pozzolana Cement and SRPC as per BIS & SLS standards.

2X18 + 6 MW - Coal based Thermal power plant

Page 3: The Ramco Cements Limited, Alathiyur Profile

Integrated Management System Certification

3

IS/ISO 9001: 2015

IS/ISO 14001: 2015

IS 18001: 2007

Quality Management System

Environment Management System

Occupational Health & Safety Management System

IS/ISO 50001:2011 Energy Management System

5S Excellence Certified Company

Page 4: The Ramco Cements Limited, Alathiyur Profile

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Page 5: The Ramco Cements Limited, Alathiyur Profile

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Page 6: The Ramco Cements Limited, Alathiyur Profile

Energy Monitoring & Reporting System

Energy consumption both electrical & thermal : Daily

Energy conservation projects : Weekly

Review meeting conducted by : Unit Head

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Page 7: The Ramco Cements Limited, Alathiyur Profile

Energy Management System

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Page 8: The Ramco Cements Limited, Alathiyur Profile

Selection

• Department - Plant Management, Production ,Maintenance Quality Control ,Accounting

Formation

• Each department Provide one or more Representatives to the Energy Management team

Coordination

• Each Energy management Clusters will be headed by Team leader and the whole is monitoring by Energy Manager

Responsibilities

• Define Objectives, Prepare Energy Planning, Optimal Energy Operation, Detect Weakness Plan and Perform Measures/Projects Prepare Energy Performance & Reporting Establish & perform Energy Controlling Review achievements

Implementing Strategy

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Page 9: The Ramco Cements Limited, Alathiyur Profile

WORKS HEAD

HOD

MINES

HOD

P & QC

HOD

MECH

ENERGY MANGER

HOD

E & I

HOD

CDS & PP

HOD

TPP

UNIT HEAD

Core Committee Team – Energy Cell

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INCHARGEMINES & CRUSHER

INCHARGE

TPP

INCHARGE

PACKING

INCHARGE

CEM MILL

INCHARGE PYRO

INCHARGE RAW MILL & COAL MILL

INCHARGE

UTILITIES

Page 10: The Ramco Cements Limited, Alathiyur Profile

Responsibilities of Steering Committee

False air study in all major sections i.e., Kiln, Raw Mill, Coal Mill and Cement

Mill on monthly basis.

Monitor production performance vis-à-vis SEC.

Monitor fan performance and initiative corrective action required, if any, on monthly basis.

Identify/Evolve new ENCON projects with and without investment.

Encourage employee participation through effective implementation of

Suggestion Box Scheme, 5S & Quality Circle.

IMS – EnMS Management Review Meetings, EMAP will be reviewed.

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Page 11: The Ramco Cements Limited, Alathiyur Profile

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Sl. No Description Units 2016-17 2017-18

1 MTOE reduction MTOE 175239 170800

2 Kiln Thermal SEC kCal/kg clinker 699 697

3 Specific Electrical Energy - clinkering kWh/T of clinker 52.76 52.58

4 Specific Electrical Energy – Grinding kWh/T of cement 26.16 25.02

5 CPP Heat rate kCal/kWh 3421 3496

6 CPP auxiliary consumption % 10.49 10.43

7 Thermal Substitution Rate % 2.2 5.95

8 Clinker factor % 0.77 0.78

9 Blended cement *%) of total cement % 94 92

10 Specific CO2 emission Kg CO2/ kg cement 702.42 700.35

Energy Performance Improvement

Page 12: The Ramco Cements Limited, Alathiyur Profile

Energy Conservation Projects Implemented in the years

2017-18

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No. of Projects : 6

Projects with NIL investment : 5 Nos.

Total amount invested : Rs. 149 Lacs

Cost savings achieved : Rs. 233 Lacs

Electrical energy saved : 52.5 Lac Kwh

Thermal Energy saved : 350 MT of coal

Reduction in GHG emissions : 5305 MT of CO2

Page 13: The Ramco Cements Limited, Alathiyur Profile

Energy Conservation Project 2017-18

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Sl. No. Title of Project

Annual Electrical

Saving (kWh)

Annual Electrical

Cost Saving (Rs

million)

Annual Thermal Saving (Ton/ye

ar)

Annual Thermal Saving

(Rs million)

Total Annual Savings

(Rs million)

Investment Made (Rs million)

Payback (Month

s)

1Modification of Line-1 Coal mill main bag filter purging from low pressure to high pressure

792,000 3.17 0 0 3.17 2.5 10

2 Retrofitting of Line-1 Cement Mill fan 3,896,640 15.59 0 0 15.59 5 4

3 Removal of damper in Line-1 RABH fan 216,000 0.86 0 0 0.86 0 0

4 Installation of Pillard burner in Line-1 Kiln 0 350 2.3 2.31 5.2 27

5Installation of VRF AC System in Rawmill-2 IO Room

275,800 1.1 0 0 1.1 1 11

6Replacement of 70W / 250W SON light fittings by energy efficient 36W / 100W LED fittings

68,240 0.27 0 0 0.27 1.2 53

Page 14: The Ramco Cements Limited, Alathiyur Profile

750

760

770

780

790

800

Target Achieved

796

768

Gate to Gate Energy Consumption for PAT Cycle-I

19th National Award for Excellence In Energy Management -2018 14

BEE-PAT Scheme : 8946 Nos. of Energy saving certificates issuedK

cal/

Kg

of

Cem

en

t

Page 15: The Ramco Cements Limited, Alathiyur Profile

650

670

690

710

730

750

Baseline Target 2017-18

756

718

697

Gate to Gate Energy Consumption for PAT Cycle-II

15

Kcal/

Kg

of

Cem

en

t

Page 16: The Ramco Cements Limited, Alathiyur Profile

Road Map To Achieve Benchmark

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Page 17: The Ramco Cements Limited, Alathiyur Profile

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Page 18: The Ramco Cements Limited, Alathiyur Profile

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Innovative Project -1

In our Alathiyur plant we have 2 nos. of Vertical Roller Mill for Clinker grinding.

