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17th
European Biosolids and Organic Resources Conference
www.european-biosolids.com
Organised by Aqua Enviro Technology Transfer
COMMISSIOINING OF ENHANCED ENZYMIC HYDROLYSIS AT LANCASTER WwTW
Leach, K.1 and Edgington, R.M.2 1United Utilities PLC, 2 United Utilities,
Corresponding Author Tel. 01925 237000 Email [email protected]
Abstract
Lancaster sludge treatment centre treats the indigenous and imported sludges from the
surrounding area. In 2011, an enhanced enzymic hydrolysis plant (EEH) was commissioned in
front of the existing mesophilic digesters. The plant is designed to treat 7080tdspa and to meet
an enhanced treated quality standard.
This paper will discuss the design, commissioning and the performance of the EEH plant and the
key lessons learned.
Keywords
Enhanced Enzymic Hydrolysis, Safe Sludge Matrix, CHP, log kill, E.Coli, Digestion
Enhanced Enzymic Hydrolysis
In the UK, the main advanced digestion processes are Enhanced Enzymic Hydrolysis (EEH) and
thermal hydrolysis (TH) to produce an enhanced treated sludge. EEH, consists of Stage 1 (three
reactors in-series at 32-42OC), followed by Stage 2 (one heating reactor, and two holding tanks
all at 55OC), before feeding into the parallel operated mesophilic anaerobic digester (MADs).
This is shown in Figure 1
420C
Figure 1: Process Flow Diagram of conventional EH and EEH (Le et al 2007)
17th
European Biosolids and Organic Resources Conference
www.european-biosolids.com
Organised by Aqua Enviro Technology Transfer
The first EEH plant was installed at United Utilities Blackburn WwTW in 2005 and showed a
volatile solids destruction (VSd) of around 55% and excellent E.Coli destruction (Le 2006). Later
plants have been installed at Cambridge (2007), Kings Lynn (2008), Great Billing (2009) and Eign
(2009) (Bungay 2008); the same paper gives details on their design. The sites show a VSd of
about 50 to 55% (Asaadi 2008, Riches 2012). With greater VSd than conventional mesophilic
anaerobic digestion, more biogas is produced which leads to greater energy generation
potential; at Kings Lynn 0.75MWh/TDS is generated (Riches 2012).
Heating in stage 1 has always been by hot water heat exchangers. Initially, heating in stage 2
was obtained using hot water heat exchangers. However, more recent plants from Kings Lynn
onwards have used direct steam injection into the sludge to reduce the risk of viviantite scaling
(due to Iron salts being used to remove phosphorous on the treatment works).
Design Parameters of Lancaster EEH Plant
Lancaster WwTW serves a population equivalent of circa 100,000. The works is a conventional
carbonaceous activated sludge plant followed by nitrifying tricking filters. The indigenous co-
settled sludges, along with imported sludges, were processed with strain presses, thickened on
gravity belt thickeners and digested in three MADs followed by secondary digesters and
operational storage. The works is unusual in that the imported sludges are discharged at a
remote tanker terminal (2 miles away, due to poor vehicle access on narrow country lanes) and
then pumped to the works.
In 2008, design commenced on the provision of an EEH plant, prior to the MADs, to meet the
sludge quality driver for the enhanced sludge standard to meet:
• 6 log kill in E.Coli
• Less than 1000 E.Coli No/gDS
• Absence of Salmonella in 2gDS
Initially the plant was design to treat 7080tdspa (equating to 370m3/d), an increase of the then
current sludge make up of 6490tdspa. The increase was due to a growth in population in the
Lancaster catchment and in imported sludges that would be Iron dosed for P removal. This then
gave six EEH reactors each with a sludge working volume of 270m3 each. However, during the
design period, the Price Review 2009 was underway and that had an impact on the scheme, as
the provision of Iron dosing for P removal at Lancaster itself and transfer of Settle WwTW
sludges for treatment at Lancaster had to be taken into consideration. Although the Price
Review sludge figures were very provisional at circa 8300tdspa, it was agreed that the design of
the EEH plant would be flexible to take into account any future approved sludge figures. This
was simply done by increasing the height of each reactor, thus increasing their sludge working
volume to 370m3 each, giving the plant a potential maximum throughput of 492m3/d. Also,
within the layouts, allowances were made for an additional EEH reactor for future expansion.
