Investigation Into Production of Refined Bismuth

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    COMMONWEALTH OF AUSTRALIA

    D E P A R T M E N T O F N A T I O N A L D E V E L O P M E N T

    BU R E A U O F M IN E R A L R E SO U R C E S

    G E O L O G Y A N D G E O P H Y SIC S

    RECORDS:

    1965/182

    INVESTIGATION INTO PRODUCTION OF REFINED BISMUTH

    (A.M.D.L. Report No.388)

    by

    R.E. Wilmshurst

    The information contained in this report has been obtained by the

    Department of National Development, as part of the policy of the Common-

    wealth Government, to assist in the exploration and development of mineral

    resources. It may not be published in any form or used in a company

    prospectus without the permission in writing of the Director, Bureau of

    Mineral Resources Geology and Geophysics.

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    INVESTIGATION INTO PRODUCTION OF REFINED BISMUTH

    A . M . D . L . R e p o r t N o . 3 8 8 )

    by

    R.E. Wilmshurst

    Records 1965/182

    T a b l e o f C o n t e n t s

    . Introduction

    A.M.D.L. Report No.388

    page 1

    Title Page

    Contents

    pages 1-12

    Figure 1

    The information contain ed in this report has been obtained

    by the Department of National D evelopment, as part of the policy

    of

    the Commonwealth Government to assist in the exploration and

    development of mineral resources, It may not be published in any

    form or used in a company prospectus without the permission in

    writing of the Director, Bureau of Mineral Resources, Geology and

    Geophysicso

    of the Australian Mineral Development Laboratories, Adelaide.

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    Introduction

    Marketing of crude bismuth metal produced by

    leaching ore from the Tenna nt Creek area proved difficult.

    The relatively low return for crude bismuth compared with

    prices listed for pharmacev. Aical grad e material prompted the

    Bureau to sponsor this research into an electro,-refining

    process suitable for the production of bismuth metal of

    acceptable _grade at Tennant Creek.

    The report has been included in the Bureau's Recol

    d

    series so that it may enjoy the wider distribution afforded.

    by the open file system. It has not been altered in any

    w a y .

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    2/1/4

    MDL Report 388

    November,

    1964

    INVESTIGATION INTO PRODUCTION OF REFINED BISMUTH

    by

    R. E. Wilmshurst

    to

    THE BUREAU OF MINERAL RESOURCES

    Investigation by: Industrial Chemistry Section

    Officer in Charge: F. R. Hartley

    L. Wallace Coffer, Director

    THE AUSTRALIAN MINERAL DEVELOPMENT LABORATORIES

    Adelaide

    outh Australia

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    CONTENTS

    Page

    1

    INTRODUCTION

    1 1

    lectro-refining of Bismuth

    2

    SUMMARY

    3

    MATERIAL EXAMINED

    4

    EQUIPMENT

    5

    EXPERIMENTAL PROCEDURE AND RESULTS

    5. 1

    reliminary

    5. 2

    aboratory Investigations

    5. 2. 1

    mprovement of Existing Process

    5. 2. 2

    efining of Ingot Metal

    5.3

    iscussion

    6

    PILOT SCALE REFINING OF BISMUTH METAL

    7

    DISCUSSION

    1

    8 REFERENCES

    2

    FIGURE 1

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    1.

    NTRODUCTION

    Early in 1962, a request was received from Mr C. N. Strong of

    Tennant Creek for the development of an electro-refining process to produce

    pharmacutical grade bismuth from crude metal. The latter was produced

    from tailings dumps in the Tennant Creek area by a process similar to that

    described by Cathro and Koch l

    (a). In his process, Mr. Strong leached the

    ore by percolation with sodium chloride-sulphuric acid solution. The leach

    solution, together with liquor used to wash the leach residue, was then

    treated with scrap iron. Bismuth metal in a finely divided sponge form

    was precipitated in this cementation step, and was subsequently melted into

    ingots. The product, although technically a good quality metal, was not of

    sufficiently high purity for use in the manufacture of pharmaceuticals.

    In September, 1962, Mr Strong approached the Commonwealth

    Bureau of Mineral Resources for support in financing the investigation.

    This support was given and work on the project commenced in January, 1963.