Line-1 mill FLS make OK 33.4 capacity of 160 TPH for PPC and Line-2 mill LOESCHE make LM 56.2 capacity of 260 TPH for PPC.

Line-1 Cement mill is consuming about 4kWh/MT higher than Line-2 Cement mill, due to this we are operating Line-1 Cement mill very less.

We have identified the difference is in the specific power consumption of fan.

Page 19: The Ramco Cements Limited, Alathiyur Profile

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Innovative Project -1

Fan Power consumption high: We have identified the reasons for low fan efficiency and done stage wise modifications like:

Increasing the fan inlet duct dia from 2 m to 2.8 m

Modification of fan outlet to chimney duct

Modification of bag filter outlet duct by conducting CFD

Modification of fan inlet suction box.

Page 20: The Ramco Cements Limited, Alathiyur Profile

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Innovative Project -1

By carrying out above all modifications, the fan inlet turbulence has reduced,

but the fan outlet turbulence did not reduce and Reason is due to the recirculation duct tapping immediately after the fan outlet, due to this the fan

outlet pressure is varying from -100mmwg to -200mmwg.

Action taken to reduce fan power:

Replacement of existing low efficiency fan (50% eff.) with high efficiency fan

(83% eff).

Installation of junction box at the mill fan outlet and rerouting recirculation duct

to eliminate turbulence at the fan outlet duct.

Page 21: The Ramco Cements Limited, Alathiyur Profile

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Page 22: The Ramco Cements Limited, Alathiyur Profile

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Modified recirculation duct routing from the junction box

Page 23: The Ramco Cements Limited, Alathiyur Profile

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Savings achieved : 6.6 Kwh/Mt of Cement

Productivity Improvement : 15 TPH

Cost savings : Rs. 155.9 lacs

Investment Cost : Rs. 50 Lacs

Simple Pay Back Period : 4 Months

Innovative Project -1

Page 24: The Ramco Cements Limited, Alathiyur Profile

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Page 25: The Ramco Cements Limited, Alathiyur Profile

Line-1 Coal Mill Main Bag Filter is designed for low pressure high volume purging.

During normal operation in Line-1 Coal mill, Bag filter DP is high which causes the frequent disturbances in Mill operation.

The disturbances causes reduction in mill output, increase in specific power consumption. Due to this we have even forced to reduce the kiln feed occasionally.

We observed that when ever there is mill trip, lot of material is collected from the bag filter to the fine coal bins.

We have taken trial with increased purging pressure up to 3.5 bar and increased the on time of purging, but there is no any significant improvement.

From the above trials we observed that the bag cleaning (purging) is not adequate.

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Innovative Project -2

Page 26: The Ramco Cements Limited, Alathiyur Profile

We studied the root cause for inadequate bag cleaning:

Line-1 coal mill is designed for Lignite / Coal grinding.

During pet coke grinding, the mill output is low and also not able to achieve the desired residue.

We have modified the mill internals and classifier to suit pet coke grinding, due to this the mill Dp has increased by 250 – 300 mmwg.

The bag filter is designed for the inlet draft of -650 mmwg. After the modification of the mill it has increased to -900 to -950 mmwg.

Due to increase in the bag filter draft, the low pressure high volume purging is not adequate for cleaning of the bags.

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Innovative Project -2

Page 27: The Ramco Cements Limited, Alathiyur Profile

We have decided to change the purging from low pressure high volume to high pressure low volume purging.

The modification was carried out in-house.

We designed and fabricated the purging air headers, purging pipes. We procured the solenoid valves, venturi.

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Innovative Project -2

Page 28: The Ramco Cements Limited, Alathiyur Profile

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DescriptionBefore modification After modification

Low pressure purging High pressure purging

Bag Ø in mm 127 127

Bag length in mm 5040 5040

Bag seating type Snap band Snap band

Qty in Nos 1024 1024

Venturi Availability No Yes ( Provided )

Purge pipe Ø 80 NB 50 NB

Tube sheet to purge pipe height

190 mm 120mm

Purge pipe purge hole dia16mm (Nozzle pipe Ø

36mm)4.5mm (Nozzle pipe Ø 6.3mm)

Operating air pressure 2.5 bar 5.5 bar

Compressor air volume 380 CFM 260 CFM

Purging Sequence 1,2 - 3,4 - 5,6 …….. 1,33 - 2,34 - 3,35 …….

On Time 0.120 Sec 0.175 Sec

Off Time (Pass Time) 7 Sec 6 Sec

Page 29: The Ramco Cements Limited, Alathiyur Profile

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Before After

Innovative Project -2

Page 30: The Ramco Cements Limited, Alathiyur Profile

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Before After

Innovative Project -2

Page 31: The Ramco Cements Limited, Alathiyur Profile

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Before Bag filter purging modification

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After Bag filter purging modification

Page 33: The Ramco Cements Limited, Alathiyur Profile

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Innovative Project -2

Investment Cost : Rs. 25 Lacs

Cost Savings : Rs. 32 Lacs/Year

Simple Pay Back Period : 10 Months

Electrical energy savings : 5.08 kWh/T matl

Page 34: The Ramco Cements Limited, Alathiyur Profile

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Best

Improvement

in Energy

performance

in

Manufacture

of Blended

Cements –

2016-17 from

NCCBM

Page 35: The Ramco Cements Limited, Alathiyur Profile

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