No additional treatment processes were required at Lancaster and the final process flow
diagram for sludge treatment is shown in Figure 2.
17th
European Biosolids and Organic Resources Conference
www.european-biosolids.com
Organised by Aqua Enviro Technology Transfer
Figure 2: Process Flow Diagram of Lancaster Sludge Treatment Centre
Iron dosing for P removal is a future requirement for Lancaster WwTW and is already practiced
at the feeder works. Based on this, it was decided that direct steam injection would be used for
the second stage heating to reduce the risk of viviantite formation.
Details of Lancaster EEH Plant
The contract was delivered by United Utilities Process Alliance Partners South. Due to the cost of
the project, the scope book was divided into four major sub contract areas; Siloxane removal
system, EEH plant, CHP kit Framework and Steam & Hot Water Plant.
Key project deliverables:
• The EEH plant comprising of 6 No. clad & thermally insulated reactor vessels, access
platform and stairway. 1st& 2nd stage sludge heating / circulation systems and a 3rd
stage air blast cooling system.
• New 525kW CHP packaged system.
• New boiler building, two steam generating boilers and ancillary equipment
• New boiler fuel oil storage tank and oil transfer pumps
• Gas booster system complete with duty / standby gas compressors
• Modification to existing digester / EEH feed pumping system
• New pumps & modifications to existing Digester hot water pumping system pipe-
work
• New Siloxane removal plant and coalescing chimney stack.
• New instrument air compressors in kiosk.
GBT's
2 off
Primary
Digesters
3 off
Poly
Secondary
Digesters 6 off
Operating
Storage
Tanks 4 off
Sludge
holding
Wash water
Enhanced
Enzymatic
Hydrolysis
Post
Screening
MBT's
4 off
Co-settled sludge
from PST
Sludge to land
Imports
S
C R E
E
N
Pre Screens
sludge
holding Tank
2 Import
Tanks
FiltrateGas Accumulator
Returns to
head of works CHPFlare Sludge
Storage
Tank
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• New process water storage tank and booster pumps in kiosk.
• Modifications to the existing and the introduction of new HV and LV electrical
services
Figure 3: Lancaster EEH
Commissioning
The original design of the EEH plant was based upon the maximum processing capability of 492
m³/d. During early commissioning meetings, it became apparent that those quantities of sludge
would not be available, as the daily site sludge production approximately 300m3/d. it was
therefore decided that the system would be modified to accommodate a maximum of 400m³/d
to enable commissioning. Reducing the available sludge capacity would increase the retention
time and increase the risk of foaming within the reactors and the digesters. The EEH plant
throughput was reduced, by isolating reactor No.1, allowing the remaining reactors to operate
at design levels for the commissioning period. Site operations began to store sludge in the
upstream process to enable the required sludge flow rates during commissioning.
Following wet testing the reactors were drained and dried before indigenous sludge was
introduced. Sludge feed was alternated every 30 minutes between the MADS and EEH to sustain
the output of the digestors during this period.
17th
European Biosolids and Organic Resources Conference
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Organised by Aqua Enviro Technology Transfer
Imported enhanced treated sludge was not used to seed the EEH process as the project output
was not reliant on producing an enhanced sludge product immediately, this would be claimed
following the completion of the future dewatering project.
Transfer of sludge commenced on the 10th Jan 2011, and filling took approximately 5 days. The
EEH plant was then re-commissioned without heating stage 1 or stage 2. Heating was applied to
both the first stage in the form of hot water and the second stage in the form of steam on the
31st January 2011. The sludge temperatures at the two main stages of the process were now
raised to the required set points of 42oC and 55oC.