    Specifications for pharmaceutical bismuth are laid down in the

    British Pharmaceutical Codex, but this authority uses arbitrary tests

    extensively, without giving numerical limits for specific impurities. Tests

    of this nature are convenient as acceptance tests to determine the suitability

    of any given material, but are inadequate for use in investigational work.

    Evaluation of the tests and correspondence with Bismuth Products Pty. Ltd.

    led to the following tentative limits for impurities in pharmaceutical grade

    bismuth metal:

    Arsenic not more than 2

    pm

    Lead

    itto - 0.04 %

    Copper

    0 ppm

    Silver

    .01

    Antimony

    0

    pm

    Tellurium

    pm

    The experimental work described in this report was aimed at

    production of a metal to this specification by an electro-refining process

    suitable for use at Tennant Creek.

    1.1

    lectro-refining of Bismuth

    Electro-refining of bismuth has been practised for many years but

    little detailed information has been published. Gruzensky and Crawford

    z

    surveyed the various electrolytes recommended from time to time and found

    only two to be satisfactory. One of these, a hydroflusilicic acid solution,

    gave excellent results but was unstable and unsuitable for large scale use,

    particularly in remote areas. The alternative hydrochloric acid-bismuth

    chloride solution gave satisfactory results except that removal, of lead was

    not achieved; this was rectified by the addition of sulphuric acid. Kern

    and Jones

    3

    recommended a similar solution, and this was used also by Cathro

    and Koch (loc cit) in refining of Tennant Creek bismuth.

    (a) See Section 8 for References.

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    Metal from Tennant Creek has been variable in composition, with

    analyses generally in the following ranges:

    Copper

    .03 - 0.20 %

    Lead

    .05 - 0.10 %

    Zinc

    a) < 0.01

    Silver

    50

    pm

    Iron

    0.01 %

    The work of Cathro and Koch, in conjunction with consideration of

    standard electrode potentials, indicates that simple electro-refining applied

    to this metal would have the effect shown in Table 1.

    TABLE 1: LIKELY PURIFICATION OF BISMUTH

    Element

    Crude Metal

    Reduction Factor

    Refined Metal

    Cu

    0.2

    5

    0.04

    Pb

    0.1

    450

    2

    Pm

    Zn

    0.01

    high

    low

    Fe

    50

    pm

    high

    low

    Ag

    0.01

    1.3

    70

    Pm

    These figures suggest that electro-refining alone is unlikely to

    produce a metal to the required specification. Pyrometallurgical methods

    of removing these impurities were therefore investigated. Some considera-

    tion was also given to modifying the existing operations at Tennant Creek to

    improve the crude metal purity.

    2.

    UMMARY

    In response to a request from Mr C. N. Strong of Tennant Creek and

    under the sponsorship of the Commonwealth Bureau of Mineral Resources,

    an electro-refining process for metallic bismuth has been developed.

    Simple electro-refining using an acidic chloride electrolyte was incapable of

    producing pharmaceutical grade bismuth from crude metal. Various

    pyrometallurgical techniques were examined and a hybrid process developed.

    Melting of the crude metal with sodium hydroxide and sodium cyanide,

    casting the resultant metal into anodes, and electro-refining in the chloride

    bath, followed by a sulphur drossing step gave pharmaceutical quality

    bismuth metal.

    (a)

    Less than.

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    3

    A large parcel of bismuth metal has been refined by this process to

    give over 200 pounds of pharmaceutical quality metal. The process is

    capable of good yields of metal and the electro-refining operation has a high

    current efficiency.

    The weaknesses inherent in electro-refining processes are considered

    to make them adaptable only with difficulty for small-scale use in remote

    areas such as Tennant Creek.

    3.

    ATERIAL EXAMINED

    The ore used in leaching experiments was from the Jubilee Mine,

    near Tennant Creek. This material contained approximately 3 per cent

    bismuth.

    In both the small scale and pilot scale refining experiments, a

    parcel of 350 pounds of crude bismuth metal from Mr Strong was used. This

    parcel consisted of 14 ingots each of 25 pounds nominal weight. As pre-

    liminary experiments had indicated that copper and silver were the elements

    most likely to cause difficulty in refining, each ingot was assayed for these

    metals. The results of these assays are set out in Table 2.

    TABLE 2: ANALYSES OF CRUDE BISMUTH INGOTS

    Ingot

    No.

    Silver

    ppm

    Copper

    23(a)

    0.074(b)

    2

    16

    0.076

    3

    12

    0.113

    4

    18

    0.062

    5

    8

    0.099

    6

    10

    0.063

    7

    18

    0.035

    8

    20

    0.070

    9

    18

    0.110

    10

    18

    0.098

    11

    18

    0.159

    12 18

    0.160

    13

    14

    0.119

    14

    16

    0.206

    a)

    Mean, values from 22 ppm to 26 ppm in various

    parts of ingot.

    b)

    Mean, values from 0.051 to 0.093 .

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    4.

    EQUIPMENT

    The pilot scale electro-refining experiments were conducted in a

    multiple cell bank constructed for the purpose. This vessel was 3 feet

    square in plan and 18 inches deep, and was divided by vertical partitions into

    ten cells 18 inches by 7 inches in plan and 18 inches deep. Welded steel

    construction was used and all internal surfaces of the tank were covered by

    epoxy resin reinforced with glass fibre.

    Two copper cathodes, approximately one sixteenth of an inch thick,

    were suspended in each cell compartment with an area 15 inches square

    immersed in the electrolyte. Only five cells were used and these were

    connected electrically in series. The current for electrolysis was obtained

    from a silicon diode rectifier set rated to deliver 50 amperes at 2 volts DC

    from a 240 volt 50 cycle AC input. A variable auto-transformer in the AC

    circuit served to control the rectifier output.

    5 .

    EXPERIMENTAL PROCEDURE AND RESULTS

    5.1

    reliminary

    An experimental pyrometallurgical treatment was begun at Tennant

    Creek by Mr Strong. The procedure is given as described by him in

    Figure 1.

    The metal corresponding to Sample B was cast into an anode and

    electro-refined. Sample C was the cathode deposit.

    Analyses by AMDL of these samples, for copper and silver only,

    are given in Table 3.

    TABLE 3: ANALYSIS OF BISMUTH METAL

    Sample

    opper

    ilver

    PPm

    Pm

    A

    60

    0

    30

    0

    15

    0

    3300

    0

    170

    0

    490

    0

    55

    0

    65

    0

    110

    27

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    5

    Samples G and H, also from Tennant Creek, are respectively

    before and after a cyanide leaching treatment of sponge metal. Samples J

    and K are from a similar experiment conducted at ANIDL.

    In general the following conclusions can be drawn:

    a.

    the copper tends to concentrate in the skimmings

    (Sample D);

    b.

    the sulphur and cyanide flux treatment reduces

    copper appreciably (Samples A-B and D-E);

    c.

    electro-refining following the flux treatment

    produces a metal of purity approaching the required

    level;

    d.

    copper can probably be removed also by cyanide

    leaching of the cemented bismuth sponge before

    smelting.

    5.2

    aboratory Investigations

    5.2.1

    mprovement of Existing Process

    To simulate the existing leaching process, 250 grams of the ore

    sample submitted by Mr Strong was crushed to pass a

    /-inch screen, and

    then leached twice by percolation with the same 500 ml of leach solution.

    This solution contained 10 per cent w/v NaC1 and 4 per cent w/v H

    z

    SO

    4

    . A

    further 100 ml of fresh solution was used as a wash.

    The leach liquor was found by analysis to contain 12.1 grams of

    bismuth per litre. It was divided into three equal parts. Part 1 was

    cemented for 24 hours with sheet steel. Part 2 was cemented for 2 hours

    with 1 gram of bismuth sponge, filtered and then cemented with iron as in

    Part 1. Part 3 was treated with 0.1 gram of sodium sulphide, stirred for

    2 hours, filtered and cemented with iron as in Part 1.

    Cementation with metallic bismuth was expected to remove copper

    from the solution, while the partial sulphide treatment of Part 3 should

    precipitate copper and some bismuth as sulphide. As the amount of metal

    in each experiment was quite small, the bismuth sponge products were

    oxidised to Bi

    2

    03before analysis.

    The results are as follows:

    Cu

    Ag

    Part 1:

    Control only 61

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    6

    5.2.2

    efining of Ingot Metal

    The metal used in the experiments was from an ingot previously

    sampled and found to contain 16 ppm of silver and 0.206 per cent copper.