Six weeks after operating on indigenous sludge a number of the sludge feed and recirculation
pumps failed due to damage to the internal pump lobes. These pumps failed before the first
scheduled inspection date. The Ethylene Propylene Diene Monomer (EPDM) coated lobes were
replaced with a Natural Buna Rubber (NBR) lobes more suited to the fine grit particles
associated with the coastal location of the site. See Figure 4
Figure 4: Damaged EPDM Sludge Pump Lobes
EEH outlet pathogen monitoring commenced shortly after the commencement of heating to
stage 1 and stage 2. The destruction of E.Coli and Salmonella was gradual as the temperature
increased and first fill of sludge was displaced from the EEH as can be seen in Figure 5.
17th
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The EEH plant first achieved a reduction in E.Coli of <1000 No/gDS and destruction of
Salmonella, monitored as Presence/Absence(PAB) approximately 10oC lower than the second
stage temperature setting of 55oC .
With reactor No.1 isolated and low sludge volume, foaming within the EEH reactors became an
issue due to increased retention time. Prior to the project anti-foam was dosed on the MAD
sludge feed line as it exited the GBT building, however this had been bypassed to allow for
installation of the EEH plant. Foaming within the sealed EEH reactors was not a problem;
however this caused foaming in downstream digesters, which required the reintroduction of
anti-foam dosing. Anti-foam was initially slug dosed via the EEH s, but this was later improved by
adding an automated system that dosed into the MAD sludge feed pipe work when transferring
sludge from the EEH, based on the detection of foam levels within the MAD’s.
0
500000
1000000
1500000
2000000
2500000
01/02/2011 00:00 06/02/2011 00:00 11/02/2011 00:00 16/02/2011 00:00 21/02/2011 00:00 26/02/2011 00:00
E.C
oli N
o./g
DS
0
0.2
0.4
0.6
0.8
1
1.2
Salm
on
ell
a P
AB
's
E.Coli Salmonella PABs
Figure 5: EEH E.Coli start up performance
Pathogen Performance
Performance Test 1
The EEH performance test was undertaken between the 14th February and 14th March 2011
returned good E.Coli destruction, all counts were below the scope book requirements of <1000
No/gDS, with significant numbers of zero detection. However the plant failed to regularly
achieve the required log kill stated in the project requirements of 6 log reduction see figure 6.
17th
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Steam plant failures on a number of days caused delayed batches, but temperature
performance was maintained. Detailed investigation of the plant did not identify any further
operational issues or defective equipment, the sampling procedure was considered to be the
most likely cause of higher than expected E.Coli detections.
0.00
1.00
2.00
3.00
4.00
5.00
6.00
7.00
8.00
9.00
11/02/2011 16/02/2011 21/02/2011 26/02/2011 03/03/2011 08/03/2011 13/03/2011 18/03/2011 23/03/2011
E.C
oli L
og
Kill
Figure 6: Performance Test 1 E.Coli and Salmonella Data 14th
February and 14th
March
2011
Performance Test 2.
The performance test was repeated and sampling procedures were reviewed to elimate any
possible sources of cross contamination. The log kill performance proved difficult to achieve due
to a low Log of E.Coli in the EEH feed sludge. Average feed count was 6.37 Log, with a 2.38 Log
on average at the outlet of the EEH plant for the duration of performance test. With such a low
level of E.Coli in the feed sludge, near zero detection of E.Coli would be needed to achieve the
enhanced treated sludge standard of 6 log reduction. Although the E.Coli performance remained
below 1000 E.Coli No/gDS for the majority of the test, E.Coli numbers monitored at the EEH
outlet increased and were now typically around 220-250 No/g/DS compared to large numbers of
zero detection observed in the first test. There were also a number of detections above the
1000 No/gDS E.Coli target that also couldn’t be explained. Once again no evidence of defective
equipment or control issues were identified that may have lead to the decline in performance
since the early test.
Salmonella performance monitored as Presence /Absence (PABS) at the outlet of the EEH has
remained consistent with zero detection on all but 4 samples since the plant reached the
17th
European Biosolids and Organic Resources Conference
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required temperature set points. As the required testing method used is not quantitative it is
not possible to ascertain a conclusive correlation between E.Coli and Salmonella destruction.