    This metal was treated by a number of different techniques with the following

    results.

    Simple Electro-refining. A sample of the metal was cast into a sheet 8 inches

    square and approximately 1/4-inch thick. This was electro-refined on to a

    waxed copper sheet at a current density of 10 amperes per square foot. The

    electrolyte contained 50 g per litre HC1, 70 g per litre bismuth (added as

    BiC1 3

    ) and 0.1 g per litre pyrogallol. The electrodes were 11/4 inches apart,

    and the solution was agitated gently. Operating voltage was 0.13 volt.

    The cathode deposit was granular, with a tendency to growth in fingers, but

    adequately adherent. The analyses of this metal indicated 61 ppm copper

    and 3 ppm silver.

    This experiment confirmed that simple refining was not adequate.

    Use of Parkes Process. One hundred grams of metal and 10 grams of

    powdered reagent grade zinc were melted and held at 450

    C for 2 hours with

    occasional stirring. After settling and solidification, the top half of the

    specimen was rejected and the bottom half sampled. A control test without

    zinc was carried out simultaneously.

    The analyses were:

    g

    pan pprr_

    Control

    1

    Experiment

    The results suggest that the zinc treatment was successful in

    removing copper and silver to acceptable limits but, more important, that

    careful settling without zinc was also effective.

    Use of Sulphur Drossing. A sample of metal was fused with 1 per cent of

    its weight of elemental sulphur, using a salt bath for ease of temperature

    control. The melt was skimmed and cast into an anode. The electro-

    refining process described above was carried out and gave a metal containing

    4 ppm copper and 3 ppm silver.

    This technique therefore gave a metal acceptable with regard to

    both copper and silver.

    Cyanide Fluxing. A sample of metal was fused with 1 per cent of its weight

    of sodium cyanide. Some difficulty was experienced and contact was not

    ideal. The treated metal was cast into an anode and refined. Two products

    were collected - one with the electrolyte described above, and the other

    after addition of 75 g per litre of H

    2

    SO

    4

    to the solution. The products

    contained:

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    Product

    With Sodium Cyanide

    ith Sodium Cyanide plus

    H 2 S O 4

    Copper,

    Cu

    15

    ppm

    Copper,

    Cu

    19

    PPm

    Silver,

    Ag

    3

    a)

    ppm Silver,

    Ag

    3

    PPm

    Lead,

    Pb

    0.015 Lead,

    Pb

    0.015

    The cyanide treatment effectively reduced the copper and silver

    concentrations. The addition of sulphuric acid to the electrolyte made no

    difference to the concentration of lead in the products.

    5.3

    iscussion

    The experiments above indicated that simple electro-refining of the

    bismuth ingot metal was not likely to produce a metal to the required

    specification.

    reliminary treatment with sulphur, sodium cyanide or

    metallic zinc, followed by electro-refining, should produce an acceptable

    metal. In the latter case the refining would be necessary to remove zinc

    left in solution in the bismuth. Of these methods, the zinc treatment would

    probably give a lower yield than the others, because of difficulty in separating

    the two metals. The sulphide treatment would give a greater loss of bismuth

    in the skimmings than the cyanide method, and the latter is therefore

    preferred.

    The removal of copper by careful settling was not fully understood,

    and may have been due partly to segregation on cooling. However, it was

    observed in the experimental work that some sulphur was present in the

    ingot material - a sample of skimmings from an ingot was found to contain

    0.2 per cent of sulphur, presumably as copper and bismuth sulphides. This

    probably accounted for copper removal by settling. Use of the method for

    refining is feasible but bismuth losses would be high.

    The presence of the sulphide was noticeable also in the electro-

    refining process. A black crystalline deposit, identified as bismuth

    sulphide, appeared at times on the anode and in the anode sludge. This

    phenomenon was also associated in some way with the appearance of a white

    coating of bismuth oxychloride on the anode in some experiments. This

    coating, if left unchecked, blanketed the anode surface and increased the cell

    voltage to 0.25 volt or higher. Both of these effects are probably associated

    with gradual loss of free acid from the electrolyte.

    At this point a complete refining process could be formulated.

    To check the validity of this proposed process, a separate proving

    experiment was carried out.

    A sample of ingot metal was melted in a steel vessel using as flux

    a mixture of equal weights of sodium hydroxide and sodium cyanide. The

    total weight of flux was 2 per cent of the weight of bismuth. The mixture

    was held at 400-500

    C for 10 minutes with occasional stirring, and then

    allowed to cool slowly. As solidification commenced about 2 per cent of the

    bismuth was skimmed off using a steel gauze and discarded. The bulk of

    the metal was reheated and cast into anodes.

    (a)

    ess than.

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    8

    The anode metal was electro-refined using a hydrochloric acid

    electrolyte containing 70 grams of bismuth, 50 grams of free acid, and

    0.1 gram pyrogallol per litre. Copper cathodes were used and were coated

    with a thin film of paraffin wax to assist in removal of the deposit. The

    current density was 10 amperes per square foot, and the electrolyte was

    agitated gently. No diaphragm or anode bag was used.

    Over a period of 90 hours, 2020 grams of metal was deposited at a

    current efficiency of 94 per cent. In the following 72 hours, 1620 grams of

    metal was deposited at virtually 100 per cent efficiency. Analyses of the

    two deposits, designated A and B respectively, are shown in Table 4 below.

    TABLE 4: ANALYSES OF BISMUTH METAL

    4 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 = 1 = 1 1 1 1 7 1 1 1 1

    Element

    Deposit

    A

    PPm

    Deposit B

    PPm

    Limit

    PPm

    Lead

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    9

    During the whole of this period, metal was deposited on the cathodes

    at high current efficiencies, except in some cases where the deposit on the

    cathodes bridged the space between the two electrodes. When this happened

    the cell was effectively short circuited and refining ceased. In an effort to

    prevent this difficulty glycerol was tried as an alternative to the pyrogallol

    used to modify the character of the deposit throughout the earlier experimen-

    tal work. Little if any improvement was evident. On some occasions the

    weight of metal deposited on the cathodes before the cell became unworkable

    was quite small.

    Removal of the deposit from the cathodes was not difficult but always

    involved some chance of contaminating the product with cathode material.

    The risk was proportionately greater when the cathode deposit was thin and

    refining had been interrupted by bridging of the electrodes.

    No purification of the electrolyte was attempted at any stage, but

    additions of hydrochloric acid were required at intervals to replace acid

    lost by evaporation and by side reactions in the cells. At the completion of

    the run the cathode deposits were melted down using sodium hydroxide flux

    and cast into ingots which were sampled for analysis. Results of the

    analyses are shown in Table 5.

    TABLE 5: ANALYSIS OF REFINED BISMUTH

    Expressed in parts per million

    Ingot Number

    Ag

    Cu As

    Te

    Pb

    Sb

    5 76 2

    40

    10

    2

    9 69

    2

    18

    10

    3 5

    140

    2

    35

    10

    4 6

    99

    2

    15 10

    5

    3

    37

    2

    10 10

    6 2

    3 7

    2

    15

    10

    7

    7

    755

    2

    8

    10

    8

    4

    110

    2

    18

    10

    9 3

    170

    2

    15 10

    10 6

    125

    2

    8

    10

    11

    6

    150

    2

    10

    10

    These analyses indicate that the refined metal was satisfactory in

    all respects except that it contains considerably more copper than is permissible.

    Following the earlier work it was thought that this might be removable by a

    skimming technique. Accordingly all of the refined metal was re-melted

    using caustic soda flux, and small amounts of skimmings were taken as the

    metal solidified. These skimmings were kept separate, the bulk of the metal

    being re-heated and cast again into ingots. Results of the analysis of these

    ingots for copper are given in Table 6.

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    TABLE 6: ANALYSIS OF SKIMMED BISMUTH

    Expressed in parts per million

    Ingot Number

    Cu

    1070

    2 320

    3 290

    4

    440

    5

    750

    6

    500

    7

    460

    8

    260

    9

    670

    Results of this operation were disappointing in that the amount of

    copper had increased rather than decreased. The increase may have been

    due in part to sampling errors but was almost certainly caused largely by

    contamination from an unidentified source. Clearly the metal was still

    unsatisfactory.