Compliance sample point
Following the failure of the 1st and 2nd performance tests, the EEH sample point was questioned
as a possible contamination source. It was thought that the detection of E.Coli may be
attributable to contamination from stagnant sludge that remained in and around the sample
pipe work and sample point. Due to limited drainage within the vicinity of the EHH plant it was
difficult to flush the sample tap sufficiently to ensure a representative sample. A new sample tap
was installed, with a sludge drainage point that allowed flushing of the sample pipework prior to
sampling. Figure 8.
Following installation of the new sample tap and incorporation of sampling technique based on
the EA sludge sampling best practice (EA 2003) an intensive sampling programme was
undertaken. However there was no improvement in the number of E.Coli detected.
Microbiological swabs taken from the old and new sample points prior to sampling and in all
cases returned zero detection of E.Coli. Thus the initial thought of contamination with old sludge
was disproved.
Figure 8: New EEH Outlet Sample Point
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Steam Injector
Whilst undertaken a training demonstration on the removal and inspection of the steam injector
in June 2012, significant damage to the steam injector lance and lance assembly pipe work was
discovered. A rupture had perforated the end of the lance within the location of the steam
injection ports. (Figure 11). The lance is precision machined from high grade stainless steel and
inserted inline with the flow of sludge on the recycle pipework of reactor 4 .
Steam is dosed at constant pressure of 6.4bar and pasteurises the sludge while also providing
heating to stage 2 sludge as it is re-circulated through reactor 4. The steam exists radially
through a number of steam ports to ensure uniform exposure to the sludge. It is thought that
following the rupture of the lance, the reduction in back pressure would have resulted in the
steam taking a preferential route from the damaged area, preventing adequate pasteurisation,
and possibly accounting for the drop in E.Coli performance across the EEH.
Due to the absence of specific data monitoring for the volume and pressure of steam delivered,
it is impossible to ascertain when the lance failed. On installation of the replacement injection
lance, a rigorous inspection schedule will be implemented. Performance testing will also be
undertaken on the EEH plant to ascertain if the sub-optimal steam injection was accountable for
the reduced E.Coli performance during the initial testing phase.
Figure 11: Steam Injector Lance Damage
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Process Performance
Volatile Solids Destruction
Sludge feed to the EEH is on average 5.42 %DS with a range of between 2.7 – 11.7%DS based on
data collected from site. The plant achieves a Volatile solids destruction (VSd) of around 55%
which is in consistent with the hydrolytic model proposed by Le et al (2007). Figure 9 shows the
Lancaster VSd plotted against Le’s model with comparable results particularly against the other
UU EEH site at Blackburn. Lancaster has seen an increase in VSd from 41% to 55% on
commissioning of the EEH plant upstream of the existing mesophilic digesters, with associated
improved gas yield and post digestion settle-ability.
0%
10%
20%
30%
40%
50%
60%
70%
0 5 10 15 20 25
Retention time (d)
Vo
latile
so
lid r
ed
uctio
n
EH +MAD Blackburn MAD Lancaster Bromborough EH1 Asaadi et al 2011 EH1 Asaadi et al 2011 EEH Asaadi et al 100% Primary. WEF 1998 50% Primary. 50% WAS. WEF 1998 100% WAS. WEF 1998
Figure 9: Hydrologic model Le et al (2007) inclusive of Lancaster Plot
Gas Production and Mixing
Reduction in sludge throughput since completion of commissioning has lead to increased
foaming, difficulties in maintaining digester temperature and erratic gas production. Average
gas production is 276 m3/hr. Operational savings were calculated upon a throughput of 370m3/d
but average throughput since project completion is 270-290m3/d. Sludge throughput has not
increased as expected, the plant has yet to export electricity, although increasing sludge imports
from other sites is being developed through the future development of a cake re-liquidization
project.
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Methane gas composition monitored at the feed to the two CHP engines is typically 63-65%.
During commissioning the newer 525kW CHP engine was prone to Lean Oxygen (Lenox) failures
caused by poor gas mixing. Gases from the EEH plant contain predominately CO2, gas should
have mixed sufficiently with the bio gas from the digesters prior to the CHP, however due to the
Siloxane removal plant not being commissioned and thus bypassed due to safety issues at other
site, the initial gas feed to engines contained high composition of CO2 resulting in a number of
Lenox fails. The EEH gas was rerouted to improve blending with the biogas, Lenox operation has
been further improved by maintaining a more consistent mixing regime in the EEH Reactors and
widening the tolerance band of the new CHP engine inline with the existing plant 323 kW CHP
engine. The presence of a gas bag would have insured homogenous gas mixing but due to
project constraints was excluded from the scope of the project.
Sludge Dewaterability
The selected option for the forthcoming Sludge Cake Project is the installation of 3 No. Belt
Presses. A belt press trial undertaken on Lancaster EEH sludge produced cake dry solids reliably
around 25%DS, this is comparable with dry solids of 23-26% obtained at sites with EH and EEH
pre-treatment and centrifuge equipment reported by Asaadi et al 2011. Following the
completion of the EEH project operations observed improved settleability within the operational
storage tanks. Sludge is stored in open tanks prior to export, on settlement the supernatant is
decanted and returned to the head of the works. Improved settlability has seen a reduction of
£110K in transport sludge to land transport costs, a reduction which will be further increased
with the completion of the sludge cake project.
Current Performance
The plant has not been able to match the earlier E.Coli destruction witnessed during the initial
performance test. The identification of the steam injector issue discussed in the paper is one
explanation for the deterioration in performance. While the reduction in sludge throughput
shouldn’t had resulted in reduced E.Coli performance it was significantly different to the flow
rates undertaken during the initial performance trial. Following the commissioning period,
sludge throughput reduced from 400m3/day to 270-290m3/day thus increasing retention time
within the reactors. The plant was unable to sustain the required throughput of sludge, which
resulted in the EEH plant holding batches and failing to feed the digestors for a number of days.
This issue is further compounded by the plant only taking sludge imports on week days.
Consistent running of the EEH plant although at lower throughput provides a steady feed rate
to the digesters resulting in a more consistent gas supply and mixing of bio-gas for the CHP
engines. Operational changes to sludge throughput are now limited to ±10% flow change.
Conclusion
• The plant achieves the enhanced sludge standard by meeting the MAC <1000 E.Coli
No/gDS , due to the low E.Coli in the feed sludge being below the guidance values the
log kill is not considered for compliance. Following completion of the sludge cake
project, the end product will be re-validated as an enhanced product.
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• Volatile solids reduction of 55% is achieved, resulting in improved gas production,
improved post digestion settleability and is consisted with previously reported values.
• Cake solids of 25% from belt presses are comparable with those attained from other EH
and EEH sites using centrifuge technology. Assadi et al 2011
• Investigations and monitoring are ongoing to identify the cause of the damage to the
steam injector and the potential impact this had on E.Coli destruction across the EEH.
• Increased sludge imports and inclusion of Ferric dosing on site will increase processed
sludge volume to maximise the efficiency of the EEH plant and realise the full electricity
export potential of the new 525kw CHP engine.
Acknowledgements
The author would like to thank the site team at Lancaster WwTW and the project team for there
assistance, time and knowledge that was invaluable in the production of this paper.
References
Asaadi, M. (2008). Review of the Performance of an Advanced Digestion. Presented at 13th
European Biosolids and Organic Resources Conference. Aqua Enviro, Leeds.
Bungay, S. and Abdelwahab, M. (2008). Monsal Enzymic Hydrolysis – New Developments and
Lesson Learnt. Presented at 13th
European Biosolids and Organic Resources Conference. Aqua
Enviro, Leeds.
Le,S. et al (2006). Enzymic Hydrolysis Technology Demonstration – Production of Enhanced
Treated Biosolids for Agricultural Recycling. . Presented at 11th
European Biosolids and Organic
Resources Conference. Aqua Enviro, Leeds.
Riches, S. et al (2011) Advanced Digestion in Anglian Water – Summary of AMP4 Delivery
Experience and AMP5 Delivery Plan. Presented at 16th
European Biosolids and Organic Resources
Conference. Aqua Enviro, Leeds.
Environment Agency (2003). The Microbiology of Sewage Sludge (2003) - Part 2 - Practices and
procedures for sampling and sample preparation. Bristol