    At this stage a sulphur drossing technique was used to reduce the

    copper content of the bismuth. The ingot material was melted once again

    using sodium hydroxide flux and, while molten, the metal was treated with

    elemental sulphur. The weight of sulphurused was 1 per cent of the weight

    of the metal in any given melt and it was added slowly with stirring to the

    bismuth. The molten metal was then allowed to cool, was skimmed, re-

    heated, and recast into ingots. Results of further analyses are given in

    Table 7.

    The amount of copper present was then well within the specified

    limit with the exception possibly of the ingot designated 9A. However, other

    ingots were so far below the limit that the metal could all be considered

    satisfactory after a single blending operation.

    The weights of finished refined metal, skimmings, and crude

    residual metal were respectively 214, 6 and 34 pounds. While the overall

    yield could be regarded as poor, considerable quantities of bismuth were

    discarded at various stages of the operation because it was considered that

    recovery would cost appreciably more than the value of the recovered metal.

    In practice excellent yields of metal should be possible.

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    TABLE 7: ANALYSIS OF DROSSED METAL

    Ingot Number

    u

    eight of Ingot

    PPm

    b

    lA 5

    24

    2A

    16

    24

    3 A

    8

    20

    4A

    20

    21

    5 A

    17

    19

    6A

    17

    21

    7A

    22 20

    8 A

    15

    201/2

    9 A

    5 9

    221/2

    10A

    20

    221/2

    7.

    ISCUSSION

    The investigation was restricted in scope as the original request

    was for development of an electro-refining process. The experimental work

    demonstrated clearly that a simple electro-refining process was not capable

    of producing metal of the required purity. Consequently a combination

    process was developed in which pyrometallurgical steps were combined with

    electro-refining to produce pharmaceutical grade bismuth. The overall

    process has been used to refine substantial quantities of metal and has been

    shown to be effective.

    In spite of the reasonable results which were obtained from the

    refining process, electro-refining can scarcely be considered a satisfactory

    refining process in the present context. Its inability to remove certain

    impurities and the possibility of impurity build-up in the electrolyte with

    subsequent falling-off in efficiency of refining are strong arguments against

    a process of this type. Control of the nature of the cathode deposits by use

    of various additives to the electrolyte is an art rather than a science. With

    experience a satisfactory technique could probably be developed. However,

    there seems to be an inherent weakness in any process which involves

    plating of metal on to a cathode of material which would be an undesirable

    contaminant in the product. Removal of the deposits from the copper

    cathodes was relatively easy but when the copper specification is so stringent

    the danger of contamination beyond the specified limit is always present.

    Possibly this could be averted by use of an alternative cathode material.

    With further development, use of bismuth cathodes may be feasible but this

    has not been attempted in the present investigation. However, it is consid-

    ered that a pyrometallurgical process along conventional lines using such

    operations as sulphur drossing, skimming, partial oxidation, chlorination

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    12

    and so on, could give metal of an acceptable quality rather more simply than

    the refining processes described above. Nevertheless it has been shown

    that a dombination process employing sulphur drossing, skimming and electro-

    refining can produce pharmaceutical grade bismuth from crude metal

    produced in the Tennant Creek area.

    8.

    EFERENCES

    1.

    CATHRO, K. J., and KOCH, D. F. A., Recovery of Bismuth from

    Chalcopyrite Calcines , paper presented at the A. I. M. M.

    Hydrometallurgy Symposium, Adelaide, February, 1960.

    See also Aust. J. App. Sci. 13, (3) 175 (1962).

    2. GRUZENSKY, P. M., and CRAWFORD, W. J., U. S. Bureau of

    Mines, Report of Investigation 5182.

    3.

    ERN, E. F., and JONES, T. R., Trans. Amer. Electrochem.

    Soc. 57, 255 (1930).

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    FIGURE

    1

    EXPERIMENT L

    PYR ONIE:r Al L LIR GIG AL

    ReprrmETN

    Crude Metal

    Skim at 600

    Metal

    Ximmings

    Sample

    A

    ample I:1

    Flux with Sulphur

    LM

    with ulphwr

    Cy

    anide

    I

    i

    Metal

    5arrtpla

    E

    Flux with 7 inic

    aizeP

    hen Sulphur and Cyan ide

    1

    Flux Discarded

    etal

    Sa.rnple

    F

    and Cyanide

    and

    Metal

    Flux Flux

    Sa mole

    1 3

    b rd

    Disc an:led

    Z G

    PR e_h